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HomeMy WebLinkAboutNC0004774_Special Order By Consent_20180713 { 3 NORTH CAROLINA ENVIRONMENTAL MANAGEMENT COMMISSION COUNTIES OF ROWAN AND STOKES IN THE MATTER OF ) NORTH CAROLINA ) SPECIAL ORDER BY CONSENT NPDES PERMITS NC0004774 & ) NC0024406 ) EMC SOC WQ S 18-004 ) HELD BY ) DUKE ENERGY CAROLINAS, LLC ) Pursuant to the provisions of North Carolina General Statutes (G.S.) 143-215.2, this Special Order by Consent is entered into by Duke Energy Carolinas,LLC,hereinafter referred to as Duke Energy, and the North Carolina Environmental Management Commission, an agency of the State of North Carolina created by G.S. 143B-282, and hereinafter referred to as the Commission. Duke Energy and the Commission are referred to hereafter collectively as the "Parties." 1. Stipulations: Duke Energy and the Commission hereby stipulate the following: a. This Special Order by Consent("Special Order") addresses issues related to the elimination of seeps (as defined in subparagraphs e, f, and g below) from Duke Energy's coal ash basins during the separate and independent process of basin closure under the Coal Ash Management Act, G.S. 130A-309.200 through 130A- 309.231 ("CAMA") and the Federal Coal Combustion Residuals Rule,40 CFR Parts 257 and 261. The Environmental Protection Agency first directed permitting authorities to consider potential impacts on surface water of seeps from earthen impoundments in 2010. At that time, Duke Energy began discussions with the North Carolina Department of Environmental Quality("the Department")regarding seeps at multiple Duke Energy facilities,including identifying certain seeps in permit applications and providing data to the Department regarding seeps. In 2014, Duke Energy provided a comprehensive evaluation of all areas of wetness and formally applied for NPDES permit coverage of all seeps. Since 2014, Duke Energy has performed periodic inspections and promptly notified the Department of new seeps and sought NPDES permit coverage where appropriate. On March 4, 2016, the Department issued Notices of Violation ("NOVs")to Duke Energy related to seeps. EMC SOC WQ S18-b04 Duke Energy Carolinas, LLC p. 2 Decanting (i.e., removal of the free water on the surface of the coal ash basins), which is required before ash basins can be closed, is expected to substantially reduce or eliminate the seeps. In order to accomplish this goal of substantially reducing or eliminating seeps, this Special Order affords certain relief to Duke Energyrelated to the non-constructed tructed see s (as defined in subparagraphs f and g below), while requiring Duke Energy to accelerate the schedule for decanting as specified more fully below. Constructed seeps (as defined in subparagraphs e and f below) will be addressed in the NPDES permits. After completion of decanting, for any remaining seeps, whether constructed or non-constructed, Duke Energy must take appropriate corrective action as specified more fully below. b. Duke Energy has been issued North Carolina NPDES permits for operation of an existing wastewater treatment works at each of the following coal fired, electric generation facilities ("Duke Energy Facilities," or in the singular, "Facility"): Permit Issuance Receiving Water Facility Number County for Primary Date Outfall Buck NC0004774 Rowan 12/02/2011 Yadkin River Belews Creek NC0024406 Stokes 10/12/2012 Belews Lake and Dan River c. The Duke Energy Facilities listed above will continue to operate. The coal-fired generation units at Buck have been retired and replaced with a natural gas fired combined cycle. The Belews Creek facility will continue to operate coal fired generation units and generate coal ash. Each Facility is subject to the provisions of this Special Order. d. Wastewater treated at coal-fired electric stations includes water mixed with ash produced through the combustion of coal for the steam generation process. Ash is controlled and collected through the use of water, creating a slurry that is conveyed to impoundments or basins with earthen dike walls. In the ash basin, the solids separate from the liquid portion, with the resulting supernatant discharged under the terms of the NPDES permit. EMC SOC WQ S 18-004 Duke Energy Carolinas,LLC P- 3 e. The coal ash basins at the Duke Energy Facilities are unlined, having no impermeable barrier installed along their floors or sides. Earthen basins and dike walls are prone to the movement of liquid through porous features within those structures through a process known as seepage. Each of the Duke Energy Facilities covered by this Special Order exhibits locations adjacent to, but beyond the confines of, the coal ash basins where seepage of coal ash wastewater from the coal ash basins may intermix with groundwater, reach the land surface (or "daylight"), and may flow from that area. Once such seepage reaches the land surface, it is referred to as a "seep." Each of the seeps identified at the Duke Energy Facilities and addressed in this Special Order exhibit some indication of the presence of coal ash wastewater. Both (a) confirmed seeps and (b) areas identified as potential seeps that were later dispositioned, are identified in Attachment A. f. Some of Duke Energy's coal ash impoundments contain constructed features on or within the dam structures (such as toe drains or filter blankets) to collect seepage. This wastewater is conveyed via a pipe or a constructed channel directly to a receiving water. These discrete, identifiable,point source discharges are or will be covered and regulated by the respective NPDES permits and designated as outfalls therein. The characteristics of these wastewater flows are similar to those discharging from other permitted outfalls for ash basin effluent. In this Special Order, seeps that are(1) on or within the dam structures and(2) convey wastewater via a pipe or constructed channel directly to a receiving water are referred to as "constructed seeps." Seeps that are not on or within the dam structure or that do not convey wastewater via a pipe or constructed channel directly to a receiving stream are referred to as "non-constructed seeps." g. Non-constructed seeps at the Duke Energy Facilities often exhibit low flow volume and may be both transient and seasonal in nature, and