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HomeMy WebLinkAbout20200967 Ver 2_Drainage_Report_20201113 Hydraulic Calculations FOR Davis Park East- Pod B DURHAM, NORTH CAROLINA SUBMITTAL JULY 14, 2020 REVISED NOVEMBER 6, 2020 Kimley>>)Horn 300 Morris St., Suite 200 Durham, NC 27701 NC LICENSE # F-0102 Storm Water System Design The storm water systems are designed to meet North Carolina Department of Transportation(NCDOT) hydraulic design standards. The inlet spacing is based on limiting the spread at each inlet to 6' encroachment into the travel lane during 4 in/hr. The pipes were sized based on the 10-year event. We have included the storm drain profile for this project and is attached separately. CREATE DATE: 7/7/2020 INLET COMPUTATION SHEET REV. DATE: I.D. NO.: Davis Park East Pod B PROJ. NO.: 13276001 COUNTY: Durham DESIGNED BY: KLF DESCRIPTION: REVD BY: VWB LOCATION I ROADWAY RUNOFF _ INLET w H o Z Lu 0 w d Ti- J w K wH.J Q ww OHIXEt z z H O O C7 t, LL u_ J reQ 0 > ❑ 4 cog mw w O w H w H M co o . w - uj z O € Q = _ ❑ QO JQ < �o u' u) REMARKS U H co 2z H LL. E > g nN Qw zw wz z _ O , 6Eg , O ' w � a aw � ce ❑ 0 I 0 w co HZ Jco 0 OO oQ O O Z ❑ LL c❑ ¢ Ogf a z2 M. } 2J < w❑ w ixU D.A. C Tc I QD.A. QC Q Q A.+Qc QI(mx) QB 101 0102 L 20+50 62 Lt 374.00 0.033 0.330 0.07 0.30 2.0 4.0 0.1 0.0 0.1 0.9 0.1 0.0 106 0105 L 20+65 33 Rt 370.31 0.033 0.058 0.09 0.80 2.0 4.0 0.3 0.0 0.3 1.3 0.3 0.0 106 0104 L 20+65 5 Rt 372.18 0.033 0.056 0.15 0.88 2.0 4.0 0.5 0.1 0.6 2.4 0.6 0.0 103 106 0103 L 20+45 5 Rt 371.50 0.033 0.061 0.03 0.88 2.0 4.0 0.1 0.0 0.1 1.2 0.1 0.0 110 0109 L 21+85 32 Rt 375.08 0.033 0.034 0.14 0.72 2.0 4.0 0.4 0.0 0.4 1.8 0.4 0.0 105 110 0108 L 21+85 CL 376.25 0.033 0.034 0.22 0.82 2.0 4.0 0.7 0.0 0.7 3.6 0.7 0.1 104 110 0114 L 23+50 32 Rt 380.66 0.034 0.031 0.21 0.72 2.0 4.0 0.6 0.0 0.6 2.2 0.6 0.0 109 110 0107 L 21+85 52 Lt 376.75 0.033 0.330 0.11 0.47 2.0 4.0 0.2 0.0 0.2 1.2 0.2 0.0 110 0113 L 23+50 6 Lt 381.92 0.034 0.031 0.06 0.80 2.0 4.0 0.2 0.1 0.3 2.7 0.3 0.0 108 110 0119 L 25+83 32 Rt 391.31 0.048 0.020 0.05 0.81 2.0 4.0 0.2 0.0 0.2 1.3 0.2 0.0 114 110 0111 L 22+90 49 Lt 381.10 0.033 0.330 0.09 0.58 2.0 4.0 0.2 0.0 0.2 1.3 0.2 0.0 110 0115 L 24+00 6 Lt 383.69 0.039 0.020 0.17 0.79 2.0 4.0 0.5 0.0 0.5 4.3 0.4 0.1 113 Spread as low as possible 110 0120 L 25+83 48 Rt 390.05 0.048 0.330 0.06 0.30 2.0 7.4 0.1 0.0 0.1 110 0121 L 26+36 32 Rt 393.98 0.048 0.017 0.11 0.85 2.0 4.0 0.4 0.0 0.4 1.9 0.4 0.0 119 110 0112 L 23+90 66 Lt 384.25 0.038 0.330 0.38 0.34 2.0 4.0 0.5 0.0 0.5 1.7 0.5 0.0 110 0116 L 25+55 6 Lt 390.35 0.048 0.015 0.00 0.38 2.0 4.0 0.0 0.0 0.0 0.5 0.0 0.0 115 110 0122 L 26+36 5 Lt 394.67 0.048 0.020 0.02 0.90 2.0 4.0 0.1 0.0 0.1 1.8 0.1 0.0 119 110 0117 L 25+55 32 Lt 390.11 0.048 0.015 0.02 0.83 2.0 4.0 0.1 0.0 0.1 1.2 0.1 0.0 115 110 0123 L 27+55 5 Lt 398.80 0.017 0.020 0.03 0.90 2.0 4.0 0.1 0.0 0.1 2.8 0.1 0.0 122 DI in turn lane 110 0118 L 25+78 32 Lt 391.05 0.048 0.020 0.22 0.88 2.0 4.0 0.8 0.0 0.8 3.2 0.7 0.0 117 128 0127 L 30+50 25 Rt 392.63 0.011 0.030 0.00 0.00 0.0 0.1 0.0 0.1 Collar 128 0133 L 30+48 6 Rt 397.18 I 0.011 0.030 0.02 0.81 2.0 4.0 0.1 0.0 0.1 2.1 0.1 0.0 130 Page 1 of 4 Printed 11/3/2020 CREATE DATE: 7/7/2020 INLET COMPUTATION SHEET REV. DATE: I.D. NO.: Davis Park East Pod B PROJ. NO.: 13276001 COUNTY: Durham DESIGNED BY: KLF DESCRIPTION: REVD BY: VWB LOCATION ROADWAY RUNOFF INLET w i- o z w w Ti-- w w SI • w OHIXEt Z Z H O O O t, W LL E -J reQ 0 > ❑ cog DW W O W I W J QLL B Q s QK OQ Qocow � M co o REMARKS� zzwzw .= Ur rx � � aaWcU ~2z I- L E j a ' fn Qw W Z Om Eg Ho wR � Et 0 1 0 w HZJco 0 OO o < O O Z ❑ LL c❑ ¢ Ogf an Z2 M. } z1 u < W❑ W ceU D.A. C Tc I QD.A. QC Q Q+Qc Ql(mx) QB I 128 0125 L 30+45 39 Lt 395.66 0.011 0.030 0.06 0.90 2.0 4.0 0.2 0.0 0.2 1.8 0.2 0.0 129 128 0134 L 30+25 6 Rt 397.43 0.011 0.030 0.11 0.83 2.0 4.0 0.4 0.0 0.4 3.7 0.3 0.0 133 Allowable spread 3.75' 128 0124 L 30+00 43 Lt 396.00 0.011 0.030 0.15 0.90 2.0 4.0 0.5 0.0 0.5 3.2 0.5 0.0 125 128 0126 L 30+42 61 Lt 393.50 0.011 0.330 0.38 0.32 2.0 1.1 0.1 0.0 0.1 207 0206 L 34+44 31 Rt 388.15 0.044 0.006 0.04 0.72 2.0 4.0 0.1 0.0 0.1 1.4 0.1 0.0 218 207 0205 L 34+02 32 Rt 389.70 0.044 0.015 0.05 0.72 2.0 4.0 0.1 0.0 0.1 1.3 0.1 0.0 206 207 0238 L 34+49 5 Lt 388.25 0.044 0.014 0.17 0.81 2.0 4.0 0.6 0.0 0.6 5.4 0.4 0.1 219 S ucture squired a to a on fo c oss pipe connec ty,sp sad depth s<7 incn. 207 0204 L 33+48 32 Rt 391.72 0.034 0.020 0.13 0.72 2.0 4.0 0.4 0.0 0.4 2.0 0.4 0.0 205 207 0208 L 34+56 65 Lt 387.07 0.044 0.006 0.39 0.38 2.0 0.9 0.1 0.0 0.1 207 0203 L 33+48 6 Lt 392.46 0.034 0.001 0.00 0.41 2.0 4.0 0.0 0.0 0.0 2.8 0.0 0.0 238 207 0202 L 32+79 6 Lt 393.93 0.019 0.015 0.00 0.41 2.0 4.0 0.0 0.0 0.0 0.6 0.0 0.0 203 207 0131 L 31+90 6 Rt 395.45 0.011 0.016 0.02 0.74 2.0 4.0 0.1 0.0 0.1 2.9 0.1 0.0 204 207 0201 L 32+79 32 Lt 393.70 0.019 0.015 0.10 0.81 2.0 4.0 0.3 0.0 0.3 2.6 0.3 0.0 238 207 0135 L 31+68 6 Rt 395.69 0.011 0.020 0.05 0.80 2.0 4.0 0.2 0.0 0.2 3.5 0.1 0.0 131 Allowable spread 3.75' 207 0132 L 31+90 32 Lt 394.62 0.011 0.020 0.10 0.88 2.0 4.0 0.3 0.0 0.3 3.0 0.3 0.0 201 207 0130 L 31+05 6 Rt 396.57 0.011 0.030 0.04 0.82 2.0 4.0 0.1 0.0 0.1 2.6 0.1 0.0 135 207 0129 L 31+05 32 Lt 395.21 0.011 0.030 0.08 0.89 2.0 4.0 0.3 0.0 0.3 1.9 0.3 0.0 132 214 0213 L 36+80 30 Rt 382.05 0.005 0.016 0.00 0.50 2.0 4.0 0.0 0.0 0.0 0.5 0.0 0.0 240 214 0212 L 36+80 5 Rt 381.76 0.005 0.016 0.01 0.76 2.0 4.0 0.0 0.0 0.0 2.9 0.0 0.0 240 214 0224 L 38+18 30 Rt 382.42 0.022 0.015 0.07 0.68 2.0 4.0 0.2 0.0 0.2 1.8 0.2 0.0 240 214 0211 L 36+80 31 Lt 381.94 0.005 0.006 0.04 0.89 2.0 4.0 0.1 0.0 0.1 1.9 0.1 0.0 239 214 0221 L 36+61 4 Rt 381.92 0.009 0.020 0.01 0.75 2.0 4.0 0.0 0.0 0.0 I 2.0 0.0 0.0 212 Page 2 of 4 Printed 11/3/2020 CREATE DATE: 7/7/2020 INLET COMPUTATION SHEET REV. DATE: I.D. NO.: Davis Park East Pod B PROJ. NO.: 13276001 COUNTY: Durham DESIGNED BY: KLF DESCRIPTION: REVD BY: VWB LOCATION ROADWAY RUNOFF INLET W i- o z w a w Ti-- w w g IX Et z z H O O O 15 LL. LL E -J reQ 0 > a w O w DW W O W 1 W J Q a � Q s Q CO Q ❑ U Cn co 0 � CO M co a ❑ � z O w .