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HomeMy WebLinkAboutNC0037508_WWTP Inspection_20020102A76. NCDENR North Carolina Department of Environment and Natural Resources Michael F. Easley, Governor January 2, 2002 Mr. Dennis Brobst Moore County Public Works Director PO Box 1978 Carthage, NC 28327 SUBJECT: Compliance Evaluation Inspection Moore County Water Pollution Control Plant NPDES Permit No. NC0037508 Moore County Dear Mr. Brobst: C,O4t-c.eAD 1/1/02, 4fi William G. Ross Jr., Secretary Gregory J. Thorpe, Ph.D. Acting Director Division of Water Quality Enclosed is a copy of the Compliance Evaluation Inspection conducted December 20, 2001. As part of the inspection a tour of the Wastewater Treatment Plant was conducted. All observations and recommendations are in Part D. Summary of Findings/Comments of this inspection report. The cooperation of Mr. Delmo Frye, Grade IV ORC, was appreciated. During the inspection a copy of the NPDES Compliance Reminders were reviewed and left with facility staff. As a reminder preservation of the Waters of the State can only be acquired through consistent NPDES permit compliance. Please review the attached report. If you or your staff have any questions do not hesitate to contact me at 910-486-1541. Sincerely, Belinda S. Henson Environmental Chemist /bsh Enclosures cc: Mr. Delmo Frye, ORC, Moore Couhty Water Pollution Plant Fayetteville Regional Office 225 Green Street — Suite 714, Fayetteville, North Carolina 28301-5043 Phone: 910-486-1541 \ FAX: 910-486-07071 Internet: www.enr.state.nc.us/.ENR An Equal Opportunity \ Affirmative Action Employer — 50% Recycled 110% Post Consumer Paper NPDES COMPLIANCE INSPECTION REPORT North Carolina Division of Water Quality Fayetteville Regional Office Section A. National Data System Coding Transaction Code: N NPDES NO. NC0037508 Date: 011220 Inspection Type: C Inspector: S Facility Type: 1 Reserved. Facility Evaluation Rating: 4 BI: N QA: N Reserved: Section B: Facility Data Name and Location of Facility inspected: Moore County Water Pollution Control Plant Entry Time/Date: 8:35am/011220 -Permit Effective Date: 000601 Exit Tirne/Date: 11:30pm/011220 Permit Expiration Date: 040731 Narne(s), Title(s) of On -Site Representative(s): De1mo Frye (Certified Grade IV) - "ORC" Jeff Corder (Certified Grade IV) - "Backup Operator" Phone Number(s): (910)281-3146 Name, Title and Address of Responsible Official: Mr. Dennis Brobst, Public Works Director PO Box 1927 Carthage, NC 28327 Contacted: no Section C: Areas Evaluated During Inspection (S = Satisfactory, M = Marginal, U = Unsatisfactory, N = Not Evaluated, N/A = Not Applicable) Permit: S Records/Reports: S Facility Site Review: S .Flow Measurement: S Laboratory: S Effluent/Receiving Waters: S Pretreatment: N Compliance Schedule: N/A Self -Monitoring Program: S Operation &Maintenance: S Sludge Disposal: S Other: Brobst Page 3 January 2, 2002 Section D: Summary of Findings/Comments: 1. The County continues to contract the operations of the wastewater treatment plant to "American Water Services". 2, The waste stream. is made up of domestic and industrial. The facility has a pretreatment program which has the following Significant Industrial Users (BTUs): Intec, Ingersoll Rand, and Erico. Wastewater from Camp McCall is received into the headworks of the facility by one designated pipe. 3. The automatic bar screen appeared to be operational. It operates on a timer or a float system. Screenings are disposed of through the Uwharrie Environmental landfill. • 4. The facility accepts septage-from various sites. The septage is discharged into a manhole at the headworks of the plant. 5. The grit removal. system was operational. 6. The influent composite sampler temperature was 1 degree C. The acceptable temperature range of samples during storage and stored sample extracts, is 1.0 - 4.4 degrees C. 7 Two blowers are used at the headworks of the plant to add aeration. One blower is normally all that is needed for post aeration. 8. The facility has two (2)_ primary clarifiers. One (1) was operational and the other was down for repairs. 9. The first stage aeration basin appeared to be operational. This component of treatment has 4 compartments. Two' compartments were utilized for treating the wastewater at the time of the inspection. The Mixed Liquor Suspended Solids (MLSS) results on the day of the inspection was 1950 mg/L. The Royce Model 711 is used to analyze MLSS. 10. The two (2) intermediate clarifiers appeared to be operating adequately. 11. The second stage aeration basin appeared to be operating adequately. The MLSS .results on the day of the inspection was 1500 mg/L. Lime is added to this area when additional treatment is needed. Polymer is added at the end of the aeration to assist with solids settling. 