may, for example, manifest as an area of wetness that does not flow to surface waters, a point of origin of a stream feature, or flow to an existing stream feature. These circumstances of the non-constructed seeps make them difficult to discern, characterize, quantify and/or monitor as discrete point source discharges. This creates challenges in permit development and compliance monitoring because it is difficult to accurately monitor for flow and discharge characterization. Non- constructed seeps at the Duke Energy Facilities present significant challenges to their inclusion in NPDES permits as point source discharges,but they do cause or contribute to pollution of classified waters of the State. Therefore, these non- constructed seeps are addressed in this Special Order rather than in an NPDES permit. EMC SOC WQ 5181004 Duke Energy Carolinas,LLC p.4 h. A subset of these non-constructed seeps at the Duke Energy Facilities do not flow directly to surface waters, but flow to some portion of an NPDES permitted wastewater treatment system. In such instances, the seeps may be referenced in NPDES permits as contributing flow to a permitted outfall. Any non-constructed seep that falls within this subset is identified in Attachment A by the following statement in its description: "This non-constructed seep flows to a portion of an NPDES wastewater treatment system." Investigations and observations conducted by the Department and U. S. Army Corps of Engineers staff have concluded that some seeps emanating from Duke Energy's coal ash ponds create and/or flow into features delineated as classified waters of the State or Waters of the United States. j. Collectively, the volume of non-constructed seeps is generally low compared to the volume of permitted wastewater discharges at the Duke Energy Facilities. k. In 2014, Duke Energy conducted a survey of each coal-fired electric generation station to identify potential seeps from the coal ash surface impoundments. Duke Energy included all areas of wetness identified around the impoundments as seeps, and submitted applications to include those seeps in NPDES permits. Beginning in 2015, Duke Energy has implemented semi-annual surveys to identify new seeps in the vicinities of the coal ash basins. Additional seeps have been observed and documented during these surveys and reported to the Department pursuant to a Discharge Identification Plan mandated by CAMA. Additional investigation has determined that not all of areas identified in 2014 are seeps, but each Duke Energy facility does have multiple seeps. 1. The Department issued NOVs to Duke Energy on March 4, 2016 for the seeps that emanate from the unlined coal ash surface impoundments at the Duke Energy Facilities. m. Non-constructed seeps create conditions such that certain surface water quality standards may not consistently be met at all Duke Energy monitoring sites. n. The presence of coal ash influenced water in the non-constructed seeps causes or contributes to pollution of the waters of this State, and Duke Energy is within the jurisdiction of the Commission as set forth in G.S. Chapter 143, Article 21. EMC SOC WQ S18-004 • Duke Energy Carolinas,LLC P. 5 o. A list of seeps identified in the vicinities of the coal ash surface impoundments at the Buck and Belews Creek plants, as well as their locations, and the bodies of water those seeps may flow into (if applicable), can be found in Attachment A to this Special Order. P. Duke Energy must close the coal ash surface impoundments at all North Carolina coal-fired electric generating stations in accordance with applicable requirements set out in CAMA and the Federal Coal Combustion Residuals Rule, requirements of which are independent of the resolution of seeps addressed in this Special Order. q. Decanting of wastewater performed at Duke Energy's coal ash basins is expected to eliminate or substantially reduce the seeps from the ash basins at the Duke Energy Facilities. r. Since this Special Order is by consent, the Parties acknowledge that review of the same is not available to the Parties in the N.C. Office of Administrative Hearings. Furthermore, neither party shall file a petition for judicial review concerning the terms of this Special Order. 2. . Duke Energy, desiring to resolve the matters causing or contributing to pollution of the waters of the State described above, hereby agrees to do the following: a. Penalties 1) Upfront Penalty. As settlement of all alleged violations due to seepage at these Duke Energy Facilities, pay the Department, by check payable to the North Carolina Department of Environmental Quality, a penalty in the amount of$84,000, calculated based upon $12,000 each for two constructed seeps identified prior to January 1, 2015 and$6,000 each for ten non-constructed seeps identified prior to January 1, 2015. A certified check in the amount of$84,000.00 must be made payable to the Department of Environmental Quality and sent to the Director of the Division of Water Resources (DWR) at 1617 Mail Service Center, Raleigh, North Carolina 27699-1617 by no later than thirty(30) days following the date on which this Special Order is approved and executed by the Commission, and received by Duke Energy. EMC SOC WQ S181004 Duke Energy Carolinas,LLC p. 6 No penalty shall be assessed for seeps identified after December 31, 2014, given Duke Energy's inclusion of seeps in permit applications and compliance with the Discharge Identification Plan required under CAMA. By entering into this Special Order, Duke Energy makes no admission of liability, violation or wrongdoing. Except as otherwise provided herein,1 payment of the upfront penalty does not absolve Duke Energy of its responsibility for the occurrence or impacts of any unauthorized discharges in the area of the Duke Energy Facilities that may be discovered in the future, nor does the payment preclude DWR from taking enforcement action for additional violations of the State's environmental laws. 2) Stipulated Penalties. Duke Energy agrees that unless excused under paragraph 5, Duke Energy will pay the Department,by check payable to the North Carolina Department of Environmental Quality, stipulated penalties according to the following schedule for failure to perform activities described in paragraphs 2(b, c, and