=_ _ ❑ a r . Q � � REMARKS co U2 z ~ LL. E > g § ' <n Qw zw Luz z O m 0Eg � O rx wR a aw >- Et ❑ 0 I- a 0 W O <n a � � O � O Z cn ¢ O � a HQ } � O FZ J co 0 W w O 0Q D! 8 HU ❑ 2 ❑ U H ❑ s. co - z2 M. COZ u, < ❑ cc 0 D.A. C Tc I QD.A. Qc Q Q+Qc Ql(mx) QB 214 0240 L 37+12 5 Rt 381.66 SAG 0.009 0.11 0.76 2.0 4.0 0.3 0.0 0.3 10.9 N/A N/A Spread as low as possible 214 0233 L 39+00 32 Rt 384.02 0.022 0.020 0.18 0.81 2.0 4.0 0.6 0.0 0.6 3.4 0.6 0.0 224 214 0210 L 36+80 57 Lt 379.20 0.005 0.330 0.08 0.49 2.0 4.0 0.2 0.0 0.2 1.6 0.2 0.0 214 0217 L 36+00 31 Lt 383.17 0.021 0.019 0.08 0.89 2.0 4.0 0.3 0.0 0.3 2.0 0.3 0.0 211 214 0239 L 37+12 31 Lt 381.94 SAG 0.002 0.02 0.89 2.0 4.0 0.1 0.0 0.1 0.9 N/A N/A 214 0220 L 36+61 5 Lt 382.05 0.009 0.029 0.04 0.80 2.0 4.0 0.1 0.1 0.2 3.0 0.2 0.0 215 214 0241 L 36+50 4 Rt 382.04 0.011 0.022 0.06 0.75 2.0 4.0 0.2 0.0 0.2 3.7 0.2 0.0 221 Allowable spread 3.75' 214 0215 L 37+12 5 Lt 381.85 SAG 0.032 0.08 0.86 2.0 4.0 0.3 0.1 0.4 3.2 N/A N/A 214 0234 L 40+65 32 Rt 387.31 0.009 0.020 0.03 0.84 2.0 4.0 0.1 0.0 0.1 1.6 0.1 0.0 233 214 0209 L 36+30 52 Lt 382.45 0.015 0.330 0.20 0.53 2.0 1.3 0.1 0.0 0.1 214 0222 L 37+50 31 Lt 382.11 0.009 0.010 0.00 0.90 2.0 4.0 0.0 0.0 0.0 0.5 0.0 0.0 239 214 0218 L 35+75 5 Rt 383.49 0.026 0.022 0.11 0.80 2.0 4.0 0.3 0.0 0.3 3.7 0.3 0.0 241 Allowable spread 3.75' 214 0216 L 37+50 5 Lt 381.94 0.009 0.010 0.11 0.83 2.0 4.0 0.4 0.0 0.4 8.0 0.3 0.1 215 Spread as low as possible 214 0235 L 41+36 34 Rt 387.80 0.003 0.018 0.03 0.90 2.0 4.0 0.1 0.1 0.2 3.1 0.2 0.0 214 0223 L 37+50 61 Lt 383.49 0.000 0.010 23.44 0.75 15.0 0.0 0.1 0.0 0.1 214 0225 L 38+70 31 Lt 383.62 0.022 0.017 0.12 0.82 2.0 4.0 0.4 0.1 0.5 3.2 0.4 0.0 216 214 0219 L 35+75 5 Lt 383.51 0.026 0.017 0.06 0.83 2.0 4.0 0.2 0.1 0.3 4.4 0.3 0.1 220 214 0236 L 41+76 32 Rt 388.31 0.003 0.020 0.18 0.90 2.0 4.0 0.6 0.0 0.6 6.5 0.6 0.1 235 Exist CB,Turn Lane 214 0226 L 38+70 46 Lt 384.25 0.022 0.330 0.17 0.50 2.0 1.5 0.1 0.0 0.1 214 0227 L 39+95 34 Lt 386.07 0.022 0.020 0.24 0.78 2.0 4.0 0.7 0.0 0.8 4.2 0.7 0.1 225 214 0237 L 41+76 44 Rt 386.17 0.003 0.330 0.10 0.90 2.0 4.0 0.3 0.0 0.3 2.4 0.3 0.0 214 0228 L 41+50 35 Lt 387.59 0.003 0.020 0.14 0.82 2.0 4.0 0.5 0.0 0.5 5.5 0.4 0.0 227 Page 3 of 4 Printed 11/3/2020 CREATE DATE: 7/7/2020 INLET COMPUTATION SHEET REV. DATE: I.D. NO.: Davis Park East Pod B PROJ. NO.: 13276001 COUNTY: Durham DESIGNED BY: KLF DESCRIPTION: REVD BY: VWB LOCATION ROADWAY RUNOFF INLET w H z o z Lu d w d ^c J w K wH.J Lz� r . - ww OHIYEt z z H O O 0 t u_ u_ € J CE 0 > ❑ 1 )g DLu w O ww � M u a wr uj - Q LL O Q QQ❑ aO J Q Q U U U") REMARKS U _ > n Qw zw wZ _ _ 6 � = ° - a awco 2z 1- LL >- ce ❑ 0 0 w 0) 1 z Jco 0 OO 0Q O O Z ❑ L c ¢ O2f an zQ co. f ZJ < w❑ w ceU D.A. C Tc I Q .A. QC Q Q+QC Ql(mx) QB r 1 i I i 214 0229 L 42+75 35 Lt 387.97 0.003 0.020 0.07 0.89 2.0 4.0 0.2 0.0 0.3 3.9 0.3 0.0 228 214 0230 L 42+75 51 Lt 388.40 0.003 0.330 0.53 0.40 2.0 4.0 0.8 0.0 0.8 3.3 0.8 0.0 214 0231 L 43+48 35 Lt 388.26 0.003 0.020 0.05 0.83 2.0 4.0 0.2 0.0 0.2 4.6 0.2 0.0 229 214 0232 L 43+99 71 Lt 390.14 0.013 0.020 0.01 0.84 2.0 4.0 0.0 0.4 0.5 3.6 0.4 0.0 231 214 0242 L 44+01 83 Lt 390.26 0.013 0.020 0.48 0.90 2.0 4.0 1.7 0.0 1.7 7.4 1.3 0.4 232 Turn Lane Page 4 of 4 Printed 11/3/2020 CREATE DATE: 7/7/2020 STORM DRAIN DESIGN COMPUTATIONS REV. DATE: I.D. NO.: avis Park East Pod PROJ. NO.: 13276001 COUNTY: Durham DESIGNED BY: KLF DESCRIPTION: REVD BY: VWB LOCATION RUNOFF PIPE DESIGN STRUCTURE = TIME OF fn U W W o ^ J _ J , g x o c( Q CONCENTRATION z = J W W Q Q Z Q Q w z NUMBER o 2 g X z (min) W 0 Z_ w O c _ w z 6 Q ACC w m REMARKS Z z I- '_ co N w O W W C w U 2' J co J 0 co w Z ? oz d Dd Q H ww J H0 W W >- o _. J 9 20 o < 1 Ww w cn J w � v W F- u, TOP, TOP, � z_ ccnn 2 u) a = O FROM TO CA d 0 w I 0 x = W d Z -i a INV INV W w > 00 101 102 0102 0101 0.22 0.09 82 2 2 10 5.8 0.5 374.00 0.00 0.021 15 C 9.0 4.3 3.25 371.13 370.75 369.00 106 105 0105 0106 0.27 0.23 15 2 5 10 5.8 1.3 370.31 0.00 0.004 15 C 4.2 3.3 3.00 367.83 367.31 367.25 106 104 0104 0105 0.18 0.16 25 2 5 10 5.8 0.9 372.18 370.31 0.034 15 C 9.0 5.9 3.95 368.74 368.23 367.31 106 103 0103 0104 0.03 0.02 16 2 2 10 5.8 0.1 371.50 372.18 0.005 15 C 5.0 0.3 3.17 368.74 368.33 368.23 110 109 0109 0110 1.88 1.25 37 2 29 29 3.6 4.4 375.08 0.00 0.123 0.016 15 S 9.0 9.2 3.00 373.24 372.08 367.27 110 108 0108 0109 0.80 0.41 30 2 8 10 5.8 2.4 376.25 375.08 0.036 15 C 9.0 7.8 3.00 373.92 373.25 372.08 110 114 0114 0109 0.94 0.73 157 2 28 28 3.7 2.7 380.66 375.08 0.035 15 C 9.0 8.4 3.00 378.53 377.66 372.08 110 107 0107 0108 0.58 0.23 49 2 7 10 5.8 1.3 376.75 376.25 0.025 15 C 9.0 6.0 2.25 375.10 374.50 373.25 110 113 0113 0114 0.47 0.39 36 2 6 10 5.8 2.3 381.92 380.66 0.033 15 C 9.0 7.5 3.00 379.70 378.92 377.66 110 119 0119 0114 0.27 0.19 229 2 22 22 4.2 0.8 391.31 380.66 0.046 15 C 9.0 6.5 3.00 388.74 388.31 377.66 110 111 0111 0107 0.48 0.18 106 2 5 10 5.8 1.1 381.10 376.75 0.040 15 C 9.0 6.7 2.25 379.29 378.85 374.50 110 115 0115 0113 0.41 0.34 47 2 5 10 5.8 2.0 383.69 381.92 0.035 15 C 9.0 7.6 3.00 381.29 380.69 378.92 