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HomeMy WebLinkAbout20190624 Ver 1_2018-11-27_Old Airport Rd_Redline Calculations_20190510Date: 11/26/2018 Kimley-Horn & Associates, Inc. Raleigh, NC Project Number: 12718003 Designed By: ANN County: Craven Checked By: DWT Ditch Computation Sheet Description Normal Ditch Location D.A. (acres) C Q25 (cfs) Slope (ft / ft) Base Width Side Slopes Depth (ft) Velocity (fps) Remarks Liner Type From To L/M/R 18+92 -L- 19+00 -L- R 0.87 0.57 3.70 0.0800 0 4:1/3:1 0.62 2.72 Class 'B' Rip Rap 19+00 -L- 22+75 -L- R 0.87 0.57 3.70 0.0024 0 4:1/3:1 0.93 1.22 Grass 22+75 -L- 25+50 -L- R 0.22 0.62 1.02 0.0040 0 4:1/3:1 0.52 1.07 Grass 25+50 -L- 29+50 -L- R 0.62 0.58 2.67 0.0035 0 4:1/3:1 0.77 1.29 Grass 29+50 -L- 32+00 -L- R 1.03 0.58 4.51 0.0040 0 4:1/3:1 0.91 1.55 Grass 32+00 -L- 32+60 -L- R 1.03 0.58 4.51 0.0033 0 4:1/3:1 0.95 1.44 Grass 32+60 -L- 35+00 -L- R 1.66 0.55 6.82 0.0063 0 4:1/3:1 0.98 2.04 Grass 35+00 -L- 36+00 -L- R 1.66 0.55 6.82 0.0350 0 4:1/3:1 0.71 3.87 Grass 36+20-L- 37+00-L- R 2.61 0.51 9.97 0.0288 0 4:1/3:1 0.85 3.96 Grass 37+00 -L- 42+30 -L- R 2.61 0.51 9.97 0.0022 0 4:1/3:1 1.37 1.51 Grass 42+30 -L- 45+35 -L- R 2.61 0.51 9.97 0.0010 0 4:1/3:1 1.59 1.12 Grass 45+35 -L- 46+70 -L- R 2.61 0.51 9.97 0.0017 0 4:1/3:1 1.44 1.37 Grass 46+70 -L- 48+00 -L- R 1.17 0.50 4.34 0.0082 0 4:1/3:1 0.79 2.01 Grass 48+00 -L- 51 +75 -L- R 1.17 0.50 4.34 0.0057 0 4:1/3:1 0.84 1.75 Grass 52+80 -L- 55+50 -L- R 0.52 0.66 2.58 0.0024 0 4:1/3:1 0.89 0.93 Grass Page 1 of 3 Ditch Computation Sheet Description Normal Ditch Location D.A. (acres) C Q25 (cfs) Slope (ft / ft) Base Width Side Slopes Depth (ft) Velocity (fps) Remarks Liner Type From To L/M/R 55+50 -L- 64+15 -L- R 1.61 0.65 7.89 0.0027 0 4:1/3:1 1.21 1.54 Grass 64+50 -L- 67+55 -L- R 1.98 0.63 9.42 0.0035 0 4:1/3:1 1.23 1.77 Grass 67+55 -L- 70+03 -L- R 2.32 0.61 10.58 0.0028 0 4:1/3:1 1.34 1.68 Grass 70+03 -L- 72+65 -L- R 2.69 0.59 11.91 0.0029 0 4:1/3:1 1.39 1.75 Grass 72+65 -L- 73+35-L- R 2.82 0.59 12.48 0.0024 0 4:1/3:1 1.47 1.65 Grass 75+61 -L- 76+22 -L- R 3.44 0.57 14.687 0.0205 0 4:1/3:1 1.05 3.84 Grass 76+43 -L- 77+10 -L- R 3.44 0.57 14.687 0.0037 0 4:1/3:1 1.44 2.02 Grass 78+10 -L- 79+50 -L- R 3.61 0.57 15.369 0.0077 0 4:1/3:1 1.28 2.69 Grass 79+50 -L- 79+95 -L- R 3.61 0.57 15.369 0.0204 0 4:1/3:1 1.06 3.88 Grass 83+59 -L- 86+50 -L- R 0.75 0.47 2.63 0.0167 0 4:1/3:1 0.57 2.31 Grass 86+50 -L- 87+00 -L- R 0.75 0.47 2.63 0.0328 0 4:1/3:1 0.50 2.98 Grass 18+62 -L- 20+10 -L- L 0.87 0.51 3.35 0.0017 0 4:1/3:1 0.96 1.04 Grass 20+10 -L- 22+00 -L- L 0.87 0.51 3.35 0.0031 0 4:1/3:1 0.86 1.31 Grass 22+00 -L- 24+50 -L- L 0.87 0.51 3.35 0.0025 0 4:1/3:1 0.89 1.21 Grass 24+50 -L- 27+70 -L- L 1.23 0.41 3.81 0.0025 0 4:1/3:1 0.94 1.25 Grass 27+70 -L- 32+00 -L- L 3.33 0.45 11.28 0.0032 0 4:1/3:1 1.34 1.79 Grass Page 2 of 3 Ditch Computation Sheet Description Normal Ditch Location D.A. (acres) C Q25 (cfs) Slope (ft / ft) Base Width Side Slopes Depth (ft) Velocity (fps) Remarks Liner Type From To L/M/R 32+00 -L- 33+65 -L- L 3.33 0.45 11.28 0.0062 0 4:1/3:1 1.18 2.30 Grass 33+65 -L- 36+00 -L- L 3.33 0.45 11.28 0.0191 0 4:1/3:1 0.96 3.50 Grass 36+20 -L- 38+00 -L- L 2.74 0.57 11.77 0.0161 0 4:1/3:1 1.01 3.32 Grass 38+00 -L- 46+90 -L- L 2.01 0.54 8.08 0.0020 0 4:1/3:1 1.29 1.38 Grass 46+90 -L- 52+55 -L- L 1.53 0.51 5.89 0.0042 