d), or for failure to comply with interim action levels listed in Attachment A. Failure to meet a deadline in the Compliance $1,000.00/day for the first seven Schedule in 2(b) of this Special Order days; $2,000.00/day thereafter Failure to meet any other deadline in this $1,000.00/day for the first seven Special Order days; $2,000.00/day thereafter Exceedance of an interim action level listed in Attachment A $4,500.00 per monitored exceedance Monitoring frequency violations $1,000.00 per violation Failure to submit, within 210 days of the completion of decanting at each Facility, adequate amendments to groundwater Corrective Action Plans or Closure Plans to $5,000.00 per day, to a maximum of address all remaining seeps, whether $1,000,000.00 per electric generating constructed or non-constructed, through facility. corrective action as applicable under paragraph 2(d) of this Special Order.2 1 See especially paragraph 2(a)(2) excepting newly identified seeps from future penalties under certain conditions. 2 Failure to adequately implement any amended Corrective Action Plan or Closure Plan will be handled in the normal course. EMC SOC WQ S18-004 Duke Energy Carolinas,LLC P. 7 As long as Duke Energy remains in compliance with the terms of this Special Order, as well as CAMA and conditions of any approvals issued thereunder, the Department shall not assess civil penalties for newly identified seeps. b. Compliance Schedule. Duke Energy shall undertake the following activities in accordance with the indicated time schedule. No later than fourteen (14) calendar days after any date identified for accomplishment of any activity, Duke Energy shall submit to the Director of DWR written notice of compliance or noncompliance therewith. In the case of compliance, the notice shall include the date compliance was achieved along with supporting documentation if applicable. In the case of noncompliance, the notice shall include a statement of the reason(s) for noncompliance,remedial action(s)taken, and a statement identifying the extent to which subsequent dates or times for accomplishment of listed activities may be affected. Duke Energy shall accelerate compliance with the requirements of G.S. 130A- 309.210(d) and(f) such that all projects necessary to eliminate discharges of stormwater into the surface impoundments at the Duke Energy Facilities and to convert to dry bottom ash handling shall be complete prior to the deadline for initiating decanting set out below. 1) Complete dry ash handling projects in accordance with the following schedule Facility Fly Ash Bottom Ash Belews Creek Complete 9/30/2018 2) Initiation of Decanting Buck 3/31/2019 Belews Creek 3/31/2019 3) Completion of Decanting Buck 3/31/2020 Belews Creek 9/30/2020 This schedule is premised upon timely issuance of necessary permits or approvals, and no requirement imposed by DWR to implement physical/chemical treatment during decanting except as required by an NPDES permit. Should any of these assumptions prove to be incorrect, the Parties shall renegotiate these deadlines, provided that the final expiration date of this Special Order will not be affected by such renegotiation. EMC SOC WQ S18-004 Duke Energy Carolinas, LLC p. 8 4) Termination of Special Order This Special Order shall terminate on a facility-by-facility basis on the later of the following dates: • 180 days following completion of decanting; or • 30 days following the approval of an amended groundwater Corrective Action Plan and/or Closure Plan as appropriate (if an amendment is submitted in compliance with subparagraph d. below). c. Additional Compliance Measures. Duke Energy nergy shall undertake the following additional compliance measures: 1) If the monitoring of any classified water of the State receiving flow from seeps regulated by this Special Order indicates exceedance of any interim action level established by the Special Order, Duke Energy shall increase monitoring at orin that location from quarterly to monthly until concentrations of monitored characteristics return to those observed at the initiation of the Special Order. If any interim action level established by the Special Order is exceeded by more than 20% in a single sampling event, or exceeded for two(2) consecutive monitoring events,in addition to paying the associated stipulated penalty, Duke Energy shall conduct a re-assessment of the contributing seep(s), including,but not limited to, evaluation of proposed remedial actions for treatment and/or control of the seep such that impacts to the receiving waters are quickly mitigated. A report compiling the findings of the re-assessment, including proposed remedial actions, shall be provided to the Director of DWR within 60 days of any applicable exceedance. Following its review, DWR shall notify Duke Energy of its concurrence or disapproval of Duke Energy's proposed remedial actions. 2) Once the decanting process is initiated, within thirty(30) days after the end of each quarter, Duke Energy shall provide reports on the status of decanting work and other activities undertaken with respect to closure of each coal ash surface impoundment to DWR. The quarterly reports are due by April 30, July 30, October 30 and January 30 while this Special Order is in effect. The reports are to be submitted as follows: one copy must be mailed to the appropriate Regional Office Supervisor for each facility and one copy must be mailed to the Water Quality Permitting Program, Division of Water Resources, 1617 Mail Service Center, Raleigh, NC 27699-1617. EMC SOC WQ S 18-004 Duke Energy Carolinas,LLC P. 9 3) Duke Energy shall conduct annual comprehensive surveys of areas down gradient of ash basins identifying new seeps, and documenting the physical characteristics of previously documented seeps. All examinations of seeps must include identification of seeps by approximate latitude and longitude and date-stamped digital photographs of their appearance. A report summarizing the findings of the surveys, including a section analyzing the effect decanting of the basin(s) has on seep flows, accompanied by copies of the photographs noted above ("Annual Seep Report"), shall be submitted to DWR in conjunction with submittal of the April 30 quarterly report noted in 2(c)(2) above. This Annual Seep Report