HomeMy WebLinkAboutNC0037508_WWTP Inspection_20020102A76.
NCDENR
North Carolina Department of Environment and Natural Resources
Michael F. Easley, Governor
January 2, 2002
Mr. Dennis Brobst
Moore County Public Works Director
PO Box 1978
Carthage, NC 28327
SUBJECT: Compliance Evaluation Inspection
Moore County Water Pollution Control Plant
NPDES Permit No. NC0037508
Moore County
Dear Mr. Brobst:
C,O4t-c.eAD
1/1/02,
4fi
William G. Ross Jr., Secretary
Gregory J. Thorpe, Ph.D.
Acting Director
Division of Water Quality
Enclosed is a copy of the Compliance Evaluation Inspection conducted December 20, 2001.
As part of the inspection a tour of the Wastewater Treatment Plant was conducted. All observations and
recommendations are in Part D. Summary of Findings/Comments of this inspection report. The cooperation
of Mr. Delmo Frye, Grade IV ORC, was appreciated. During the inspection a copy of the NPDES
Compliance Reminders were reviewed and left with facility staff. As a reminder preservation of the Waters
of the State can only be acquired through consistent NPDES permit compliance.
Please review the attached report. If you or your staff have any questions do not hesitate to
contact me at 910-486-1541.
Sincerely,
Belinda S. Henson
Environmental Chemist
/bsh
Enclosures
cc: Mr. Delmo Frye, ORC, Moore Couhty Water Pollution Plant
Fayetteville Regional Office
225 Green Street — Suite 714, Fayetteville, North Carolina 28301-5043
Phone: 910-486-1541 \ FAX: 910-486-07071 Internet: www.enr.state.nc.us/.ENR
An Equal Opportunity \ Affirmative Action Employer — 50% Recycled 110% Post Consumer Paper
NPDES COMPLIANCE INSPECTION REPORT
North Carolina Division of Water Quality
Fayetteville Regional Office
Section A. National Data System Coding
Transaction Code: N NPDES NO. NC0037508 Date: 011220 Inspection Type: C
Inspector: S Facility Type: 1 Reserved.
Facility Evaluation Rating: 4 BI: N QA: N Reserved:
Section B: Facility Data
Name and Location of Facility inspected:
Moore County Water Pollution Control Plant
Entry Time/Date: 8:35am/011220 -Permit Effective Date: 000601
Exit Tirne/Date: 11:30pm/011220 Permit Expiration Date:
040731
Narne(s), Title(s) of On -Site Representative(s):
De1mo Frye (Certified Grade IV) - "ORC"
Jeff Corder (Certified Grade IV) - "Backup Operator"
Phone Number(s): (910)281-3146
Name, Title and Address of Responsible Official:
Mr. Dennis Brobst, Public Works Director
PO Box 1927
Carthage, NC 28327
Contacted: no
Section C: Areas Evaluated During Inspection
(S = Satisfactory, M = Marginal, U = Unsatisfactory, N = Not Evaluated, N/A = Not Applicable)
Permit: S
Records/Reports: S
Facility Site Review: S
.Flow Measurement: S
Laboratory: S
Effluent/Receiving Waters: S
Pretreatment: N
Compliance Schedule: N/A
Self -Monitoring Program: S
Operation &Maintenance: S
Sludge Disposal: S
Other:
Brobst
Page 3
January 2, 2002
Section D: Summary of Findings/Comments:
1. The County continues to contract the operations of the wastewater treatment plant to "American
Water Services".
2,
The waste stream. is made up of domestic and industrial. The facility has a pretreatment program
which has the following Significant Industrial Users (BTUs): Intec, Ingersoll Rand, and Erico.
Wastewater from Camp McCall is received into the headworks of the facility by one designated
pipe.
3. The automatic bar screen appeared to be operational. It operates on a timer or a float system.
Screenings are disposed of through the Uwharrie Environmental landfill.
• 4. The facility accepts septage-from various sites. The septage is discharged into a manhole at the
headworks of the plant.