0 4:1/3:1 1.00 1.69 Grass 52+55 -L- 57+50 -L- L 0.75 0.51 2.83 0.0025 0 4:1/3:1 0.84 1.16 Grass 57+50 -L- 62+50 -L- L 0.75 0.56 3.13 0.0020 0 4:1/3:1 0.91 1.09 Grass 62+50 -L- 73+50 -L- L 1.98 0.55 8.17 0.0020 0 4:1/3:1 1.30 1.39 Grass 73+50 -L- 76+10 -L- L 3.39 0.48 12.31 0.0096 0 4:1/3:1 1.13 2.76 Grass 76+10 -L- 77+00 -L- L 3.39 0.48 12.31 0.0059 0 4:1/3:1 1.24 2.30 Grass 77+00 -L- 79+54 -L- L 3.39 0.48 12.31 0.0215 0 4:1/3:1 0.97 3.74 Grass 83+82 -L- 86+15 -L- L 0.82 0.55 3.35 0.0215 0 4:1/3:1 0.60 2.70 Grass 86+15 -L- 87+50 -L- L 0.54 0.52 2.11 0.0151 0 4:1/3:1 0.53 2.11 Grass 10+41-Y2- 13+25 -Y2- L 1.22 0.67 6.07 0.002 0 4:1/3:1 1.16 1.29 Grass 10+45 -Y2- 13+50 -Y2- R 0.53 0.44 1.73 0.002 0 4:1/3:1 0.76 0.86 Grass Page 3 of 3 Date 11/26/2018 Project No. 012718003 I.D. No. PIPE DATA SHEET Sheet County Craven Designed By DWT Checked By 1 of 1 LDR Shoulder CL Elev. 18.72 PLAN SUMMARY DATA Elev 18.95 Drainage Area 57.71 ac Design Freq. 50 yr Station 36+12 -L- Design Disch. 111.00 cfs Skew 84.30 ° H Design H.W. Elev. 16.57 ft Size/Type Pipe 2-42" RCP H.W. T.W. Q100 Disch. 127.00 cfs Type Entrance Groove End with HW LSo �� Q100 H.W. Elev. 16.89 ft Direction of Flow Rt to Lt Overtopping Freq. yr Hydrological Method USGS Inv. Elev. 13.00 So = 1.25 % Inv. Elev. 12.25 Overtopping Disch. 207.10 cfs HW Control Elev 18.95 L = 60.00 Overtopping Elev. 18.95 ft Size & Type Pipe Freq (Yrs.) Q (cfs) Nat. H.W Allow. H.W. T.W. INLET CONTROL OUTLET CONTROL H.W. Elev. Vo (ft/s) COMMENTS HW/D H.W. Ke do do+d ho H LSo H.W. 2 2 - 42" RCP 10 75.00 0.62 0.76 2.67 0.2 1.90 2.70 2.70 0.12 0.75 2.82 15.82 1 9.94 Outlet Control 2 - 42" RCP 25 95.00 0.62 0.88 3.09 0.2 12.1512.83 2.83 0.43 0.75 3.25 16.25 10.51 Outlet Control 2 - 42" RCP 50 111.00 0.62 0.97 3.40 0.2 2.33 2.92 2.92 0.66 0.75 3.57 16.57 10.91 Outlet Control 2 - 42" RCP 100 127.00 0.62 1.06 3.72 0.2 2.50 3.00 3.00 0.89 0.75 3.89 16.89 11.29 Outlet Control SUMMARY AND RECOMMENDATIONS: 2-42" RCP USGS method used to determine discharge. 15% imperviousness used to account for future development. Water will breach Shld pt at sta. 36+12 -L- elevation = 18.95. This vields 2.38' of freeboard during the 50-vr storm. OLD AIRPORT RD OUTFALL ANALYSIS OUTFALL ANALYSIS 36+12 -L- (LT) Description: The proposed outfall are dual 42" RCPs that outlet at Sta. 36+12 -L- (LT) replacing existing dual 24" RCPs. The pipes discharge into an existing wetland. The inlet and outlet were raised 0.5' from existing inverts to maintain tailwater depth in the proposed 42" pipes. Photo 1: Existing Condition Downstream of Outlet Photo 2: Existing Condition of Outlet Analysis: • There are no adverse effects on the downstream receiving water. • There are no downstream inadequacies that would adversely impact the highway. • There will be no effects to the adjacent property from the 25-yr storm. • The outfall has a pre -construction flow of 219.32 cfs and post -construction flow of 225.94 cfs. This yields a percent increase of 3.00%. The pre -construction velocity is 4.34 fps and the post - construction velocity is 4.37 fps. This yields a percent increase of 0.70%. The pre -construction water surface is 2.25 ft and the post -construction water surface is 2.27 ft which yields a percent increase of 0.90%. The minor increases are due to the addition of impervious area. • Based on the minimal impact to