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HomeMy WebLinkAbout20140762 Ver 4_12 - R-2915D 4B Meeting Minutes_20190918Minutes from the Interagency 4B Hydraulic Design Review Meeting R-2915D in Ashe County April 18, 2013 1:00 PM — 2:30 PM Team Members: Monte Matthews, USACE Marella Buncick, USFWS Marla Chambers, NCWRC Amy Chapman, NCDWQ Chris Militscher, EPA Michael Batuzich, NCDOT David Harris, NCDOT Brenda Moore, NCDOT Trent Beaver, NCDOT Minutes: (present) (present) (present) (present) (absent) (absent) (absent) (absent) (absent) Participants: Marshall Clawson, Hydraulics Will Hines, Sungate Design Group Brad Smith, Sungate Design Group Quang Nguyen, Structure Design Tatia White, Roadway Design Mark Staley, REU Erin Cheely, PDEA John Conforti, PDEA Carla Dagnino, NES Elizabeth Lusk, NES General Introduction was initiated by Marshall Clawson. Introductions were made by all in attendance. Sheet 4: No comments. Sheet 5: No comments. Sheet 6: No comments. Sheet 7: No impacts. Sheet 8: NES will let Hydraulics know if the wetland will be a total take. Sheet 9: No impacts. Sheet 10: No comments. Sheet 11: Station 537+00 -L- Left (Structure 1103): Investigate realigning 30" CSP with JS. Sheet 12: No impacts. Sheet 13: No comments. Sheet 14: No comments. Sheet 15: Station 587+50 -L- Right (Structure 1502): Investigate extending the proposed 24" pipe and using a Preformed Scour Hole if the design criteria allows. Station 588+00 -L- Right: Remove debris (existing detached FES) from stream. Sheet 16: Station 607+50 -L- Left (Structure 1610): Add drop box in proposed 24" pipe in order to reduce velocity in the wetland. Sheet 17: No Comments. Sheet 18: Station 628+50 -L- Right (Structure 1808): Investigate realigning the proposed 24" pipe with JS. Sheet 19: Station 642+00 -L- Right: Hydraulics explained that the wetland to the left will head up and flow to the 30" pipe inlet. Station 642+00 -L- Left: The Hydraulics Engineer explained that the gap between the two 30" pipes will be maintained and that the proposed riprap will be placed between the 30" outlet and the wetland boundary. Sheet 20: No comments. Sheet 21 Station 663+50 -L- Right: Place a note on Plans stating to tamp down riprap at outlet of 60" pipes or call for riprap on banks only. Station 17+00 — 21+00 -Y32- Right: Hand clear wetland 5 feet from slope stake line. Station 668+00 -L- Right: The Hydraulics Engineer pointed out that a portion of the wetland shown on the Plans was actually a mowed lawn. NES stated that the wetlands on this project will be confirmed. Station 670+00 -L- Right (Structure 2129): Place inlet of proposed 30" pipe on grade in order to avoid draining wetland. Sheet 22 Station 677+00 -L- Right: Redesign Lateral "V" Ditch in order to reduce the velocity going into the wetland. Sheet 23 No impacts. Meeting adjourned.