must list any seep that has been dispositioned (as described below) during the previous year, including an analysis of the manner of disposition. For purposes of this Special Order, "dispositioned"includes the following: (1) the seep is dry for at least three consecutive quarters; (2)the seep does not constitute, and does not flow to, waters of the State or Waters of the United States for three consecutive quarters; (3)the seep is no longer impacted by flow from any coal ash basin as determined by the Director of DWR in accord with applicable law and best professional judgment; or(4) the seep has been otherwise eliminated (e.g., through an engineering solution). If a seep that has been dispositioned through drying up reappears in any subsequent survey, such a seep will no longer be deemed dispositioned and can be subsequently re-dispositioned as specified above. Non-constructed seeps described in paragraph 1(h) of this SOC cannot be dispositioned through option (2) above. 4) No later than 90 days following the completion of decanting at each Facility, and in the same manner as in the annual surveys,Duke Energy shall conduct a comprehensive survey of areas down gradient of ash basins identifying new seeps, and documenting the physical characteristics of previously documented seeps. All examinations of seeps must include identification of seeps by approximate latitude and longitude and date- stamped digital photographs of their appearance. A report summarizing the findings of this survey, including a section analyzing the effect decanting of the basin(s) has had on seep flows, accompanied by copies of the photographs noted above, shall be submitted to the Director of DWR ("Final Seep Report"). This Final Seep Report must list any seep that has been dispositioned (as described in subparagraph (3) above) during decanting process, including an analysis of the manner of disposition. The determination of whether a seep is dispositioned rests with the Director of DWR. At, or at any time prior to, submission of the Final Seep Report, Duke Energy shall seek formal certification from the Director of DWR, certifying the disposition of any seep that Duke Energy has characterized as dispositioned. Any seeps not certified as dispositioned by the Director of DWR shall not be deemed as dispositioned. EMC SOC WQ S 18 1004 Duke Energy Carolinas,LLC p. 10 d. Further Corrective Action. Following completion of decanting, if any seeps (including both constructed and non-constructed seeps)have not been certified by the Director of DWR as dispositioned (as described in subparagraph c. above), Duke Energy shall conduct a characterization of those seeps.3 Duke Energy shall submit a report on the findings of these characterizations ("Seep Characterization Report")to the Director of DWR within 150 days of completion of decanting at each Facility(i.e., within 60 days of the submittal of the Final Seep Report). The Seep Characterization Report must include all sampling data for each remaining seep as well as Duke Energy's evaluation of the jurisdictional status of all seeps at the relevant Facility. The determination regarding whether a surface water feature is a classified water of the State rests with DWR. Within 60 days of the submittal of the Seep Characterization Report, Duke Energy shall submit a complete and adequate proposed amendment to the groundwater Corrective Action Plan and/or Closure Plan as appropriate for the Facility describing how any seeps identified in the Seep Characterization Report will be managed in a manner that will be sufficient to protect public health, safety, and welfare, the environment, and natural resources. This proposed amendment will go to public comment. Duke Energy shall submit documentation that the proposed modification has been submitted to the appropriate division within the Department that has authority for approving modification of the groundwater Corrective Action Plan and/or Closure Plan. The content of, and DEQ's review of, an amendment to a groundwater Corrective Action Plan shall be consistent with Title 15A, Chapter 2L of the N.C. Administrative Code (specifically including 2L.0106(h)-(o)). The amendment to the Corrective Action Plan and/or Closure Plans shall be implemented by Duke Energy in accordance with the deadlines contained therein, as approved or conditioned by the Department. Failure by Duke Energy to implement the amendment will be handled in the normal course by the Department in accordance with its enforcement procedures (i.e., outside this Special Order). 3 If any seep is dispositioned between the time that the Final Seep Report is submitted and the time the Seep Characterization Report is submitted, an analysis of the manner of disposition must be included in the Seep Characterization Report, and Duke Energy must seek certification of such a disposition from the Director of DWR. Only if such certification is received prior to the due date of the proposed amendment described in paragraph 2(d) may such a seep, certified as dispositioned, be omitted from the proposed amendment. • EMC SOC WQ S 18-004 Duke Energy Carolinas,LLC p. 11 For clarity, listed below is a summary of the timetable for the documents due after completion of decanting (as described in 2(c)(4) and 2(d) above): Document Due Date Final Seep Report 90 days after completion of decanting 150 days after completion of Seep Characterization Report decanting (i.e., 60 days after submission of Final Seep Report) Proposed amendment to groundwater 210 days after completion of Corrective Action Plan and/or Closure decanting (i.e., 60 days after Plan submission of Seep Characterization Report) e. Interim Action Levels. 1) Duke Energyshallperform monitoringof waters receivingflow from non- constructed seeps in accordance with the schedules listed in Attachments A and B, except as noted in paragraph 2(c)(1) above. 2) Upon the complete execution of this Special Order, with regard to non- constructed seeps, interim action levels for the receiving waters (which are minor tributaries) are hereby established as noted in Attachment A. The interim action levels are site-specific. Duke Energy shall monitor at approved sampling sites to ensure interim action levels are met. Interim action levels shall remain effective in the designated surface waters until the applicable termination date in paragraph 2(b)(4) is reached. 