the downstream facilities, no corrective measures are needed. • No actions recommended at this time. OUTFALL ANALYSIS 13+23 -Y2- (LT) Description: The outfall at Sta. 13+23 -Y2- (LT) is a proposed ditch that outlets to an existing 15" RCP. There is a ditch downstream of the existing 15" driveway pipe. Photo 1: Existing Condition of Upstream of Outlet Analysis: • There are no adverse effects on the downstream receiving water. • There are no downstream inadequacies that would adversely impact the highway. • There will be no effects to the adjacent property from the 25-yr storm. • The outfall has a pre -construction flow of 2.04 cfs and post -construction flow of 3.49 cfs. This yields a 70.80% increase. The pre -construction velocity is 1.54 fps and the post -construction velocity is 1.76 fps. This yields a percent increase of 14.30% increase. The pre -construction water surface is 0.66 ft and the post -construction water surface is 0.81 ft which yields a percent increase of 22.70%. The increases are due to the addition of impervious area and consideration of future development per city zoning maps. • Based on the minimal impact to the downstream facilities, no corrective measures are needed. • No actions recommended at this time. Kimley>»Horn Project Information Project Name: Old Airport Rd KHA Project #: 012718003 Designed by: ANN Date: 11/26/2018 Checked by: DWT Date: 11/26/2018 Revised by: Date: 25 Year Analysis Pre- vs Post -Construction Discharges EXISTING CONDITIONS PROPOSED CONDITIONS Station/Structure # DRAINAGE AREA A (acres) RUNOFF COEFF. C Time of Concentration Tc (min) Storm Intensity I (in/hr) Q TOTAL Q10 (cfs) Station/Structure # DRAINAGE AREA A (acres) RUNOFF COEFF. C Time of Concentration Tc (min) Storm Intensity I (in/hr) O TOTAL Quo (cfs) DISCHARGE DIFF. (CFS) DISCHARGE INCREASE M) 36+12 -L- LT/0204 63.75 0.46 10.00 7.50 219.32 36+12 -L- LT/0204 63.75 0.47 10.00 7.50 225.94 6.63 3.0 13+23 -Y2- LT 0.70 0.39 10.00 7.50 2.04 13+23 -Y2- LT 0.70 0.67 10.00 7.50 3.49 1.44 70.8 Note: Future development was taken into account during the computing of the proposed C-values. Page 1 of 1 Kimley>Morn Project Information Pre Downstream Outfalls Post Downstream Outfalls Downstream Outfalls Qzs Outfall Channel Analysis Project Name: Old Airport Rd KHA Project M 012718003 Designed by: ANN Date: 11/26/2018 Checked by: DWT Date: 11/26/2018 Revised by: Date: Outlet DA C Tc izs Qns s Fore Slope Backslope Base Width Ditch Existing I Design Depth y V Manning's (ac) Value (min) (in/hr) (cfs) (ft/ft) (ft) Type Depth (ft)l of Ditch (ft.) (ft) (fps) n 36+12 -L- LT/0204 63.75 0.46 10.00 7.50 219.32 0.0090 10A 10A 0 Exist Wetland N/A Leave as is 2.25 4.34 0.035 13+23 -Y2- LT 0.70 0.39 10.00 7.50 2.04 0.0062 3:1 3:1 0 Exist Swale N/A Leave as is 0.66 1.54 0.035 Outlet DA C Tc izs Qzs s Fore Slope Backslope Base Width Ditch Existing Design Depth y V Manning's (ac) Value (min) (in/hr) (cfs) (ft/ft) (ft) Type De th (ft) of Ditch (ft.) (ft) (fps) n 36+12 -L- LT/0204 63.75 0.47 10.00 7.50 225.94 0.0090 10:1 10:1 0 Exist Wetland N/A Leave as is 2.27 4.37 0.035 13+23 -Y2- LT 0.70 0.67 10.00 7.50 3.49 0.0062 3:1 3:1 0 Exist Swale N/A Leave as is 0.81 1.76 0.035 Outlet Depth Velocity Depth Velocity Change Change (ft) Change (fps) Change (%) 36+12 -L- LT/0204 0.02 0.03 0.9 0.7 13+23 -Y2- LT 0.15 0.22 22.7 14.3 Page 1 of 1