5. The grit removal. system was operational.
6. The influent composite sampler temperature was 1 degree C. The acceptable temperature range of
samples during storage and stored sample extracts, is 1.0 - 4.4 degrees C.
7 Two blowers are used at the headworks of the plant to add aeration. One blower is normally all that
is needed for post aeration.
8. The facility has two (2)_ primary clarifiers. One (1) was operational and the other was down for
repairs.
9. The first stage aeration basin appeared to be operational. This component of treatment has 4
compartments. Two' compartments were utilized for treating the wastewater at the time of the
inspection. The Mixed Liquor Suspended Solids (MLSS) results on the day of the inspection was
1950 mg/L. The Royce Model 711 is used to analyze MLSS.
10. The two (2) intermediate clarifiers appeared to be operating adequately.
11. The second stage aeration basin appeared to be operating adequately. The MLSS .results on the day
of the inspection was 1500 mg/L. Lime is added to this area when additional treatment is needed.
Polymer is added at the end of the aeration to assist with solids settling.
12. The two (2) final,clarifiers appeared to be operational. The sludge depths in each clarifier was less
than 1 foot with a tank depth of 15 feet. .
13. The effluent is disinfected with chlorine. The chlorine contact tank appeared to be clean.
14. Sulfur Dioxide is used to dechlorinate the effluent.
Brobst
Page 4
January 2, 2002
15. The effluent appeared to be free of solids. The effluent outfall was easily accessible.
16. The effluent composite sampler refrigerator temperature was 1 degree C. The effluent composite
sampler is not flow proportional at the present time due to an electical storm which caused it's
malfunction. Repairs should be made immediately to continue effluent flow proportional
sampling.
17. The DAP units are not utilized at this time.
18. Wasting from the clarifiers is on the average of 50,000 gallons/day.
19. Sludge from the primary, intermediate and final clarifiers flows to the primary digester where it is
heated up to 99 degrees Celsius and travels to the top of the digester. After the sludge is heated it
is pumped to the secondary digester where it goes to the drying beds. From the drying beds it is
disposed of in the Uwhan-ie Environmental Landfill. The facility has 36 drying beds. Some
vegetative growth was noted in some of the drying beds. These areas should be cleaned and
maintained to ensure proper drying of the sludge. The facility has a permit (#WQ0018018) to land
apply sludge effective March 30, 2001.
. 20. The influent flow meter is used in reporting on the Discharge Monitoring Reports (DMRs). The
meter was calibrated August 10, 2001 by "Carolina Technical Services, Inc". As stated in the
calibration report the % error is 0.
21.
The facility has a certified laboratory on site which analyzes most NPDES permit required
parameters. All other parameters are analyzed by the commercial laboratory "TBL".
22. Laboratory records were reviewed for the months March, April.andMay 2001 and compared to
DMRs. All reviewed data appeared to be accurately reported.
PLEASE RESPOND IN WRITING WITH A PLAN OF ACTION FOR ITEM #16 BY
JANUARY 31, 2002,
Name and Signature of Inspector Agency/Office/Telephone Date
Belinda S. Henson
j, it '7q.Cii 'fit
Naive and Signature of Reviewer
Paul Rawls/
Action Taken
DENR/Fayetteville/(910)486-1541 1
Agency/Office/Telephone Date
DENR/Fayetteville/(910)486-1541
Regulatory Office Use Only
Compliance Status
_Noncompliance
_Compliance
Date
Section D: Summary of Findings/Comments
Brief Facility Description:
The facility operates a 6.7 MGD WWTP consisting of preaeration, grit removal, primary.
clarification, first stage activated sludge. intermediate clarification, second stage aeration, final
clarification. anaerobic sludge digestion. sludge drying beds, post aeration, chlorination and
dechlorination.
FACILITY SITE REVIEW
s 3 No N/A 1. Treatment units properly operated and maintained.
�Ye No N/A 2. Standby power or other equivalent provision provided.
Yes No N/A 3. Adequate alarm system for power or equipment failure available.
4. Sludge disposal procedures appropriate:
Tep No N/A a. Disposal of sludge according to regulations
Yes) No N/A b. State approval for sludge disposal received.