3) Monitoring associated with seeps covered by this Special Order is exempt from the electronic reporting requirements associated with NPDES permits. Results of monitoring required exclusively per the terms of this Special Order shall be reported to the Director of DWR in a spreadsheet/worksheet format agreed to by Duke Energy and DWR. Monitoring data shall be submitted to the Director of DWR in a digital format no later than 30 days following the end of each calendar quarter for as long as the Special Order is in effect. Monitoring data shall be sent to the following email address: desocdata@ncdenr.gov. Data from those sites with monitoring required exclusively per the terms of the Special Order will be posted on DWR's website to provide the public with the opportunity for viewing. 3. Duke Energy will continue to operate its coal ash surface impoundments in such a manner that their performance is optimized, and potential for surface waters to be affected by seeps is minimized. EMC SOC WQ S 184)04 Duke Energy Carolinas,LLC p. 12 4. Duke Energy shall make available on its external website the NPDES permits, this Special Order and all reports required under this Special Order for each of the Duke Energy Facilities no later than thirty(30) days following their effective or submittal dates. 5. Duke Energy and the Commission agree that the stipulated penalties specified in paragraph 2(a)(2) are not due if Duke Energy satisfies DWR that noncompliance was caused solely by: a. An act of God; b. An act of war; c. An intentional act or omission of a third party, but this defense shall not be available if the act or omission is that of an employee or agent of Duke Energy or if the act or omission occurs in connection with a contractual relationship with Duke Energy; d. An extraordinary event beyond the Duke Energy's control, specifically including any court order staying the effectiveness of any necessary permit or approval. Contractor delays or failure to obtain funding will not be considered as events beyond Duke Energy's control; or e. Any combination of the above causes. 6. Failure within thirty(30) days of receipt of written demand by DWR to pay the stipulated penalties, or challenge them by a contested case petition pursuant to G.S. 150B-23, will be grounds for a collection action, which the Attorney General is hereby authorized to initiate. The only issue in such an action will be whether the thirty(30) days has elapsed. 7. Any non-constructed seeps causing or contributing to pollution of waters of the State associated with the coal ash impoundments at Duke Energy's Buck and Belews Creek electric generation stations, and listed in Attachment A to this Special Order, are hereby deemed covered by this Special Order. Any newly-identified non-constructed seeps discovered during the annual investigations for seeps referenced in paragraph 2(c)(3) above, or at any other time while this Special Order is in effect, and timely reported to the Department per the terms of CAMA and this Special Order, shall be deemed covered by the terms of the Special Order,retroactive to the time of their discovery. Newly- identified non-constructed seeps must be sampled for the presence of those characteristics listed in Attachment B to this Order. Newly-identified non-constructed seeps found to be causing or contributing to pollution of the waters of the State, with the effect of causing a violation of water quality standards in surface waters not already referenced in the Special Order, may require modification of the Special Order to address those circumstances. EMC SOC WQ S18-004 Duke Energy Carolinas,LLC p. 13 8. Noncompliance with the terms of this Special Order is subject to enforcement action in addition to the above stipulated penalties, including, but not limited to injunctive relief pursuant to G.S. 143-215.6C or termination of this Special Order by the Director of DWR upon ten (10) days' notice to Duke Energy. Noncompliance with the terms of this Special Order will not be subject to civil penalties in addition to the above stipulated penalties. 9. This Special Order and any terms or conditions contained herein, hereby supersede any and all previous Special Orders, Enforcement Compliance Schedule Letters, terms, conditions, and limits contained therein issued in connection with NPDES permits NC0004774 and NC0024406. 10. This Special Order may be modified at the Commission's discretion,provided the Commission is satisfied that Duke Energy has made good faith efforts to secure funding, complete all construction, and achieve compliance within the dates specified. In accordance with applicable law, modification of this Special Order will go to public notice prior to becoming effective. 11. Failure to pay the up-front penalty within thirty(30) days of execution of this Special Order will terminate this Special Order. 12. In addition to any other applicable requirement, each report required to be submitted by Duke Energy under this Special Order shall be signed by a plant manager or a corporate official responsible for environmental management and compliance, and shall include the following certification: I certify under penalty of law that this document and all attachments were prepared under my direction or supervision in accordance with a system designed to assure that qualified personnel properly gather and evaluate the information submitted. Based on my inquiry of the person or persons who manage the system, or those persons directly responsible for gathering the information, the information submitted is, to the best of my knowledge and belief, true, accurate, and complete. I am aware that there are significant penalties for submitting false information, including the possibility of fine and imprisonment for knowing violations. 13. This Special Order shall become effective in accordance with state law, and once effective, Duke Energy shall comply with all schedule dates, terms, and conditions herein. EMC SOC WQ S 18-004 Duke Energy Carolinas, LLC p. 14 This Special Order by Consent shall expire no later than June 30, 2022. F r D e Ener: ..rolinas, LLC: CQ .... 1111111110,....