12. The two (2) final,clarifiers appeared to be operational. The sludge depths in each clarifier was less than 1 foot with a tank depth of 15 feet. . 13. The effluent is disinfected with chlorine. The chlorine contact tank appeared to be clean. 14. Sulfur Dioxide is used to dechlorinate the effluent. Brobst Page 4 January 2, 2002 15. The effluent appeared to be free of solids. The effluent outfall was easily accessible. 16. The effluent composite sampler refrigerator temperature was 1 degree C. The effluent composite sampler is not flow proportional at the present time due to an electical storm which caused it's malfunction. Repairs should be made immediately to continue effluent flow proportional sampling. 17. The DAP units are not utilized at this time. 18. Wasting from the clarifiers is on the average of 50,000 gallons/day. 19. Sludge from the primary, intermediate and final clarifiers flows to the primary digester where it is heated up to 99 degrees Celsius and travels to the top of the digester. After the sludge is heated it is pumped to the secondary digester where it goes to the drying beds. From the drying beds it is disposed of in the Uwhan-ie Environmental Landfill. The facility has 36 drying beds. Some vegetative growth was noted in some of the drying beds. These areas should be cleaned and maintained to ensure proper drying of the sludge. The facility has a permit (#WQ0018018) to land apply sludge effective March 30, 2001. . 20. The influent flow meter is used in reporting on the Discharge Monitoring Reports (DMRs). The meter was calibrated August 10, 2001 by "Carolina Technical Services, Inc". As stated in the calibration report the % error is 0. 21. The facility has a certified laboratory on site which analyzes most NPDES permit required parameters. All other parameters are analyzed by the commercial laboratory "TBL". 22. Laboratory records were reviewed for the months March, April.andMay 2001 and compared to DMRs. All reviewed data appeared to be accurately reported. PLEASE RESPOND IN WRITING WITH A PLAN OF ACTION FOR ITEM #16 BY JANUARY 31, 2002, Name and Signature of Inspector Agency/Office/Telephone Date Belinda S. Henson j, it '7q.Cii 'fit Naive and Signature of Reviewer Paul Rawls/ Action Taken DENR/Fayetteville/(910)486-1541 1 Agency/Office/Telephone Date DENR/Fayetteville/(910)486-1541 Regulatory Office Use Only Compliance Status _Noncompliance _Compliance Date Section D: Summary of Findings/Comments Brief Facility Description: The facility operates a 6.7 MGD WWTP consisting of preaeration, grit removal, primary. clarification, first stage activated sludge. intermediate clarification, second stage aeration, final clarification. anaerobic sludge digestion. sludge drying beds, post aeration, chlorination and dechlorination. FACILITY SITE REVIEW s 3 No N/A 1. Treatment units properly operated and maintained. �Ye No N/A 2. Standby power or other equivalent provision provided. Yes No N/A 3. Adequate alarm system for power or equipment failure available. 4. Sludge disposal procedures appropriate: Tep No N/A a. Disposal of sludge according to regulations Yes) No N/A b. State approval for sludge disposal received. (sue' No N/A 5. Sufficient sludge disposed of to maintain treatment process equilibrium. (VeJ No N/A 6. The ORC and Backup Operator are officially designated with NCDENR/DWQ Training and Certification Unit. Cues) No N/A 7. Adequate spare parts and supplies inventory maintained. es' No N/A 8. Plant has general safety structures such as rails around or covers over tanks, pits, or wells. (Yes No N/A 9. Plant is generally clean, free from open trash areas. 10. Screening: Yes No (LA a. Manual &es) No N/A b. Mechanical Les) No .N/A c. Buildup of debris Yes No N/A d. Screenings properly disposed of. Yes To) N/A Yes «o) N/A Yes No N/A 11. Grit Removal: a. Excessive organic content in the grit chamber b. Excessive odors c. Grit properly disposed of. Page 2 12. Primary clarifier: Yes N/A a. Excessive gas bubbles Yes N/A b. Black and odorous wastewater Yes (N N/A c. Poor suspended solids removed Yes N/A d. Excessive buildup of solids in center well of circular clarifier No " N/A e. Weirs level Yes To` N/A f. Weir blockage Yes QS@ N/A g. Evidence of short circuiting Yes N/A h. " Lack of adequate scum removal Yes To N/A i. Excessivefloating sludge Yes 10 N/A j. Broken sludge scraper: Yes No Yes No Yes No Yes No Yes No Yes . No Yes No Yes No N/A N/A N/A N/A N/A N/A N/A 13. Trickling Filter: a. Trickling filter ponding(indicating clogged media) b. Leak at center column of trickling filter's distribution arms c. Uneven distribution of flow on trickling filter surface d. Uneven or discolored growth e. Excessive sloughing of growth f. Odor g. Clogging of trickling filter's distribution arm orifices h. Filter flies, worms, or snails. 