110 120 0120 0119 0.06 0.02 15 2 2 10 5.8 0.1 390.05 391.31 0.029 15 C 9.0 3.0 1.25 388.98 388.80 388.31 110 121 0121 0119 0.16 0.13 50 2 20 20 4.4 0.6 393.98 391.31 0.050 15 C 9.0 6.1 3.00 391.38 390.98 388.31 110 112 0112 0111 0.38 0.13 104 2 2 10 5.8 0.7 384.25 381.10 0.007 15 C 5.7 3.2 4.70 380.01 379.55 378.85 110 116 0116 0115 0.24 0.21 152 2 3 10 5.8 1.2 390.35 383.69 0.041 15 C 9.0 7.1 3.37 387.53 386.98 380.69 Page 1 of 5 Printed 11/3/2020 CREATE DATE: 7/7/2020 STORM DRAIN DESIGN COMPUTATIONS REV. DATE: I.D. NO.: avis Park East Pod PROJ. NO.: 13276001 COUNTY: Durham DESIGNED BY: KLF DESCRIPTION: REVD BY: VWB LOCATION RUNOFF PIPE DESIGN STRUCTURE = TIME OF fn U W W o ^ J _1 J g x o c( Q CONCENTRATION Z = J W W Q Q Z Q Q w NUMBER o 2 g X z (min) w t 0 Z_ Ej 6 d w z ° Q w w m REMARKS z z HL co y W Ow W 2w U w J 0 ln0 w Z ? 5g d Da Q H W W J I- I W W >- D _. J O g0 ° Q � Wr cn J w o w F- C TOP, TOP, � z_ ccnn 2 u) a = O c7 CC FROM TO CA a O w I Q X = a I z o INV INV W w > 00 110 122 0122 0121 0.05 0.04 34 2 17 17 4.7 0.2 394.67 393.98 0.014 15 C 8.4 2.9 3.17 391.72 391.50 390.98 110 117 0117 0116 0.24 0.21 22 2 2 10 5.8 1.2 390.11 390.35 0.005 15 C 5.2 3.4 3.00 387.67 387.11 386.98 110 123 0123 0122 0.03 0.03 116 2 2 10 5.8 0.2 398.80 394.67 0.035 15 C 9.0 3.7 3.17 395.84 395.63 391.50 110 118 ®®® 0.20 20 Una) ®® 391.05 ® :: 387.117 0 .®O.® 6.6 ', ®I 128 127 0127 0128 0.72 0.42 28 4 10 5.8 2.4 392.63 0.00 0.011 18 C 11.9 5.1 1.50 391.72 391.13 390.83 397.18 392.63 128 133 0133 0127 0.72 0.42 18 2 4 10 5.8 2.4 391.31 391.13 0.010 18 C E 11.1 4.8 5.87 392.03 128 125 0125 0133 0.60 0.31 42 2 3 10 5.8 1.8 395.66 397.18 0.012 18 C E 12.5 5.0 3.82 392.51 391.84 391.31 128 134 0134 0133 0.11 0.09 20 2 2 10 5.8 0.5 397.43 397.18 0.011 15 C 7.3 3.4 3.17 394.64 394.26 394.01 128 124 0124 0125 0.15 0.14 40 2 2 10 5.8 0.8 396.00 395.66 0.011 15 C 7.4 3.9 3.00 393.47 393.00 392.52 128 126 0126 0125 0.38 0.12 22 2 2 10 5.8 0.7 393.50 395.66 0.007 18 C 9.4 0.9 1.50 392.54 392.00 391.84 _ 207 206 0206 0207 • 1.16 0.76 9 2 16 16 4.8 3.7 388.15 0.00 0.007 15 C 6.0 5.0 3.07 386.13 385.08 385.00 207 205 0205 0206 0.56 0.45 39 2 15 15 4.9 2.2 389.70 388.15 0.037 15 C 9.0 7.8 2.99 387.31 386.71 385.15 207 238 0238 0206 0.57 0.29 34 2 3 10 5.8 1.7 388.25 388.15 0.005 15 C E 4.7 1.5 3.00 386.16 385.25 385.08 207 204 0204 0205 0.51 0.41 51 2 15 15 4.9 2.0 391.72 389.70 0.037 15 C 9.0 7.8 3.00 389.46 388.72 386.71 207 208 0208 0238 0.39 0.15 59 2 I 2 10 5.8 0.9 387.07 388.25 0.005 15 C E 5.1 0.9 1.50 386.19 385.57 385.25 207 203 0203 0204 10.38 0.32 36 2 14 14 5.2 1.6 392.46 391.72 0.019 15 C 9.0 5.8 3.00 390.10 389.46 388.72 Page 2 of 5 Printed 11/3/2020 CREATE DATE: 7/7/2020 STORM DRAIN DESIGN COMPUTATIONS REV. DATE: I.D. NO.: avis Park East Pod PROJ. NO.: 13276001 COUNTY: Durham DESIGNED BY: KLF DESCRIPTION: REVD BY: VWB LOCATION RUNOFF PIPE DESIGN STRUCTURE = TIME OF fn U W W b ^ J � J g � o c( Q CONCENTRATION Z = J W W WW Q < Z QI Q w NUMBER o g X (min) W 0 Z_ _, - w z ¢ w w m REMARKS H Z z I- t w W O w W 2 W U J co J 0 coo w Z ? 5g a Da Q H ww J I- 0 W W >- DS J O g0 0 Q I- Wa W (n J W co 0 W F- U) TOP, TOP, � z_ ccnn 2 u) � a = O0 CC FROM TO CA a n O w I Q X = W d z a INV INV W w > 00 207 202 0202 0203 0.38 0.32 66 2 14 14 5.2 1.6 393.93 392.46 0.016 15 C 8.8 5.5 3.37 391.22 390.56 389.46 207 131 0131 0202 0.11 0.09 87 2 10 10 5.8 0.5 395.45 393.93 0.017 15 C 9.0 4.0 3.00 392.74 392.45 390.93 207 201 0201 0202 0.27' 0.23 22 2 8 10 5.8 1.3 393.70 393.93 0.006 15 C 5.3 2.0 3.00 391.31 390.70 390.56 207 135 0135 0131 0.09 0.07 22 2 9 10 5.8 0.4 395.69 395.45 0.009 15 C 6.8 3.1 3.00 392.96 392.69 392.45 207 132 0132 0201 0.17 0.15 86 2 6 10 5.8 0.9 394.62 393.70 0.010 15 C 7.1 3.9 3.00 392.02 391.62 390.70 207 130 0130 0135 0.04 0.03 60 2 2 10 5.8 0.2 396.57 395.69 0.011 15 C 7.4 2.6 3.17 393.63 393.40 392.69 207 129 0129 0132 0.08 0.07 81 2 2 10 5.8 0.4 395.21 394.62 0.007 15 C 5.9 2.7 3.00 392.54 392.21 391.62 214 213 0213 0214 26.87 20.00 23 2 15 15 4.9 97.3 382.05 0.00 0.017 0.004 48 C 120.0 11.9 7.49 377.65 374.56 374.15 214 212 0212 0213 26.28 19.50 22 2 15 15 4.9 95.0 381.76 382.05 0.014 0.004 48 C 120.0 11.5 6.86 377.95 374.90 374.56 214 224 0224 0213 0.59 0.50 138 2 7 10 5.8 2.9 382.42 382.05 0.005 15 C 4.9 4.2 3.00 380.13 379.42 378.73 214 211 0211 0212 25.68 19.02 33 2 15 15 4.9 92.8 381.94 381.76 0.013 0.004 48 C 120.0 11.6 6.59 379.25 375.35 374.90 214 221 0221 0212 0.29 0.23 16 2 5 10 5.8 1.3 381.92 381.76 0.008 15 C 6.4 4.0 3.00 379.45 378.92 378.76 214 240 0240 0212 0.31 0.25 29 2 4 10 5.8 1.4 381.66 381.76 0.005 15 C 4.9 3.5 2.95 379.34 378.71 378.55 214 233 0233 0224 0.52 0.45 79 2 6 10 5.8 2.6 384.02 382.42 0.020 15 C 9.0 6.7 3.00 381.71 381.02 379.42 214 210 0210 0211 0.28 0.15 25 2 4 10 5.8 0.8 379.20 381.94 0.000 15 C 1.3 0.7 2.25 379.26 X 15"OEP 376.95 376.94 214 217 0217 0211 0.08 0.07 76 2 2 10 5.8 0.4 383.17 381.94 0.016 15 C 8.7 3.7 3.00 380.52 380.17 378.94 Page 3 of 5 Printed 11/3/2020 CREATE DATE: 7/7/2020 STORM DRAIN DESIGN COMPUTATIONS REV. DATE: I.D. NO.: avis Park East Pod PROJ. NO.: 13276001 COUNTY: Durham DESIGNED BY: KLF DESCRIPTION: REVD BY: VWB LOCATION RUNOFF PIPE DESIGN STRUCTURE = TIME OF fn U W W O ^ J _ J , g � x o c( Q CONCENTRATION z i J W W Q Q Z QI Q w z NUMBER o 2 g X z (min) W co -0 z_ LU 0 c _ w z 6 Q ACC w m REMARKS Z z ~ L N w O W W C w U a' J co J 0 coo w Z ? 