-- -11311 Pau Draovitch Date Senior Vice President, Environmental, Health & Safety For the No /Cart in. 1 nvironmental Management Commission: Al� r11 ( 2_ / 10 J. D of •v, P.E. C .it of th-/ ommission Date Attachment A 518-004 Duke Energy Carolinas, LLC—Buck Steam Station, p.1 Constructed Seeps See ID Approximate Receiving P Location Coordinates Description Receiving Waterbody SOC Monitoring Interim Action Number Waterbody Levels Latitude Longitude Classification Seep discharge from terracotta pipe to ra UT to N/A—Monitoring riprapped 35.70713 -80.37403 p Peed channel on north dike wall of Yadkin WS-V Established per Terms of See page 4 of this ash basin. Flow conveyed to unnamed Attachment A tributary(UT)to the Yadkin River. River NPDES Permit Filter blanket discharge from west dike UT to N/A—Monitoring S-17 35.7058 -80.3753 wall of ash basin. Flow conveyed to UT Yadkin WS-V Established per Terms of See page 4 of this to the Yadkin River. River NPDES Permit Attachment A *Location previously investigated as a seep. Monitoring has not indicated the presence of coal combustion residuals. **Seep dispositioned via repair and/or non-flowing condition to potentially reach WOTUS,or other,as noted. Monitoring shall be conducted at the approximate locations indicated on the attached site map. All monitoring shall be conducted per the requirements found in Attachment B of this Order. Attachment A S18-004 Duke Energy Carolinas, LLC— Buck Steam Station, p.2 Non-Constructed Seeps See ID Approximate Location Receiving p Coordinates Description Receiving Waterbody SOC Monitoring Interim Number Waterbody Action Level Latitude Longitude Classification Seep to UT that flows north to Yadkin River Unnamed Monitoring at in approximately 2 foot wide channel. Tributary point prior to N/A—2B Standards S-01 35.70914 -80.36044 -V Located northeast of the active ash basin, (UT)to WS any tributary Apply north of Leonard Road. Yadkin River flow to UT Located northeast of the active ash basin, * north of Leonard Road. Flows north to UT to Yadkin N/A—Seep N/A—Seep S-02 35.709414 -80.359441 -V Yadkin River via approximately 4.5 foot wide River WS Dispositioned Dispositioned stream. From sampling—No CCR impacts. Located northeast of the active ash basin, north of Leonard Road. Flows north to UT to Yadkin N/A—Seep N/A—Seep S-03* 35.710382 -80.360097 -V Yadkin River via approximately 8.5 foot wide River WS Dispositioned Dispositioned stream. From sampling—No CCR impacts. Seep to approximately 2 foot wide channel, Monitoring at located northeast of the active ash basin, UT to Yadkin point prior to Hardness 200 mg/L 5-04 35.711273 -80.360796 north of Leonard Road.Stream flows east to River WS V entering Yadkin Mercury 0.1 p.g/L Yadkin River River Seep to short UT below stormwater culvert Monitoring at near toe of ash basin dam. UT may receive UT to Yadkin established Duke pH 6-10 s.u. S-05 35.71224 -80.3646 flow from S-14 prior to reaching Yadkin River WS V Energy S-05 Hardness 200 mg/L River. monitoring site Approximately 4 foot wide stream located north of active ash basin,east of • * UT to Yadkin N/A—Seep N/A—Seep S-06 35.711971 -80.369032 decommissioned Buck Steam Station facility. WS-V River Dispositioned Dispositioned Flows north toward Yadkin River. From sampling—No CCR impacts. Approximately 3.5 foot wide stream, located northwest of the active ash basin,west of UT to Yadkin N/A—Seep N/A—Seep S-07* 35.708704 -80.378637 -V Dukeville Road. Flows northwest to Yadkin River WS Dispositioned Dispositioned River. From sampling—No CCR impacts. *Location previously investigated as a seep. Monitoring has not indicated the presence of coal combustion residuals. **Seep dispositioned via repair and/or non-flowing condition to potentially reach WOTUS,or other,as noted. Monitoring shall be conducted at the approximate locations indicated on the attached site map. All monitoring shall be conducted per the requirements found in Attachment B of this Order. Attachment A 518-004 Duke Energy Carolinas, LLC— Buck Steam Station, p.3 Approximate Location Receiving Seep ID Coordinates Description Receiving Waterbody SOC Monitoring Interim Number Waterbody Action Level Latitude Longitude Classification Seep to approximately 1 foot wide channel, Monitoring at located northwest of the active ash basin, UT to Yadkin established Duke S-08 35.708212 -80.378345 WS-V Hardness 200 mg/L west of Dukeville Road. Flows northwest to River Energy S-08 Yadkin River. monitoring site ** UT to Yadkin N/A—Seep N/A—Seep S-09 35.7055 -80.3757 Sampling Location;not a seep WS-V River Dispositioned Dispositioned Approximately 2 foot wide stream, located * west of the active ash basin,west of UT to Yadkin N/A—Seep N/A—Seep S-10* 35.702188 -80.376455 WS V Dukeville Road. Flow is to Yadkin River. River Dispositioned Dispositioned From sampling—No CCR impacts. ** Channeled seep through a terracotta pipe. UT to Yadkin N/A—Seep N/A—Seep S-12 35.707429 -80.373661 Pipe has been plugged;discharge WS V River Dispositioned Dispositioned eliminated. Minimal AOW with no flow. Identified as a ** damp area near pump house; no sufficient UT to Yadkin N/A—Seep N/A—Seep S-13** 35.711931 -80.364056 flow to perform sampling.Any flow would River WS V Dispositioned Dispositioned move to adjacent storm drain. Low flow seep near stormwater culvert just Monitoring at UT to Yadkin established Duke S-14 35.712171 -80.364817 above S-05 location.Any flow will move to WS-V See S-05 UT to Yadkin River near S-05. River Energy S-05 monitoring site Low flow seep downgradient of S-05 Monitoring at UT to Yadkin established Duke S-15 35.7123 -80.3644 location. Seep flows to braided,short reach WS-V See 5-05 UT prior to entering Yadkin River River Energy S-05 monitoring site Static area of wetness along west dike wall ** of ash basin. Flow would drain toward S-09 UT to Yadkin N/A—Seep N/A—Seep S-16 35.7044 -80.3746 WS-V sampling site. Location has been repaired River Dispositioned Dispositioned based on no area of wetness. *Location previously investigated as a seep. Monitoring has not indicated the presence of coal combustion residuals. **Seep dispositioned via repair and/or non-flowing condition to potentially reach WOTUS,or other,as noted. Monitoring shall be conducted at the approximate locations indicated on the attached site map. All monitoring shall be conducted per the requirements found in