(sue' No N/A 5. Sufficient sludge disposed of to maintain treatment process equilibrium.
(VeJ No N/A 6. The ORC and Backup Operator are officially designated with
NCDENR/DWQ Training and Certification Unit.
Cues) No N/A 7. Adequate spare parts and supplies inventory maintained.
es' No N/A 8. Plant has general safety structures such as rails around or covers over
tanks, pits, or wells.
(Yes No N/A 9. Plant is generally clean, free from open trash areas.
10. Screening:
Yes No (LA a. Manual
&es) No N/A b. Mechanical
Les) No .N/A c. Buildup of debris
Yes No N/A d. Screenings properly disposed of.
Yes To) N/A
Yes «o) N/A
Yes No N/A
11. Grit Removal:
a. Excessive organic content in the grit chamber
b. Excessive odors
c. Grit properly disposed of.
Page 2
12. Primary clarifier:
Yes N/A a. Excessive gas bubbles
Yes N/A b. Black and odorous wastewater
Yes (N N/A c. Poor suspended solids removed
Yes N/A d. Excessive buildup of solids in center well of circular clarifier
No " N/A e. Weirs level
Yes To` N/A f. Weir blockage
Yes QS@ N/A g. Evidence of short circuiting
Yes N/A h. " Lack of adequate scum removal
Yes To N/A i. Excessivefloating sludge
Yes 10 N/A j. Broken sludge scraper:
Yes No
Yes No
Yes No
Yes No
Yes No
Yes . No
Yes No
Yes No
N/A
N/A
N/A
N/A
N/A
N/A
N/A
13. Trickling Filter:
a. Trickling filter ponding(indicating clogged media)
b. Leak at center column of trickling filter's distribution arms
c. Uneven distribution of flow on trickling filter surface
d. Uneven or discolored growth
e. Excessive sloughing of growth
f. Odor
g. Clogging of trickling filter's distribution arm orifices
h. Filter flies, worms, or snails.
14. Activated Sludge Basins/Oxidation Ditches:
Yes N/A a. Dead spots
Yes Nob. Failure of surface aerators
Yes N/A • c. Air rising in clumps
Yes N/A d. Dark foam or bad color
Yes (No) N/A • . e. Thick billows of white, sudsy foam
Yes I N/A ' f Air rising unevenly
Yes N/A . g. Excessive air leaks in compressed air piping.
15.
Yes No CN/
Yes No " N/A
Yes No N/A
Yes No N/A
Stabilization Ponds/Lagoons:
a. Excessive weeds including duckweed in stabilization ponds
b. Dead fish or aquatic organisms
c. • Buildup of solids around influent pipe
d. Excessive scum on surface.
Page 3
16. Secondary Clarifier:
Yes N/A a. . Excessive gas bubbles on surface
ems' No N/A ' b. Level overflow weirs
Yes No N/A c. Weir blockage
Yes 1 0 N/A d. Evidence of short circuiting
Yes N/A e: Excessive buildup of solids in center well of circular clarifier
. Yes) No N/A f Pin floc in overflow -Se, vile- vri- c iq:.s ' =
Yes No N/A g. Effective scum rake
CM‘g No N/A h. Floating sludge on surface
Yes N/A i. Excessive high sludge blanket
Yes ® N/A j. Clogged sludge withdrawal ports on secondary clarifier.
17. Filtration:
Yes No a. Filter surface clogging
Yes No N/A 'b. Short filter run
Yes No . N/A c. Gravel displacement of filter media
Yes No N/A d. Loss of filter media during backwashing'
Yes No N/A e.. Recycled filter backwash water in excess of 5 percent
Yes No N/A f Formation of mudballs in filter media.
Yes' N/A
Yes N/A
Yes 0) N/A
s No N/A
Yes No N/A
No N/A
No N/A
@@ No N/A
18. Chlorination Unit:
a. Sludge buildup in contact chamber
b. Gas bubbles
c. Floating scum and/or solids
d. Adequate ventilation of chlorine feeding room and storage area
e. NIOSH-approved 30 minute air pack
f All standing chlorine cylinders chained in place
g. All personnel trained in the use of chlorine
h. Proper chlorine feed, storage, and reserve supply.