5g a Da Q H ww J H0 W W D �. J 9 gO ° Q I- Wa W (n J w v w F- u) TOP, TOP, � z_ ccnn 2 u) Cl) a = O C7 CC FROM TO CA a 0 w I Q x I w d z ❑ INV INV W w > 00 214 239 0239 0211 25.27 18.76 29 2 15 15 4.9 91.8 381.94 381.94 0.014 0.003 48 C 120.0 7.4 6.13 379.15 375.81 375.35 214 220 0220 0221 0.04 0.04 8 2 2 10 5.8 0.2 382.05 381.92 0.012 15 C 7.6 0.4 3.00 379.45 379.05 378.92 214 241 0241 0221 0.23 0.19 8 2 5 10 5.8 1.1 382.04 381.92 0.009 15 C 6.8 3.9 3.02 379.45 379.02 378.92 214 215 0215 0240 0.19 0.16 8 2 3 10 5.8 0.9 381.85 381.66 0.004 15 C 4.2 1.5 3.10 379.38 378.75 378.71 214 234 0234 0233 0.34 0.30 162 2 4 10 5.8 1.8 387.31 384.02 0.014 15 C 8.2 5.3 4.05 383.81 383.26 381.02 214 209 0209 0210 0.20 0.10 48 2 2 10 5.8 0.6 382.45 379.20 0.086 15 C 9.0 7.4 1.25 381.61 381.20 376.95 214 222 0222 0239 25.25 18.74 35 2 15 15 4.9 91.7 382.11 381.94 0.014 0.003 48 C 120.0 11.9 5.75 380.25 376.36 375.81 214 218 0218 0241 0.17 0.14 72 2 3 10 5.8 0.8 383.49 382.04 0.020 15 C 9.0 4.8 2.98 380.98 380.51 379.02 214 216 0216 0215 0.11 0.10 35 2 2 10 5.8 0.6 381.94 381.85 0.005 15 C 4.9 0.9 3.00 379.41 378.94 378.75 214 235 0235 0234 0.31 0.28 68 2 3 10 5.8 1.6 387.80 387.31 0.006 15 C E 5.6 3.9 4.09 384.23 383.71 383.26 214 223 0223 0222 23.44 17.50 30 15 15 15 4.9 85.8 383.49 382.11 0.033 0.003 48 C 120.0 13.5 6.08 381.97 377.41 376.36 214 225 0225 0222 1.81 1.24 117 2 5 10 5.8 7.2 383.62 382.11 0.013 0.010 15 C 7.8 7.2 3.00 381.94 380.62 379.11 214 219 0219 0218 0.06 0.05 8 2 2 10 5.8 0.3 383.51 383.49 0.004 15 C 4.2 0.7 2.96 380.99 380.55 380.51 214 236 0236 0235 0.28 0.25 37 2 3 10 5.8 1.4 388.31 387.80 0.009 15 C E 6.8 4.4 4.10 384.85 384.21 383.83 214 226 0226 0225 0.17 0.09 14 2 I 2 10 5.8 0.5 384.25 383.62 0.149 15 S 9.0 5.2 1.25 383.39 383.00 380.62 214 227 0227 0225 1.52 1.05 122 2 4 10 5.8 6.1 386.07 383.62 0.020 0.008 15 C 9.0 8.4 3.00 384.12 383.07 380.62 Page 4 of 5 Printed 11/3/2020 CREATE DATE: 7/7/2020 STORM DRAIN DESIGN COMPUTATIONS REV. DATE: I.D. NO.: avis Park East Pod PROJ. NO.: 13276001 COUNTY: Durham DESIGNED BY: KLF DESCRIPTION: REVD BY: VWB LOCATION RUNOFF PIPE DESIGN STRUCTURE = TIME OF U W W b ^ J _1 J - g � x o c( ^ <r I CONCENTRATION Cl)Z i W W W WW Q Q Z Q Q W Y NUMBER o g X cp (min) w U Z_ 8 d w z ° < - w w o REMARKS z o z I- L � N w OW W � w U w J lnU w Z ? og d Dd Q H W w J I- I W W co>- Dom. J O go o Q I- Wr W (n J W � v W F u, TOP, TOP, � z_ ccnn 2 co a O C7 cc FROM TO CA d J 0 w I Q xI W d Z a INV INV W J CO> 00 214 237 0237 0236 0.10 0.09 10 2 2 10 5.8 0.5 386.17 388.31 0.020 15 C E ' 9.0 4.1 1.45 385.09 384.72 384.46 214 228 0228 0227 1.28 0.87 152 2 4 10 5.8 5.0 387.59 386.07 0.008 0.005 15 C 6.3 5.7 3.25 385.29 384.34 383.07 214 229 0229 0228 1.14 0.75 123 2 3 10 5.8 4.4 387.97 387.59 0.005 0.004 15 C 5.0 4.4 3.00 386.12 384.97 384.34 214 230 0230 0229 0.53 0.21 14 2 2 10 5.8 1.2 388.40 387.97 0.069 15 C 9.0 7.8 2.25 386.75 386.15 384.97 214 231 0231 0229 0.54 0.48 70 2 3 10 5.8 2.8 388.26 387.97 0.004 15 C 4.4 2.4 3.00 386.25 385.26 384.97 214 232 0232 0231 0.49 0.44 62 2 2 10 5.8 2.6 390.14 388.26 0.029 15 C 9.0 7.6 2.99 387.92 387.15 385.26 214 242 0242 0232 0.48 0.43 9 2 2 10 5.8 2.5 390.26 390.14 0.009 15 C 6.6 4.8 3.00 388.20 387.26 387.15 Page 5 of 5 Printed 11/3/2020 Ditch Calculations We have evaluated the proposed discharge points in both the pre and post construction scenarios to determine the increase, if any, in flow rate offsite. In addition, the outfall ditches were designed to contain the 10-year event within their respective banks. Temporary and permanent ditch linings have been designed to meet North Carolina Department of Transportation design standards. Date: 4/15/2020 Kimley-Horn & Associates, Inc. Raleigh, NC Project Number: 12329063 Designed By: DLH County: WAKE Checked By: Ditch Computation Sheet Description: Holly Springs Road Ph2 Ditch Location D.A. C Q10 Slope Base Side Depth Velocity Remarks Liner Type From To L/M/R (acres) (cfs) (ft/ft) Width Slopes (ft) (fps) 20+50-L- 21+85-L- LT 0.07 0.30 0.12 0.020 0 4:1/3:1 0.17 1.14 21+85-L- 22+60-L- LT 0.11 0.47 0.29 0.043 0 4:1/3:1 0.21 1.91 35+80-L- 36+30-L- LT 0.20 0.53 0.61 0.030 2 4:1/3:1 0.21 1.06 38+70-L- 39+75-L- LT 0.17 0.50 0.50 0.019 0 4:1/3:1 0.30 1.60 Page 1 of 1 Cross Pipe Data Sheet The following pipe data sheet shows the calculations for the proposed pipe from structure 223 to structure 214. PIPE DATA SHEET Date 07/09/200 Sheet 1 of 1 Project No. 013276001 I.D. No. Davis Park East County Durham Designed By KLF Checked By Shoulder CL Elev. 382.06 PLAN SUMMARY DATA Elev 383.06 Drainage Area 23.44 ac Design Freq. 25 yr Station 36+80 Design Disch. 95.00 cfs Skew 90.0 ° A A H Design H.W. Elev. 381.96 ft v Size/Type Pipe 48" H.W. A T.W. Q100 Disch. 107.00 cfs Type Entrance Grooved End w/HW LSo v Q100 H.W. Elev. 382.43 ft Direction of Flow Lt to Rt T Overtopping Freq. >100yr yr Hydrological Method Rational Inv. Elev. 377.41 So = 1.71 % Inv. Elev. 374.15 Overtopping Disch. 