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HomeMy WebLinkAboutNC0003425_Correspondence_20191022V f DUKE ENERGY, PROGRESS File: 12520 Mr. Rick Bolich North Carolina Division of Environmental Quality 1628 Mail Service Center Raleigh, NC 27699-1628 Subject: Roxboro Electric Generating Plant NPDES Permit No.00003425 Five-day Follow-up Letter Incident No.272096 Dear Mr. Bolich: Duke Energy Progress, LLC Roxboro Steam Electric Plant 1700 Aun nan ur Road Seinora NC 27.44 October 22, 2019 NC Dept of Environmental Quality OCT 18 2019 Raleigh Regional Office On October 20, 2019 at approximately 1:23 F.M., Duke Energy staff made verbal notification to Mr. George Bernard of an unanticipated bypass of treatment at the Roxboro Steam Station in Person County. The verbal notification was made as required by Fart II, Section E.9.(c) of the above -referenced permit. Also, as required by Part Il, Section E.9, this letter fulfills the five-day written letter requirement. At approximately 7:32 A.M. on Sunday, October 20, 2019, station operations received a Hi level alarm in the process water redirect sump during a period of intense rain. Station operations verified from DCS that two available normal service pumps (pumps B & C) were in service and operating when the Hi Hi level alarm was received approximately two minutes after the first alarm. A station operator was dispatched to investigate. While in route, another alarm for Lined Retention Basin inlet valve deviation was received, indicating low flow for the B & C pumps and tripping both off. The station operator and supervisor arrived at the sump to find the level elevated and overflowing into the heated water discharge canal. A higher capacity secondary Lined Retention Basin inlet valve failed to open on the Hi Hi level alarm which also had signaled and caused the primary valve to close. The primary inlet valve was forced open from the DCS allowing flow from the B & C pumps to be restored. Concurrently, the operator and supervisor placed the standby diesel pump in service. The process water redirect sump level decreased below overflow within 4 minutes. Total estimated overflow time was 10 minutes according to DCS alarm history. The primary inlet valve will remain in manual to prevent loss of flow until the secondary valve can be repaired. The total bypass volume discharged to heated water discharge canal was estimated to be 3,500 gallons. Duke Energy made an environmental event press release on October 20, 2019 and included it on the Duke Energy website. If you have any questions concerning this ;ubmittal, please contact Ms. Lori Tollie at (336)-8544916 or at Lori.Tollie@duke-energv.com. "I certify, under penalt-Y of la►r, that this doctuuent and till attachments n-ere prepared tinder ruy direction or supert-ision in accordance iiith a system designed to assure that qualified personnel properly gather and evahutte the information submitted. Based on mY inquiry of the person or DUKE ENERGY. PROGRESS Duke Enerl;y Progress, LLC Rnxbora Steam Elecuie Plant 1700 Dunncnt'av Road Sonora, NC 2744.4 persons who manage the system, or those persons elirectlS• responsible for gathering the information, the information submitted is, to the best of nn knowledge and belief, trite, accurate, and complete. 1 cam aware that there are significant penalties for submitting false information, including the pos•s•ibilit►, of fines and imprisonment for knowing violations. " Sincerely, Tom Copolo General Manger — Roxboro Steam Station