14. Activated Sludge Basins/Oxidation Ditches: Yes N/A a. Dead spots Yes Nob. Failure of surface aerators Yes N/A • c. Air rising in clumps Yes N/A d. Dark foam or bad color Yes (No) N/A • . e. Thick billows of white, sudsy foam Yes I N/A ' f Air rising unevenly Yes N/A . g. Excessive air leaks in compressed air piping. 15. Yes No CN/ Yes No " N/A Yes No N/A Yes No N/A Stabilization Ponds/Lagoons: a. Excessive weeds including duckweed in stabilization ponds b. Dead fish or aquatic organisms c. • Buildup of solids around influent pipe d. Excessive scum on surface. Page 3 16. Secondary Clarifier: Yes N/A a. . Excessive gas bubbles on surface ems' No N/A ' b. Level overflow weirs Yes No N/A c. Weir blockage Yes 1 0 N/A d. Evidence of short circuiting Yes N/A e: Excessive buildup of solids in center well of circular clarifier . Yes) No N/A f Pin floc in overflow -Se, vile- vri- c iq:.s ' = Yes No N/A g. Effective scum rake CM‘g No N/A h. Floating sludge on surface Yes N/A i. Excessive high sludge blanket Yes ® N/A j. Clogged sludge withdrawal ports on secondary clarifier. 17. Filtration: Yes No a. Filter surface clogging Yes No N/A 'b. Short filter run Yes No . N/A c. Gravel displacement of filter media Yes No N/A d. Loss of filter media during backwashing' Yes No N/A e.. Recycled filter backwash water in excess of 5 percent Yes No N/A f Formation of mudballs in filter media. Yes' N/A Yes N/A Yes 0) N/A s No N/A Yes No N/A No N/A No N/A @@ No N/A 18. Chlorination Unit: a. Sludge buildup in contact chamber b. Gas bubbles c. Floating scum and/or solids d. Adequate ventilation of chlorine feeding room and storage area e. NIOSH-approved 30 minute air pack f All standing chlorine cylinders chained in place g. All personnel trained in the use of chlorine h. Proper chlorine feed, storage, and reserve supply. Yes No O 19. Ultraviolet radiation disinfection present and in use. 20. •Dechlorinatiori: CY�s No .N/A a. Proper storage of sulfur dioxide cylinders Ye" No N/A b. Adequate ventilation of sulfur dioxide feeding room Tsp No N/A c. Automatic sulfur dioxide feed or feedback control operating properly: 21. Aerobic Digester: Yes No I� a. Excessive foaming in tank Yes No 'N/A b: Noxious odor Yes No N/A c Mechanical aeration failure Yes No N/A d.- Clogging of diffusers. Page 4 22. Anaerobic Digester: Yes No 1'dTA a. Floating cover tilting es, No N/A b. Gas burner operative 23. sludge Drying and/or disposal: Yes SO N/A a. Poor sludge distribution on drying beds ies No N/A b. Vegetation in drying beds Ye No N/A c. Dry sludge remaining in drying beds es� No N/A d. Dry sludge stored on site No N/A e. Filtrate from sludge drying beds returned to front of plant No N/A f Sludge disposal through county landfill. Yes N , N'A g. Sludge land applied. 24. Filter Press: Yes NoiA a. High level of solids in filtrate from filter presses or vacuum filters Yes No N/A b. Thin filter cake caused by poor dewatering Yes No N/A c. Sludge buildup on belts and/or rollers of filter press Yes No N/A d. Excessive moisture in belt filter press sludge cake. Yes No(N7A Yes No N/A Yes No N/A 25. Polishing Ponds or Tanks: a. Objectionable odor, excessive foam, floating solids, or oil sheens on water surface b. Solids or scum accumulations in tank or at side of pond c. Evidence of bypassed polishing ponds or tanks because of low capacity. 26. Plant Effluent: Yes (j N/A a. Excessive suspended solids, turbidity, foam, grease, scum, color, and other macroscopic particulate matter present Yes N/A b. Potential toxicity (dead fish, dead plant at discharge) oyes' No N/A c. Outfall discharge line easily accessible. 27.. Flow Measurement: CYO No N/A a. Proper placement of flow measurement device No N/A b. Flow meter calibrated CEO N/A c. Buildup of solids in flume or weir Yes Nb N/A d. Broken or cracked flume or weir Yes No e. Clogged or broken stilling wells Yes (N N/A f. Weir plate edge corroded or damaged (Ye's No N/A g. Flow measurement error less than 10%. Page 5 s� No N/A No N/A E._ No N/A Yes No N/A 28. Sampling: a. Sampling and analysis completed on parameters specified by permit b. Composite sample temperatures maintained at.4 degrees Celsius or less (but above freezing) during sampling c. Contract laboratory used for sample analysis d. Effluent composite samples obtained are flow proportional. CYe,§) No N/A (MS) No N/A : No N/A «eJ No N/A T -4) No N/A e§` No N/A es," No N/A 6.a No N/A Yes No N/A No N/A (Ys No N/A Yes No N/A Yes No N/A 'No N/A REOORDKEEPING AND REPORTING 1. Records and reports maintained as required by permit. 