113.80 cfs HW Control Elev 382.87 L = 190.40 S Overtopping Elev. 382.73 ft INLET CONTROL OUTLET CONTROL Size &Type Pipe Freq Q Nat. Allow. T.W. HW/D H.W. Ke do dc+d ho H LSo H.W. H.W. Vo COMMENTS (Yrs.) (cfs) H.W H.W. 2 Elev. (ft/s) 48" RCP 10 86.00 2.48 1.06 4.22 0.2 2.85 3.42 3.42 1.45 3.26 1.00 381.63 14.59 Inlet Control 48" RCP 25 95.00 2.67 1.14 4.55 0.2 3.02 3.51 3.51 1.77 3.26 1.47 381.96 14.92 Inlet Control 48" RCP 50 100.00 2.77 1.19 4.74 0.2 3.11 3.56 3.56 1.96 3.26 2.22 382.15 15.11 Inlet Control 48" RCP 100 107.00 2.92 1.26 5.02 0.2 3.24 3.62 3.62 2.25 3.26 2.55 382.43 15.46 Inlet Control SUMMARY AND RECOMMENDATIONS : Proposed 48"RCP with HW at entrance.Average slope from HW to outlet used for analysis. Water will breach shoulder at 37+00-L-LT=382.87'. This yields 0.91'of freeboard during the 25 yr storm. Outfall Analysis The following Post Construction Discharge Q 10 Outfall Channel Analysis sheet shows the pre and post outfall calculations. Kimley>>>Horn 2 Year Analysis Pre-vs Post-Construction Discharges Project Information Project Name:Davis Park East Pod B KHA Project#: 013276001 Designed by: KLF Date: 7/13/2020 Checked by: Date: Revised by: Date: EXISTING CONDITIONS I I PROPOSED CONDITIONS DRAINAGE RUNOFF Time of Storm Q DRAINAGE RUNOFF Time of Storm Q DISCHARGE DISCHARGE AREA COEFF. Concentration Intensity TOTAL AREA COEFF. Concentration Intensity TOTAL DIFF. INCREASE Station/Structure# A(acres) C Tc(min) I(in/hr) Clio(cfs) Station/Structure# A(acres) C Tc(min) I(in/hr) Qio(cfs) (CFS) VA) 19+71-L-LT/0101 0.38 0.41 10.00 4.50 0.70 19+71-L-LT/0101 0.22 0.41 10.00 4.50 0.40 -0.30 -42.73 20+68-L-RT/0106 0.09 0.90 10.00 4.50 0.37 20+68-L-RT/0106 0.27 0.86 10.00 4.50 1.02 0.65 175.17 21+65-L-RT/0110 3.93 0.51 10.00 4.50 8.98 21+65-L-RT/0110 3.95 0.51 10.00 4.50 9.05 0.08 0.87 30+53-L-RT/0128 0.55 0.57 10.00 4.50 1.40 30+53-L-RT/0128 0.73 0.88 10.00 4.50 2.88 1.48 105.89 34+42-L-RT/0207 0.76 0.53 10.00 4.50 1.80 34+42-L-RT/0207 _ 1.16 0.90 10.00 4.50 4.71 2.90 160.92 36+80-L-RT/0214 25.70 0.73 15.00 3.80 71.00 36+80-L-RT/0214 26.80 0.74 15.00 3.80 75.75 4.75 6.69 Page 1 of 6 Kimley>>>Horn Post-Construction Discharge Q2 Outfall Channel Analysis Project Information Project Name:Davis Park East Pod B KHA Project#: 013276001 Designed by: KLF Date: 7/13/2020 Checked by: VWB Date: 7/14/2020 Revised by: Date: Outlet T DA C Tc i2 Q2 s Fore Slope Backslope Base Width Ditch Existing Design Depth y V Manning's (ac) Value (min) (in/hr) (cfs) (ft/ft) (ft) Type Depth(ft) of Ditch(ft.) (ft) (fps) n 19+71-L-LT/0101 0.38 0.41 10.00 4.50 0.70 0.025 3:1 3:1 3.00 Base 2.0000 Leave as is 0.13 1.59 0.035 Pre 20+88-L-RT/0106 0.09 0.90 10.00 4.50 0.37 0.200 20:1 20:1 0.00 Triangular N/A Leave as is 0.09 2.37 0.035 Downstream 21+65-L-RT/0110 3.93 0.51 10.00 4.50 8.98 0.060 20:1 20:1 0.00 Triangular N/A Leave as is 0.37 3.35 0.035 Outfalls 30+53-L-RT/0128 0.55 0.57 10.00 4.50 1.40 0.010 10:1 10:1 0.00 Triangular N/A Leave as is 0.33 1.28 0.035 34+42-L-RT/0207 0.76 0.53 10.00 4.50 1.80 0.025 3:1 3:1 5.00 Base 2.0000 Leave as is 0.17 1.93 0.035 36+80-L-RT/0214 25.70 0.73 15.00 3.80 71.00 0.010 1:1 1:1 5.00 Base 5.0000 Leave as is. 2.89 3.11 0.069 Outlet DA C Tc i2 Q2 s Fore Slope Backslope Base Width Ditch Existing Design Depth y v Manning's lac) Value (min) (in/hr) (cfs) (ft/ft) (ft) Type Depth(ft) of Ditch(ft.) (ft) (fps) n 19+71-L-LT/0101 0.22 0.41 10.00 4.50 0.40 0.025 3:1 3:1 3.00 Base 2.0000 Leave as is 0.14 0.84 0.069 Post 20+68-L-RT/0106 0.27 0.86 10.00 4.50 1.02 0.200 20:1 20:1 0.00 Triangular N/A Leave as is 0.17 1.83 0.069 Downstream 21+65-L-RT/0110 3.95 0.51 10.00 4.50 9.05 0.060 20:1 20:1 0.00 Triangular N/A Leave as is 0.47 2.02 0.069 Outfalls 30+53-L-RT/0128 _ 0.73 _ 0.88 10.00 4.50 _ 2.88 0.010 10:1 10:1 0.00 _ Triangular _ N/A _ Leave as is _ 0.56 _ 0.92 _ 0.035 34+42-L-RT/0207 1.16 0.90 10.00 4.50 4.71 0.025 3:1 3:1 5.00 Base 2.0000 Leave as is 0.44 1.71 0.069 36+80-L-RT/0214 26.80 0.74 15.00 3.80 75.75 0.010 1:1 1:1 5.00 Base 5.0000 Leave as is 3.07 3.06 0.072 Downstream Outlet Depth Velocity Outfalls Change(ft) Change(fps) 19+71-L-LT/0101 0.01 -0.75 20+68-L-RT/0106 0.08 -0.54 30+53-L-RT/0128 0.23 -0.36 34+42-L-RT/0207 0.27 -0.22 36+80-L-RT/0214 0.18 -0.05 Page 2 of 6 Kimley>>>Horn 5 Year Analysis Pre-vs Post-Construction Discharges Project Information Project Name:Davis Park East Pod B KHA Project#: 013276001 Designed by: KLF Date: 7/13/2020 Checked by: VWB _ Date: 7/14/2020 Revised by: Date: EXISTING CONDITIONS I I PROPOSED CONDITIONS DRAINAGE RUNOFF Time of Storm Q DRAINAGE RUNOFF Time of Storm Q DISCHARGE DISCHARGE AREA COEFF. Concentration Intensity TOTAL AREA COEFF. Concentration Intensity TOTAL DIFF. INCREASE Station/Structure# A(acres) C Tc(min) I(in/hr) Clio(cfs) Station/Structure# A(acres) C Tc(min) I(in/hr) Qio(cfs) (CFS) (%) 19+71-L-LT/0101 0.38 0.41 10.00 5.20 0.80 19+71-L-LT/0101 0.22 0.41 10.00 5.20 0.46 -0.34 -42.73 20+68-L-RT/0106 0.09 0.90 10.00 5.20 0.43 20+68-L-RT/0106 0.27 0.86 10.00 5.20 1.18 0.75 175.17 21+65-L-RT/0110 3.93 0.51 10.00 5.20 10.37 21+65-L-RT/0110 3.95 0.51 10.00 5.20 10.46 0.09 0.87 30+53-L-RT/0128 0.55 0.57 10.00 5.20 1.62 30+53-L-RT/0128 0.73 0.88 10.00 5.20 3.33 1.71 105.89 34+42-L-RT/0207 0.76 0.53 10.00 5.20 2.08 34+42-L-RT/0207 _ 1.16 0.90 10.00 5.20 5.44 3.35 160.92 36+80-L-RT/0214 25.70 0.73 15.00 4.40 82.22 36+80-L-RT/0214 26.80 0.74 15.00 4.40 87.72 5.50 6.69 Page 3 of 6 Kimley>>>Horn Post-Construction Discharge Q5 Outfall Channel Analysis Project Information Project Name:Davis Park East Pod B KHA Project#: 013276001 Designed by: KLF Date: 7/13/2020 Checked by: VWB Date: 7/14/2020 Revised by: Date: Outlet T DA C Tc i5 Q5 s Fore Slope Backslope Base Width Ditch Existing Design Depth y V Manning's r (ac) Value (min) (in/hr) (cfs) (ft/ft) (ft) Type Depth(ft) of Ditch(ft.) (ft) (fps) n 19+71-L-LT/0101 0.38 0.41 10.00 5.20 0.80 0.025 3:1 3:1 3.00 Base 2.0000 Leave as is 0.14 1.67 0.035 Pre 20+68-L-RT/0106 0.09 0.90 10.00 _ 5.20 0.43 0.200 20:1 20:1 _ 0.00 Triangular N/A Leave as is 0.09 2.47 0.035 Downstream 21+65-L-RT/0110 3.93 0.51 10.00 5.20 10.37 0.060 20:1 20:1 0.00 Triangular N/A Leave as is 0.39 3.47 0.035 • • Outfalls 30+53-L-RT/0128 0.55 0.57 10.00 5.20 1.62 0.010 10:1 10:1 0.00 _ Triangular N/A Leave as is 0.35 1.32 0.035 34+42-L-RT/0207 0.76 0.53 10.00 5.20 2.08 0.025 3:1 3:1 5.00 Base 2.0000 Leave