Loading...
HomeMy WebLinkAboutSW3240702_Soils/Geotechnical Report_20240801 CEST Civil - Geotechnical - Surveying May 23, 2024 Mr. Randy Humphries Performance Precast, Inc. Reference: Seasonal High-Water Table Determination Proposed PPI Office and Welding Site 70 Zane Road Midland, Cabarrus County, North Carolina CESI Project Number 240260.000 Mr. Humphries: In accordance with your request, Concord Engineering & Surveying, Inc. (CESI) has performed an evaluation of seasonal high-water table (SHWT) on the above referenced project. The SHWT was performed within the area of the proposed sand filter, as shown below: il DS-1 RIM.693.00 15' INV OUT(N):686.53 0 d Ilk :72C'' 98.L SHWT O Test Location - cv 0 1Y) 1� CO in rn co BUILDING F.F.E. 141.31'/15' RCP/0.501 cn< `O 698.50 r i f J FEs-1 INV OUT: 689.19 ^ 161.51715.RCP 0.50E '--r i 1 73.92718'RCP/0.50% - \ __.,- RIM-1 ��, RIM:693.08 1�.\�� 1• 6", /18" IN�(..OUTS(E)6 89.56` \ - ` 45 Spring Street, SW P.O. Box 268 Concord, NC 28026-0268 704-786-5404 www.cesicgs.com NC License No. C-0263 On May 22, 2024, a CESI representative monitored the excavation and the soil horizon at the above referenced location.At the proposed test location, a Hyundai 235 excavator owned and operated by Randall Site Services, was used to excavate to a depth of 11' below existing ground surface. The soil horizon encountered at the excavation included: • 2" of grass and topsoil, • 15" of brown and gray moderately plastic silty CLAY (CL), • 38" of brown, yellow and gray clayey SILT (ML) with sand and gravel, • 67" of WEATHERED ROCK sampled as brown , yellow and gray SILT (ML) with seams of harder WEATHERED ROCK • No water was recorded at the time of excavation. • No indications of groundwater were observed to the depths explored. On May 23, 2023, CESI returned to the site to observe the conditions within the excavation. No water was observed in the excavation. As a result of our site observations, we offer the following: Sand Filter Seasonal Hiqh-Water Table Ground Elevation at Test Location Elevation 694.0 Bottom of Excavation Elevation 683.0 Water Level Elevation not encountered Bottom of Proposed SCM 689.0 Bottom Sand Filter System Elevation 685.0 24" Buffer Requirement Elevation 683.0 Based on our observations it was determined that the seasonal high groundwater elevation at the proposed sand filter location is deeper than 683.0. The seasonal highwater elevation supports the use of a sand filter at this location and elevation. 45 Spring Street, SW P.O. Box 268 Concord, NC 28026-0268 704-786-5404 www.cesicgs.com NC License No. C-0263 We appreciate the opportunity to be of service to you and we look forward to helping you through project completion. If you have any questions, please feel free to call. Respectfully submitted, .\ \`‘�N CA R p��.,,, oFEsS/0 ( tiq'- SE AL 24 James G. (Jay) Eaves III, PE Division Engineer 45 Spring Street, SW P.O. Box 268 Concord, NC 28026-0268 704-786-5404 www.cesicgs.com NC License No. C-0263