Yes No O 19. Ultraviolet radiation disinfection present and in use.
20. •Dechlorinatiori:
CY�s No .N/A a. Proper storage of sulfur dioxide cylinders
Ye" No N/A b. Adequate ventilation of sulfur dioxide feeding room
Tsp No N/A c. Automatic sulfur dioxide feed or feedback control operating
properly:
21. Aerobic Digester:
Yes No I� a. Excessive foaming in tank
Yes No 'N/A b: Noxious odor
Yes No N/A c Mechanical aeration failure
Yes No N/A d.- Clogging of diffusers.
Page 4
22. Anaerobic Digester:
Yes No 1'dTA a. Floating cover tilting
es, No N/A b. Gas burner operative
23. sludge Drying and/or disposal:
Yes SO N/A a. Poor sludge distribution on drying beds
ies No N/A b. Vegetation in drying beds
Ye No N/A c. Dry sludge remaining in drying beds
es� No N/A d. Dry sludge stored on site
No N/A e. Filtrate from sludge drying beds returned to front of plant
No N/A f Sludge disposal through county landfill.
Yes N , N'A g. Sludge land applied.
24. Filter Press:
Yes NoiA a. High level of solids in filtrate from filter presses or vacuum filters
Yes No N/A b. Thin filter cake caused by poor dewatering
Yes No N/A c. Sludge buildup on belts and/or rollers of filter press
Yes No N/A d. Excessive moisture in belt filter press sludge cake.
Yes No(N7A
Yes No N/A
Yes No N/A
25. Polishing Ponds or Tanks:
a. Objectionable odor, excessive foam, floating solids, or oil sheens on
water surface
b. Solids or scum accumulations in tank or at side of pond
c. Evidence of bypassed polishing ponds or tanks because of low
capacity.
26. Plant Effluent:
Yes (j N/A a. Excessive suspended solids, turbidity, foam, grease, scum, color, and
other macroscopic particulate matter present
Yes N/A b. Potential toxicity (dead fish, dead plant at discharge)
oyes' No N/A c. Outfall discharge line easily accessible.
27.. Flow Measurement:
CYO No N/A a. Proper placement of flow measurement device
No N/A b. Flow meter calibrated
CEO N/A c. Buildup of solids in flume or weir
Yes Nb N/A d. Broken or cracked flume or weir
Yes No e. Clogged or broken stilling wells
Yes (N N/A f. Weir plate edge corroded or damaged
(Ye's No N/A g. Flow measurement error less than 10%.
Page 5
s� No N/A
No N/A
E._ No N/A
Yes No N/A
28. Sampling:
a. Sampling and analysis completed on parameters specified by permit
b. Composite sample temperatures maintained at.4 degrees Celsius or
less (but above freezing) during sampling
c. Contract laboratory used for sample analysis
d. Effluent composite samples obtained are flow proportional.
CYe,§) No N/A
(MS) No N/A
: No N/A
«eJ No N/A
T -4) No N/A
e§` No N/A
es," No N/A
6.a No N/A
Yes No N/A
No N/A
(Ys No N/A
Yes No N/A
Yes No N/A
'No N/A
REOORDKEEPING AND REPORTING
1. Records and reports maintained as required by permit.
2. All required information available, complete, and current.
3. Records maintained for 3 years and all sludge records maintained for 5
years.
4. Analytical results consistent with data reported on DMRs.
5. Sampling and analyses data adequate and include:
a. Dates, times, and location of sampling
b'. Name of individual performing sampling
c. Results of analyses and calibration
d. Dates of analyses_
e.. Name of person performing analyses.
6. Monitoring records adequate and include:
a. Monitoring charts kept for 3 years
b. Flowmeter calibration records kept for 3 years.
7. The pH meter is calibrated daily with two buffers and checked with a
third buffer and properly documented.