as is _ 0.18 _ 2.03 0.035 36+80-L-RT/0214 25.70 0.73 15.00 4.40 82.22 0.010 1:1 1:1 5.00 Base 5.0000 Leave as is 3.13 3.23 0.069 DA C Tc i5 Q5 s Fore Slope Backslope Base Width Ditch Existing Design Depth y V Manning's (ac) Value (min) (in/hr) (cfs) (ft/ft) (ft) Type Depth(ft) of Ditch(ft.) (ft) (fps) n 19+71-L-LT/0101 0.22 0.41 10.00 5.20 0.46 0.025 3:1 3:1 3.00 Base 2.0000 Leave as is 0.15 0.88 0.069 Post 20+68-L-RT/0106 0.27 0.86 10.00 5.20 1.18 0.200 20:1 20:1 0.00 Triangular N/A Leave as is. 0.18 1.90 0.069 Downstream 21+65-L-RT/0110 3.95 0.51 10.00 5.20 10.46 0.060 20:1 20:1 0.00 Triangular N/A Leave as is _ 0.50 2.09 0.069 Outfalls 30+53-L-RT/0128 0.73 0.88 10.00 5.20 3.33 0.010 10:1 10:1 0.00 Triangular N/A Leave as is 0.59 0.95 0.069 34+42-L-RT/0207 1.16 0.90 10.00 5.20 5.44 0.025 3:1 3:1 5.00 Base 2.0000 Leave as is _ 0.47 1.79 0.069 36+80-L-RT/0214 26.80 0.74 15.00 4.40 87.72 0.010 1:1 1:1 5.00 Base 5.0000 Leave as is 3.31 3.18 0.072 Downstream Outlet Depth Velocity Outfalls Change(ft) Change(fps) 19+71-L-LT/0101 0.01 -0.79 20+68-L-RT/0106 0.09 -0.57 30+53-L-RT/0128 0.24 -0.37 34+42-L-RT/0207 0.29 -0.24 36+80-L-RT/0214 0.18 -0.05 Page 4 of 6 Kimley>>>Horn 10 Year Analysis Pre-vs Post-Construction Discharges Project Information Project Name:Davis Park East Pod B KHA Project#: 013276001 Designed by: KLF Date: 7/13/2020 Checked by: VWB Date: 7/14/2020 Revised by: Date: EXISTING CONDITIONS I I PROPOSED CONDITIONS DRAINAGE RUNOFF Time of Storm Q DRAINAGE RUNOFF Time of Storm Q DISCHARGE DISCHARGE AREA COEFF. Concentration Intensity TOTAL AREA COEFF. Concentration Intensity TOTAL DIFF. INCREASE Station/Structure# A(acres) C Tc(min) I(in/hr) Clio(cfs) Station/Structure# A(acres) C Tc(min) I(in/hr) Qio(cfs) (CFS) (%) 19+71-L-LT/0101 0.38 0.41 10.00 5.80 0.90 19+71-L-LT/0101 0.22 0.41 10.00 5.80 0.51 -0.38 -42.73 20+68-L-RT/0106 0.09 0.90 10.00 5.80 0.48 20+68-L-RT/0106 0.27 0.86 10.00 5.80 1.31 0.84 175.17 21+65-L-RT/0110 3.93 0.51 10.00 5.80 11.57 21+65-L-RT/0110 3.95 0.51 10.00 5.80 11.67 0.10 0.87 30+53-L-RT/0128 0.55 0.57 10.00 5.80 1.81 30+53-L-RT/0128 0.73 0.88 10.00 5.80 3.72 _ 1.91 105.89 34+42-L-RT/0207 0.76 0.53 10.00 5.80 2.32 34+42-L-RT/0207 _ 1.16 0.90 10.00 5.80 6.07 3.74 _ 160.92 36+80-L-RT/0214 25.70 0.73 15.00 4.90 91.56 36+80-L-RT/0214 26.80 0.74 15.00 4.90 97.68 6.13 6.69 Page 5of6 Kimley>>>Horn Post-Construction Discharge Clio Outfall Channel Analysis Project Information Project Name:Davis Park East Pod B KHA Project#: 013276001 Designed by: KLF Date: 7/13/2020 Checked by: VWB Date: 7/14/2020 Revised by: Date: Outlet DA C Tc in, 410 s Fore Slope Backslope Base Width Ditch Existing Design Depth y V Manning's (ac) Value (min) (in/hr) (cfs) (ft/ft) (ft) Type Depth(ft) of Ditch(ft.) (ft) (fps) n 19+71-L-LT/0101 0.38 0.41 10.00 5.80 0.90 _ 0.025 3:1 3:1 3.00 Base 2.0000 Leave as is 0.15 1.73 0.035 Pre 20+68-L-RT/0106 0.09 0.90 10.00 5.80 0.48 0.200 20:1 20:1 0.00 Triangular N/A Leave as is 0.10 2.53 0.035 Downstream 21+65-L-RT/0110 3.93 0.51 10.00 5.80 11.57 0.060 20:1 20:1 0.00 Triangular N/A Leave as is 0.40 3.57 0.035 Outfalls 30+53-L-RT/0128 0.55 0.57 10.00 5.80 1.81 0.010 10:1 10:1 0.00. Triangular N/A Leave as is 0.36 1.36 0.035 34+42-L-RT/0207 0.76 0.53 10.00 _ 5.80 2.32 0.025 3:1 3:1 5.00 Base 2.0000 Leave as is 0.20 2.11 0.035 36+80-L-RT/0214 25.70 0.73 15.00 4.90 91.56 0.010 1:1 1:1 5.00 Base 5.0000 Leave as is 3.31 3.32 0.069 Outlet DA C Tc 110 410 s Fore Slope Backslope Base Width Ditch Existing Design Depth y V Manning's (ac) Value (min) (in/hr) (cfs) (ft/ft) (ft) Type Depth(ft) of Ditch(ft.) (ft) (fps) n 19+71-L-LT/0101 0.22 0.41 10.00 5.80 0.51 0.025 3:1 3:1 3.00 Base 2.0000 Leave as is 0.16 0.91 0.069 Post 20+68-L-RT/0106 0.27 0.86 10.00 5.80 1.31 0.200 20:1 20:1 0.00 Triangular N/A Leave as is 0.18 1.96 0.069 Downstream 21+65-L-RT/0110 3.95 0.51 10.00 5.80 11.67 0.060 20:1 20:1 0.00 Triangular N/A Leave as is _ 0.52 2.15 0.069 Outfalls 30+53-L-RT/0128 0.73 0.88 10.00 5.80 3.72 0.010 10:1 10:1 0.00 Triangular N/A Leave as is 0.62 0.98 0.069 34+42-L-RT/0207 1.16 0.90 10.00 5.80 6.07 0.025 3:1 3:1 5.00 Base 2.0000 Leave as.is 0.50 1.85 0.069 36+80-L-RT/0214 26.80 0.74 15.00 4.90 97.68 0.010 1:1 1:1 5.00 Base 5.0000 Leave as is 3.51 3.28 0.072 Downstream Outlet Depth Velocity Change(ft) Change(fps) Outtalk 19+71-L-LT/0101 0.01 -0.82 20+68-L-RT/0106 0.08 -0.57 30+53-L-RT/0128 0.26 -0.38 34+42-L-RT/0207 0.30 -0.26 36+80-L-RT/0214 0.20 -0.04 Page 6 of 6 Outfall Analysis for Davis Park East Pod B. Table of Contents 2-yr, 5-yr, 10-yr Pre-vs-Post Condition Flow Analysis Outfall Analysis Document for 10-yr Storm Drainage Area Figure and Description of Residential Drainage Issues Note: The 2-yr, 5-yr, and 10-yr storms were analyzed for the pre and post condition flows. Only the 10-yr storm results were reported on the redline drainage plans and in the Outfall Analysis Document. There were no concerns with the 2-yr and 5-yr storms where the 10-yr storm was not a concern. OUTFALL ANALYSIS 19+71 -L- (LT) OUTLET 0101 Description: The proposed outfall at 19+71 -L- (LT)is a 15"RCP that outlets into Class 'B' Rip Rap and flows into an existing ditch. The proposed system contains a drop inlet that will be piped under the driveway and discharged to the existing ditch. It flows in this ditch until it ultimately enters an existing system that continues to the west along Hopson Rd. : • I • E r i Igir - F I Photo 1: Existing Ditch Upstream of Existing Driveway .• Molt - • .I • . 4411k. • • . ••.