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HomeMy WebLinkAboutNC0026921_Note to File_20000907Parkton — note to the file September 7, 2000, P.M., Belinda and myself stopped by the plant to visit with Roy Lowder. The facility looked good, I could see the bottom of the chlorine contact chamber. Parkton has purchased new ISCO samplers and Belinda recommended that a thermometer be installed for proof of proper temperature and that it be logged. Roy mentioned that he had been receiving considerable grit in the influent. I suggested that he look at his pump stations and collection system to try and locate the source. The plant chart recorder showed flow spikes and I suggested that he check his stations to see if two pumps were coming on at the same time, which that is what appeared to be happening. I noticed that the chlorinator was not feeding, by looking at the rotormeter. The flow pace appears to be way out of adjustment. Roy called the next day to say that he had been in touch with Regal and they had instructed him how to calibrate the flow pacer. Parkton is continuing to have fecal violations and I went over with Roy the proper protocol for collecting his fecal sample. I plan a flow -up next week Don Register file:///Untitled It has been brought to my attention that moneys are left over from a sewer collection system rehab project. The Town of Parkton WWTP has several immediate needs that this money could go a long way in , protecting water quality. I have worked with Parkton personnel on technical assistance at the wwtp and / there are a few things that are beyond their operating control such as the chlorine contact being too small. ✓ From Jan. 1999 - June 2000 there has been eleven fecal coliform violations reported on the D.M.R.. Technical assistance has shown that part of the problem was possibly too low of a chlorine residual, but more importantly it was determined the chlorine contact chamber is too small. This was determined by adding dye to the effluent entering the chamber with a flow rate during the test ranging from a rate of 110,000 gpd to 140,000 gpd. The detention time was determined to be nine minutes, which is much less than the required thirty minutes. The wwtp also needs a automatic fine tooth barscreen in the place of the current coarse manual screen. This facility is not manned full-time, so rags accumilate heavily on the screen. Grit in the oxidation ditches has also been a serious problem, because the facility does not have grit removal. All of the grit in the influent wastewater settles in the oxidation ditches reducing it's volume and the quality of it's effluent, risking non-compliance with their permit limits. To be assured that water quality is not compromised, these corrections need to be made to this facility. I hope the unspent money can be used for this critical and much needed water quality purpose. If I can further explain or assist in any way please call me at the Fayetteville Regional Office, DWQ. 910-486-1541 Don Register, Environmental Tech. IV. 1 of 1 02/28/2001 11:00 AM