8. Expiration dates of pH buffers adequate.
9. All thermometers used in NPDES permit reporting is calibrated
annually with an NIST certified thermometer or a traceable
thermometer annually and documented.
10. The following NPDES permit required parameters are analyzed on site:
pH, Temperature, Dissolved Oxygen and Chlorine Residual.
Page 6
Yes :No N/A
Yes No N/A
Yes No N/A
s Tlo N/A
- Yes> No N/A
des' No N/A
Yes No
Yes No A
c No N/A
(' No N/A
ees;' No N/A
s: No N/A
s '' No N/A
No N/A
No N/A
CeSD No N/A
11. The NPDES permit required parameter Total Chlorine Residual is
analyzed by approved method.
12. BOD incubator temperature maintained at 20 +/- 1 Degrees Celsius
and the temperature maintained in a log for every day of Operation.
13. .Fecal coliform incubator maintained at 44.5 +/- 0.2 Degree Celsius and
the temperature maintained in a log for every day of operation.
14. Plant records adequate and include:
a. O & M Manual
b. "As -built" engineering drawings
c. Schedules and dates of equipment maintenance repairs
d. Equipment data cards.
15. Permittee is meeting compliance schedule.
16. DMRs complete and include all NPDES permit required parameters.
17. The facility has a permitted flow greater than 5 MGD and is required
to operate seven days per week 24 hours a day.
18. ORC visitation logs available and current.
19. ORC certified at a level equal to or greater than the classification of
the wastewater facility,
20. Backup Operator certified at one level less than the classification of
the wastewater facility or greater.
21. Current copy of the complete NPDES permit on site.
22. Facility description verified as contained in NPDES permit.
23. Facility analyzes process control parameters for example: v1I.,SS,
MCRT, Settleable Solids and others that are applicable.
Yes No N/A 24.
Revised 7/16/01
by Belinda Henson
Industrial Waste Surveys (IWS) sent to all possible Significant
Industrial Users (SIiJs) within the last five years (especially new
industries).
America . Water Services, Incl.
An American Water Works Company
January 30, 2002
North Carolina Department Of Environment and Natural Resources
Division of Water Quality
Attn: Belinda S. Henson
225 Green Street
Suite 714
Fayetteville, North Carolina 28301-5043
SUBJECT: Compliance Evaluation Inspection
Moore County Water Pollution Control Plant
NPDES Permit No. NC0037508
Moore County
Dear Ms Henson:
'JIAN 3 12002
In response to your letter dated January 2, 2002 we would like to provide you with a response in
regard to a plan of action on item #16, "the composite sampler is currently not flow proportional".
We currently have acquired the services of KM Industrial Electric, LLC to correct this problem.
They have thoroughly investigated the problem and has assured us the problem would be corrected no later
than February 15, 2002 (see attached).
We would also like to bring to your attention a typographical error in item # 19 that states
"Primary digester where it is heated up to 99 degrees Celsius". The unit should be Fahrenheit
instead of Celsius.
If you have any other questions please feel free to contact us at 1-910-281-3146.
Thank You
James Frye
ORC, Moore County Wastewater Treatment
CC: Dewayne G. Dousay, American Water Services, Inc.
Dennis Brobst, Moore County Public Works Director
1/29/2002 17:39 9104281526
KM INDUSTRIAL ELEC PAGE 01
=NM
KM INDUSTRIAL. ELECTRIC, LLC.
201 McCaskill Street • eisco , N.C. 27209
Office (910) 428-1414
January 29, 2002
American Water Services Inc.
P.O. Box 813
Pinebluhi NC. 28373
910 281-3146
910 281-2047 fax
Reference: Wiring to Sampler @ Effluent
Moore County Waste Water Treatment Plant
Attention: James Frye
Auer testing the wiring, to the Plant Effluent Sampler it is my recommendation that this
circuit be replaced. Circuit is defective and must be replaced to resolve current condition.
This will be repair by February 15, 2002
Thank You,
David McCollum
President
C:1My Documents\moorewwtpeffiuentsump1er.doe