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HomeMy WebLinkAboutWQSV00006_Application_20240213 (2)�1 February 7, 2024 NCDEQ-DWR Highfill Infrastructure Engineering, P.C. 2703 Jones Franklin Road, Suite 201 H I G H F I LL Cary, North Carolina 27518 Tel 919-481-4342 � NC Firm License No. C5 WQS� (0 0 0 0 6 Attn:PERCS Unit Supervisor 512 N. Salibury St., Ste. 925 Raleigh, NC 27604 RE: Variance Request Paliouras Force Main Relocation HIGHFILL Project No.: GEM2201 Dear Reviewer: ["ECEIVED FEB 13 2024 NCDEQ/DWRNIDES The Paliouras Pump Station (PS) was constructed in 2014. The pump station conveys flow thru a 3-inch force main. According to NCDENR Minimum Design Criteria for Permitting of Pump Stations and Force Mains, a minimum 4-inch force main shall be used unless the force main is served by pumps capable of grinding, chopping, or cutting solids or a mechanical means of reducing the size of a three-inch solid and any trash or stringy material that can pass through a 4-inch hose is installed at the pump station. However, it appears that this requirement was overlooked when the pump station was reviewed and permitted in 2014. This issue was only realized once the design of the force main relocation had commenced. As part of this project, a grinder will be installed. Due to miscommunication, the Aldi Grocery store is ready to open; however, the grinder has yet to be installed. Due to a lengthy lead time, it is anticipated that the grinder will be installed in four months. This Variance request is to allow new wastewater flow produced from the Aldi Grocery store to be conveyed to the existing Paliouras PS prior to the installation of the grinder. Currently, it is estimated that the PS is receiving approximately 4,000 GPD from a Sheetz Gas Station that includes food preparation. The PS has been in operation under the current conditions for 10 years and there are no records of clogging of the pumps or force main. The Aldi Grocery store is estimated to add 1,921 GPD to the PS. We expect the characteristics of the flow will be very similar to the existing flow. A recent pump test revealed that the pumps are operating at approximately 100 GPM, which results in a force main velocity of 4.5 feet per second (fps). A velocity of 4.5 fps is able to clear settled deposits from the force main. Considering the historical performance of the PS, and the Aldi sewer will have similar characteristics to the ex. Sheetz sewer, it is anticipated that the PS will continue to operate as it has for the past 10 years Engineering is our profession. Service is our passion. NCDEQ-DWR February 7, 2024 until the grinder can be installed. However, in the event that a clog occurs, a maintenance company will be notified by the station's high-level alarm, at which time an emergency pump & haul operation will commence until the clog can be cleared. Please find enclosed two copies of each of the following documents for review and approval: • Request Form VADC 10-23. • Engineering Plans and Specifications. a Sewer Extension Application (FTA 10-23) and supporting documentation. Also, please find the following: 0 Application fee check in the amount of $600.00 Please contact me at 919-481-4342 or fallen@hiepc.com if you have any questions or concerns. Sincerely, HIGHFILL INFRASTRUCTURE ENGINEERING, P.C. V►• api. Jeremy Allen, PE Project Manager enclosures HIGHFILL I Page 2