2. All required information available, complete, and current. 3. Records maintained for 3 years and all sludge records maintained for 5 years. 4. Analytical results consistent with data reported on DMRs. 5. Sampling and analyses data adequate and include: a. Dates, times, and location of sampling b'. Name of individual performing sampling c. Results of analyses and calibration d. Dates of analyses_ e.. Name of person performing analyses. 6. Monitoring records adequate and include: a. Monitoring charts kept for 3 years b. Flowmeter calibration records kept for 3 years. 7. The pH meter is calibrated daily with two buffers and checked with a third buffer and properly documented. 8. Expiration dates of pH buffers adequate. 9. All thermometers used in NPDES permit reporting is calibrated annually with an NIST certified thermometer or a traceable thermometer annually and documented. 10. The following NPDES permit required parameters are analyzed on site: pH, Temperature, Dissolved Oxygen and Chlorine Residual. Page 6 Yes :No N/A Yes No N/A Yes No N/A s Tlo N/A - Yes> No N/A des' No N/A Yes No Yes No A c No N/A (' No N/A ees;' No N/A s: No N/A s '' No N/A No N/A No N/A CeSD No N/A 11. The NPDES permit required parameter Total Chlorine Residual is analyzed by approved method. 12. BOD incubator temperature maintained at 20 +/- 1 Degrees Celsius and the temperature maintained in a log for every day of Operation. 13. .Fecal coliform incubator maintained at 44.5 +/- 0.2 Degree Celsius and the temperature maintained in a log for every day of operation. 14. Plant records adequate and include: a. O & M Manual b. "As -built" engineering drawings c. Schedules and dates of equipment maintenance repairs d. Equipment data cards. 15. Permittee is meeting compliance schedule. 16. DMRs complete and include all NPDES permit required parameters. 17. The facility has a permitted flow greater than 5 MGD and is required to operate seven days per week 24 hours a day. 18. ORC visitation logs available and current. 19. ORC certified at a level equal to or greater than the classification of the wastewater facility, 20. Backup Operator certified at one level less than the classification of the wastewater facility or greater. 21. Current copy of the complete NPDES permit on site. 22. Facility description verified as contained in NPDES permit. 23. Facility analyzes process control parameters for example: v1I.,SS, MCRT, Settleable Solids and others that are applicable. Yes No N/A 24. Revised 7/16/01 by Belinda Henson Industrial Waste Surveys (IWS) sent to all possible Significant Industrial Users (SIiJs) within the last five years (especially new industries). America . Water Services, Incl. An American Water Works Company January 30, 2002 North Carolina Department Of Environment and Natural Resources Division of Water Quality Attn: Belinda S. Henson 225 Green Street Suite 714 Fayetteville, North Carolina 28301-5043 SUBJECT: Compliance Evaluation Inspection Moore County Water Pollution Control Plant NPDES Permit No. NC0037508 Moore County Dear Ms Henson: 'JIAN 3 12002 In response to your letter dated January 2, 2002 we would like to provide you with a response in regard to a plan of action on item #16, "the composite sampler is currently not flow proportional". We currently have acquired the services of KM Industrial Electric, LLC to correct this problem. They have thoroughly investigated the problem and has assured us the problem would be corrected no later than February 15, 2002 (see attached). We would also like to bring to your attention a typographical error in item # 19 that states "Primary digester where it is heated up to 99 degrees Celsius". The unit should be Fahrenheit instead of Celsius. If you have any other questions please feel free to contact us at 1-910-281-3146. Thank You James Frye ORC, Moore County Wastewater Treatment CC: Dewayne G. Dousay, American Water Services, Inc. Dennis Brobst, Moore County Public Works Director 1/29/2002 17:39 9104281526 KM INDUSTRIAL ELEC PAGE 01 =NM KM INDUSTRIAL. ELECTRIC, LLC. 201 McCaskill Street • eisco , N.C. 27209 Office (910) 428-1414 January 29, 2002 American Water Services Inc. P.O. Box 813 Pinebluhi NC. 28373 910 281-3146 910 281-2047 fax Reference: Wiring to Sampler @ Effluent Moore County Waste Water Treatment Plant Attention: James Frye Auer testing the wiring, to the Plant Effluent Sampler it is my recommendation that this circuit be replaced. Circuit is defective and must be replaced to resolve current condition. This will be repair by February 15, 2002 Thank You, David McCollum President C:1My Documents\moorewwtpeffiuentsump1er.doe