• • • • • "21,•-e-• • Photo 2: Existing Ditch Downstream of Existing Driveway Analysis: • There are no expected adverse effects on the downstream receiving water. • There are no expected downstream inadequacies that would adversely impact the highway. • There are no expected effects to the adjacent property from the 10-yr storm. • The outfall has a 10-yr pre-construction flow of 0.90 cfs. The 10-yr post-construction flow is 0.51 cfs. This yields a 42.73% increase. This decrease was anticipated due to the interception of the ditch upstream of inlet 0102 by inlets 0107 and 0111,which discharge via outlet 0110 to the same ultimate outfall. The pre-construction velocity is 1.73 fps and the post-construction velocity is 0.91 fps. This yields a percent decrease of 47.40%. The water surface elevation for the pre- construction condition is 0.15 ft and 0.16 ft for the post-construction condition. This yields a percent increase of 6.67%. The changes in velocity and water surface elevation are due to the decrease in flow and the proposed rip rap pad at the outlet. • The proposed water surface is contained within the existing swale in the post condition. • No actions recommended at this time. OUTFALL ANALYSIS 20+68 -L- (RT) OUTLET 0106 Description: The proposed outfall at 20+68 -L-(RT)is a 15"RCP that outlets into Class 'B' Rip Rap. System 0106 and 0110 both ultimately flow into a detention-like channel along Distribution Drive. The existing pipe outlet was inaccessible due to dense vegetation. ;N - ti UI RI, 1.12misill iMnmEN. 15"RCP Outfall to '§ "{ "2°�`— Proposed Rip Rap Bed __ .„,, .. 7 ., _ t_...,..L.91=-a---- -mm- 7..! IYT k " L+4HE • • • k11 Q 1 - r'Y mo ' + �1 . .. , ,,, ---mr. - _, 1# T 1t 4 arm - . f R / '• ,. — -- V;ia w.w+H+j=n .. _ _ wir � E WAYe • l x • A ! f r +x 5 t r ! t • ti f t r r k 'x t c2 '! r i Photo 1: Proposed Drainage for Outfall 0106 Analysis: • There are no expected adverse effects on the downstream receiving water. • There are no expected downstream inadequacies that would adversely impact the highway. • There are no expected effects to the adjacent property from the 10-yr storm. • The outfall has a pre-construction flow of 0.48 cfs. The post-construction flow is 1.31 cfs. This yields a 175.17% decrease,but only a decrease of 0.83 cfs. The pre-construction velocity is 2.53 fps and the post-construction velocity is 1.96 fps. This yields a percent decrease of 22.53%. The water surface elevation for the pre-construction condition is 0.10 ft and 0.18 ft for the post- construction condition. This yields a percent increase of 80%. These increases were anticipated due to intercepting water on the curb to the south of the median. • The proposed water surface is contained within the existing channel in the post condition. • No actions recommended at this time. OUTFALL ANALYSIS 21+65 -L- (RT) OUTLET 0110 Description: The proposed outfall at 21+65 -L-(RT)is a 15"RCP that outlets into Class `B' Rip Rap just downstream of where the existing pipe outlets today. System 0106 and 0110 both ultimately flow into a detention-like channel along Distribution Drive. The existing pipe outlet was inaccessible due to dense vegetation. In both the pre-and post-conditions, offsite flow from the property just west of Keystone Park Drive was included as it gets to the ultimate outfall. gi _ 1Sw r il ' m. ±•... L u+RMiTa94 . 1, ��.y rry _ .—.slim Po W375.02 1 • 4g30 300.16 ; _"____. �� --_- ' _- - _�-v � ,© �40 — 15"RCP Outfall to ` - - Proposed Rip Rap Bed I 1 — x { , } t , r a �i `.— - ��,, 1 I_ r , , .. r - , , r - - -- girt? roar N-P tub Photo 1: Proposed Drainage for Outfall 0110 Analysis: • There are no expected adverse effects on the downstream receiving water. • There are no expected downstream inadequacies that would adversely impact the highway. • There are no expected effects to the adjacent property from the 10-yr storm. • The outfall has a pre-construction flow of 11.57 cfs. The post-construction flow is 11.67 cfs. This yields a 0.87%increase. The pre-construction velocity is 3.57 fps and the post-construction velocity is 2.15 fps. This yields a percent decrease of 39.78%. The water surface elevation for the pre-construction condition is 0.40 ft and 0.52 ft for the post-construction condition. This yields a percent increase of 30.00%. These changes in velocity and water surface elevation are due to adding a rip rap pad at the outlet. • The proposed water surface is contained within the existing channel in the post condition. • No actions recommended at this time. OUTFALL ANALYSIS 30+53 -L- (RT) OUTLET 0128 Description: The proposed outfall at 30+53 -L- (RT)outlets from an 18"RC,which will be extended from existing to discharge into the same channel. The existing pipe outlet was inaccessible due to dense vegetation. • • Yx Photo 1: Existing Conditions Upstream of Existing Pipe(Struct. 0126) $4 ° R }y 18"RCP Outfall to —- — ■ - - - - Existing Channel 4 i II it 1111 Alik P -- _ _.., . __ 1 _ At', -- _____. —__ __ .„-___, _ ., . -_...._. ,0-,-)). ____ . __....... . . ., . . _ , COL,. _ . ie.- ._, , __•- ,, .