Attachment B of this Order. Attachment A S18-004 Duke Energy Carolinas, LLC— Buck Steam Station, p.4 Instream Monitoring Description Receiving Waterbody Receiving Waterbody SOC Monitoring Interim Action Levels Classification Instream Monitoring to Instream Monitoring of arm/cove of N/A—2B Standards evaluate potential impacts Yadkin River WS-V from S-01 and S-04 Yadkin Rivers Apply Instream Monitoring to Instream Monitoring of arm/cove of N/A—2B Standards evaluate potential impacts Yadkin River WS-V from S-05,S-14 and S-15 Yadkin Rivers Apply Instream Monitoring to Monitoring of the Yadkin River evaluate potential impacts Yadkin River WS-V Upstream and Downstream of Buck N/A—2B Standards from all non-constructed Apply Steam Station site seeps Instream Monitoring to Monitoring of UT to Yadkin River at Unnamed Tributary evaluate potential impacts WS-V established Duke Energy S-09 Hardness 200 mg/L from S-11 and S-17 (UT)to Yadkin River monitoring location 1. Instream monitoring requirement will become effective 30 days following the elimination of NPDES permit NC0004774 outfall 002. *Location previously investigated as a seep. Monitoring has not indicated the presence of coal combustion residuals. **Seep dispositioned via repair and/or non-flowing condition to potentially reach WOTUS,or other,as noted. Monitoring shall be conducted at the approximate locations indicated on the attached site map. All monitoring shall be conducted per the requirements found in Attachment B of this Order. Buck Steam Station — Water Quality Monitoring Locations .. ..-- . ---., �- N dam, M , a /f, ,r .. - �y s . 4 lip' 411111 , M ' ' . w ,ft'.�'f •a. - _ _ y r �r i 441 t a ;, / \ted 111.11 a'.� Y 49 '''''ill 4 /. r '4. f' ,. G.anrRd i 4 .1.11111,41 ' f,, ' - k-- Upstream in Yadkin River Stream Monitoring Downstream in Yadkin River Stream Monitoring Attachment A S18-004 Duke Energy Carolinas, LLC- Belews Creek Steam Station, p.1 Constructed Seeps See ID Approximate Receiving p Location Coordinates Description Receiving Waterbody SOC Monitoring Interim Action Number Waterbody Levels Latitude Longitude Classification Constructed seep conveying toe drain N/A—Monitoring discharge from dam via rip-rapped UT to the See page 5 of this S-11 36.29859 -80.07571 effluent channel to unnamed tributary Dan River WS IV Established per Terms of Attachment A NPDES Permit to the Dan River. *Location previously investigated as a seep. Monitoring has not indicated the presence of coal combustion residuals. **Seep dispositioned via repair and/or non-flowing condition to potentially reach WOTUS,or other,as noted. Monitoring shall be conducted at the approximate locations indicated on the attached site map. All monitoring shall be conducted per the requirements found in Attachment B of this Order. Attachment A S 18-004 Duke Energy Carolinas, LLC- Belews Creek Steam Station, p.2 Non-Constructed Seeps Approximate Receiving Seep ID Location Coordinates Description Receiving Waterbody SOC Monitoring Interim Action Number Levels Latitude Longitude Waterbody Classification Flow via approximately 3 foot wide unnamed tributary to the Dan River, Unnamed * tributary N/A—Seep N/A—Seep S-01 36.29323 -80.0852 located northwest of the active ash WS-V basin,west of Middleton Loop. From (UT)to the Dispositioned Dispositioned sampling—No CCR impacts. Dan River Seep to approximately 3.5 foot wide Monitoring at stream channel,located northwest of UT to the pH 5-10 s.u. 5-02 36.29689 -80.0844WS-V established Duke Energy the active ash basin.Stream flows Dan River Hardness 200 mg/L S-02 monitoring site north to the Dan River Flow via approximately 3 foot wide unnamed tributary to the Dan River, S-03* 36.29841 -80.0833 located northwest of the active ash UT to the WS-V N/A—Seep N/A—Seep basin,west of Middleton Loop. From Dan River Dispositioned Dispositioned sampling—No CCR impacts. Flow via approximately 3 foot wide unnamed tributary to the Dan River, S-04* 36.29802 -80.0821 located northwest of the active ash UT to the WS-V N/A—Seep N/A—Seep basin,west of Middleton Loop. From Dan River Dispositioned Dispositioned sampling—No CCR impacts. Flow via approximately 3.5 foot wide unnamed tributary to the Dan River, S-05* 36.30047 -80.0808 located northwest of the active ash UT to the WS-V N/A—Seep N/A—Seep basin,west of Middleton Loop. From Dan River Dispositioned Dispositioned sampling—No CCR impacts. Seep to UT to Belews Lake(former ash UT to Monitoring at pH 5-10 s.u. S-06 36.29615 -80.061 Belews WS-IV established Duke Energy Hardness 300 mg/L basin outfall channel). Lake S-06 monitoring site TDS 700 mg/L *Location previously investigated as a seep. Monitoring has not indicated the presence of coal combustion residuals. **Seep dispositioned via repair and/or non-flowing condition to potentially reach WOTUS,or other,as noted. Monitoring shall be conducted at the approximate locations indicated on the attached site map. All monitoring shall be conducted per the requirements found in Attachment B of this Order. Attachment A 518-004 Duke Energy Carolinas, LLC- Belews Creek Steam Station, p.3 See ID Approximate Receiving p Location Coordinates Description Receiving Waterbody SOC Monitoring Interim Action Number Waterbody Levels Latitude Longitude Classification Low diffuse flow to a wetland area with * initial flow to Charlie's Pond and Charlie's N/A—Seep N/A—Seep S-07 36.28717 -80.0642 ultimate discharge to Belews Lake. Pond WS IV Dispositioned Dispositioned From sampling—No CCR impacts. Seep to approximately 4 foot wide UT to Monitoring at stream channel, located south of the pH 5-10 s.u. S-08 36.27986 -80.0776 Belews C established Duke Energy Pine Hall Road Ash Landfill. Stream Lake S-08 monitoring site Selenium 10µ/L flows south to Belews Lake Seep to approximately 2.5 foot wide Monitoring at point pH 5-10 s.u. stream channel,located south of Pine UT to downstream of Selenium 10µ/L S-09 36.28022 -80.0722 Hall Road,and west of Structural Fill Belews C confluence of S-09 and Sulfates 600 mg/L site. Stream flows south to Belews Lake S-16 flows, prior to Hardness 500 mg/L Lake entering Belews Lake TDS 800 mg/L Monitoring location about 500 feet pH 5-10 s.u. below the toe of the dam for seep to Cadmium 2µg/L approximately 6 foot wide stream Monitoring at 5-10 36.29923 -80.0758 channel,just