•. •. Arisrn,„, 4 4, Photo 2: Outlet of System 0128 into Existing Channel Analysis: • There are no expected adverse effects on the downstream receiving water. • There are no expected downstream inadequacies that would adversely impact the highway. • There are no expected effects to the adjacent property from the 10-yr storm. • The outfall has a pre-construction flow of 1.81 cfs. The post-construction flow is 3.72 cfs. This yields a 105.89% increase,but only an additional 1.91 cfs. The pre-construction velocity is 1.36 fps and the post-construction velocity is 0.98 fps.This yields a percent decrease of 27.94%. The water surface elevation for the pre-construction condition is 0.36 ft and 0.62 ft for the post- construction condition. This yields a percent increase of 72.22%. The flow increases are due to the widening and realignment of Hopson Drive east of Keystone Park Drive resulting in a larger total drainage area as well as more impervious area. The changes in water surface elevation and velocity are due to the flow increases and the installation of a rip rap pad. • The proposed water surface is contained within the existing channel in the post condition. • No actions recommended at this time. OUTFALL ANALYSIS 34+42 -L- (RT) Outlet 0207 Description: The outfall at 34+42-L-(RT) is an existing 15"RCP that is outlets into an existing channel south of Hopson Road just west of the existing railroad bridge. In the proposed condition, the pipe outlets 2' further from the road due to the proposed widening. The pipe outlet was not accessible due to dense vegetation. ;::.. r • a v.b: • 9 Via, - 41, y 14 ;,. • • , Photo 1: Existing Condition Upstream of Outlet Pipe(Struct. 0208) y I I 1 I I I . . -. • • 17bIF' .. 1 wry_ ~ - - ---Y +'lY l lI 4 f r J- -=- r ._=-_ - • _ saz. MT. OF STEEL CRIER 1,it lr ' r I; B-F*F:.�+@6T.9F STEEL ORDERr-—Ili 0 ,IMIM=...._ _,- II NIF 2111. ., 4, im. ( f• i !ff: urim :. „_,-_-:, • i ----` , • IFri A lL1! ;'I 7:s /leay r #;-M , �'� � 15"RCP Outfall to r t II ' - ; L, r'-- _ � -rik �� ° Existing Channel I + L 1 5 .z__ _ __- 7 I 1 rr11 f ``1J��,�� `_- , r r 1 l i • • J I l f 1r . __ r , II I I I •f • f r r 1F F .' --- �___�- % I I 1 I I F r F f r F } -_ r --- 1 1 f 1 FF + +Ff r r /FF/ �r • I'-1 + II E Photo 2:Proposed Outlet for System 0207 Analysis: • There are no expected adverse effects on the downstream receiving water. • There are no expected downstream inadequacies that would adversely impact the highway. • There are no expected effects to the adjacent property from the 10-yr storm. • The outfall has a pre-construction flow of 2.32 cfs. The post-construction flow is 6.07 cfs. This yields a 160.92%decrease. The pre-construction velocity is 2.11 fps and the post- construction velocity is 1.85 fps. This yields a percent decrease of 12.32%. The water surface elevation for the pre-construction condition is 0.20 ft and 0.50 ft for the post-construction condition. This yields a percent increase of 250%. These increases are a result of the increased impervious area and total area from the roadway widening. • The proposed water surface is contained within the existing channel in the post condition. • No actions recommended at this time. OUTFALL ANALYSIS 36+80 -L- (RT) Outlet 0214 The outfall at 36+80-L- (RT) is a 48"RCP conveying a jurisdictional stream. In existing, the jurisdictional stream flows through 3 @ 24"RCP's to an open channel before entering a 48"CMP to cross Hobson Road, as seen in Photo 1. The existing 48"CMP is in poor condition due to corrosion and breakage, as seen in Photo 3. The proposed design systemizes the JS and discharges it via a 48"RCP with a Class I Rip Rap pad to the existing channel. poi y 5 II y�,._1. I 1 _ kE57 I r I 5 7 rjr . --- R nvr37&,• + I f r __ Eesr I -3s_ '1 4'-^ - � ^ I f� - 1- CEI4: 1 ,-,7-...-"-z-- ':--------. ....Tr.s._CI"- rn . i il el;T:11 1.- i ii � - I _Mi�k IFIA MA!4.10±Ziqi dnirryna.. Tql5R-1111A • Existing 3 24"RCP's 41, _ET conveying JS,to be + Fa41 ti .— systemized via 48"w/ • ° 1.._, 1:I wo— II j : 1 r I•. '-+;� I=J. -", -117 I ! I y r1 ' rr- j/71� 111 tYY ,M ,1 • I I --I Iti 1 ; Ir Ir`l \1. I '•, F 48"Pipe Outlet with . 1 -;- i I 1� - t Class I Rip Rap i 11 1 ;' RCP• -�` I I I II , � I I 4 I 1 - i 171 ' AtE# R(" II I I .Aly .ir II, ,II I I II 50 ', 48 + 'P Photo 1: Proposed Drainage at Outlet 0214 _;going. "Tir If , .: . )111.4: r .4 1a t ^1�•. 's ,1F�.• old.t.r • ,. Existing 48"CMP Photo 2: Existing Conditions Upstream of 48" Crossing j�+g 1.. ' 't . % Corrosion/Breakage ,' ;, •- -.< -,`. , -. e 16 IL-. ;R• .• =R , 4 _ J '' r. ��y At. ! y� it r '''\ ' -sSk` N ,, t , --**4��, D `�� €'� 4 _� A __.�' Existing 48"CMP . -I ,„„ , ___ Photo 3: Existing Conditions at Outlet of 48" CMP i 4 1 m r + �4*y�� t r,I� 1 H • ! = W- '"Wi +[ r_ y <: na } ' ,,rr a R • ma .s. i '4,' i , . k'r Rµ � �1 pp t. 4 s rat �f a •. A ; ...:*+'.07 , livo7 * a $ s -ad • . � �F� 4 7fi- E Vit' v"�_ y itr"---- O ''w• y i mot—+ ti r iiirtw.al ,,,, 446-,t--,-, 17. 4 ,. -- . - _ fit" "r /" A' l „ x s'I f 1 e - 7 * R ,4j, It ,R! -r` - Photo 4: Existing Conditions Looking Downstream of 48" CMP Outlet Analysis: • There are no expected adverse effects on the downstream receiving water. • There are no expected downstream inadequacies that would adversely impact the highway. • There are no expected effects to the adjacent property from the 10-yr storm. The proposed 48" crossing meets NCDOT standards for the headwater/diameter for the 10- and 25yr storms. • The outfall has a pre-construction flow of 91.56 cfs. The post-construction flow is 97.68 cfs. This yields a 6.69%increase. The pre-construction velocity is 3.32 fps and the post-construction velocity is 3.28 fps. This yields a percent decrease of 1.20%. The water surface elevation for the pre-construction condition is 3.31 ft and 3.51 ft for the post-construction condition. This yields a percent increase of 6.04%. These increases are a result of the increased impervious area and total area from the roadway widening. • The proposed water surface is contained within the existing channel in the post condition. • No actions recommended at this time.