before the stream joins a UT to the WS-IV established Duke Energy Chlorides 600 mg/L larger UT. Combined stream flow has Dan River S-10 monitoring site Mercury 0.1µg/L Hardness 600 mg/L confluence with ash basin discharge TDS 1200 mg/L flow from concrete flume structure. Seep to natural stream in small valley * east of active ash basin.Stream flows UT to N/A—Seep N/A—Seep S-12 36.2968 -80.0605 south into UT to Belews Lake(former Belews WS-IV Dispositioned Dispositioned ash basin outfall channel). From Lake sampling—No CCR impacts. *Location previously investigated as a seep. Monitoring has not indicated the presence of coal combustion residuals. **Seep dispositioned via repair and/or non-flowing condition to potentially reach WOTUS,or other,as noted. Monitoring shall be conducted at the approximate locations indicated on the attached site map. All monitoring shall be conducted per the requirements found in Attachment B of this Order. Attachment A 518-004 Duke Energy Carolinas, LLC- Belews Creek Steam Station, p.4 See ID Approximate Receiving p Location Coordinates Description Receiving Waterbody SOC Monitoring Interim Action Number Waterbody Levels Latitude Longitude Classification Minor seep to small stream channel east of active ash basin, located east of UT to S-13* 36.2925 -80.0617 Pine Hall Road.Stream flows south to Belews WS-IV N/A—Seep N/A—Seep Belews Lake. From sampling—No CCR Lake Dispositioned Dispositioned impacts. Minor seep to small stream channel east of active ash basin, located east of UT to S-14** 36.29221 -80.0624 Pine Hall Road.Stream flows south to Belews WS-IV N/A—Seep N/A—Seep Belews Lake. No flow observed during Lake Dispositioned Dispositioned most recent sampling events. Seep to small stream located east of 5- 10 and S-11 locations. Stream flow drains north,joining other stream S-15* 36.29927 -80.0754 flows.Combined flow has confluence UT to the WS IV N/A—Seep N/A—Seep with ash basin discharge flow from Dan River Dispositioned Dispositioned concrete flume structure. From sampling—No CCR impacts. Seep to small stream channel, located south of Pine Hall Road,and west of UT to N/A—Seep N/A—Seep S-16* 36.27961 -80.0726 Structural Fill site. Stream flows south Belews C to Belews Lake. From sampling—No Lake Dispositioned Dispositioned CCR impacts. Small seep located downgradient from N/A— the toe of the dam,just west of the rip- Flows to rapped effluent channel. Flows from effluent N/A—Monitored per N/A—Not a S-18 36.29833 -80.07572 wetland area to effluent channel.This channel for N/A terms of the NPDES classified surface non-constructed seep flows to a NPDES permit water portion of an NPDES wastewater outfall treatment system. *Location previously investigated as a seep. Monitoring has not indicated the presence of coal combustion residuals. **Seep dispositioned via repair and/or non-flowing condition to potentially reach WOTUS,or other,as noted. Monitoring shall be conducted at the approximate locations indicated on the attached site map. All monitoring shall be conducted per the requirements found in Attachment B of this Order. Attachment A 518-004 Duke Energy Carolinas, LLC- Belews Creek Steam Station, p.5 Instream Monitoring Description Receiving Waterbody Receiving Waterbody SOC Monitoring Interim Action Levels Classification Instream Monitoring to evaluate potential impacts Dan River WS IV,WS-V Upstream & Downstream Monitoring of the N/A—2B Standards from S-02 and S-10 Dan River Apply pH 5-10 s.u. Instream Monitoring to Monitoring of UT to Dan River prior to its Cadmium 2µg/L evaluate potential impacts Unnamed Tributary WS-IV confluence with ash basin discharge flow Chlorides 700 mg/L from 5-10 and S-11 (UT)to Dan River from concrete flume structure Mercury 0.1µg/L Hardness 800 mg/L TDS 1500 mg/L Instream Monitoring to evaluate potential impacts Belews Lake WS IV Monitoring of Belews Lake downstream of N/A—2B Standards from S-06 steam station Apply Instream Monitoring to evaluate potential impacts Belews Lake C Monitoring of Belews Lake upstream of N/A—2B Standards from S-08 and S-09 steam station Apply *Location previously investigated as a seep. Monitoring has not indicated the presence of coal combustion residuals. **Seep dispositioned via repair and/or non-flowing condition to potentially reach WOTUS,or other,as noted. Monitoring shall be conducted at the approximate locations indicated on the attached site map. All monitoring shall be conducted per the requirements found in Attachment B of this Order. Belews Creek Water Quality Monitoring Locations (North) * '. ‘4'.4:\ 5 •i i *I o - . . o'er t ., Iry * ' 4441r , sior7 s, .^ 7 . • 1 ... ,,.. —.A e.... A . . 4 .411k,446.. S-02 l 4 s-o6 Ash Basin �., ;, Belews r. Lake 4, ./3',,,," V'A : '4 ' IS' /444,71°Cts "4,4 ' t k..4., 4 ' y b Upstream Monitoring — Dan River * Stream Monitoring Downstream Monitoring — Dan River & Belews Lake Stream Monitoring Belews Creek Water Quality Monitoring Locations (South) ' .. Ash Basin Belews t.. `'�., Lake N ,, �� r.. Nt ,+, „1$41' '7;,-7. �" %..... . * o ,, I: 4:.... /,' / --.. etglk'' " ‘' C , # , ►, r/ M / `." �r 4 �r 4 : . ' ) i I' 'Noy e s. /` * - s - 1 igs ...• i S-08 r � ' �71 t 1 S-09 .63...., ' L f d 4 _-'^: +., ail` • i-.a. ..- 'r. l {. :. .� , r ►s , • j pit+ . •� • '.ryr�' " , '3/ s,k� .,' , �,- ' •" �'.� / Belews Lake 1 >r , Downstream Monitoring — Belews Lake * Stream Monitoring SOC S18-004 Duke Energy Carolinas, LLC Attachment B Monitoring Requirements The following represents the parameters to be analyzed and reported at all monitoring locations designated within this Special Order. Parameter Reporting Units Monitoring Frequency TSS mg/L Annually Oil and Grease mg/L Annually pH Standard Units(s. u.) Quarterly Fluoride pg/L Quarterly Total Mercury ng/L Quarterly Total Barium pg/L Quarterly Total Zinc pg/L Quarterly Total Arsenic pg/L Quarterly Total Boron pg/L Quarterly Total Cadmium pg/L Quarterly Total Chromium pg/L Quarterly Total Copper pg/L Quarterly Total Thallium pg/L Quarterly Total Lead pg/L Quarterly Total Nickel pg/L Quarterly Total Selenium pg/L Quarterly Nitrate/Nitrite as N mg/L Quarterly Bromides mg/L Quarterly Sulfates mg/L Quarterly Chlorides mg/L Quarterly TDS mg/L Quarterly Total Hardness mg/L Quarterly Temperature ° C Quarterly Conductivity, pmho/cm pmho/cm Quarterly