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HomeMy WebLinkAboutNC0003425_Fact Sheet_20200608 (4)DEPARTEMENT OF ENVIRONMENTAL QUALITY DIVISION OF WATER RESOURCES FACT SHEET FOR NPDES PERMIT DEVELOPMENT NPDES No. NC0003425 Facility Information Applicant/ FaciliName: Duke Energy Progress/ Roxboro Steam Electric Generating Plant Applicant Address: 1700 Dunnaway Rd., Semora, NC 27343 Facility Address: 1700 Dunnaway Rd., Semora, NC 27343 Permitted Flow Not limited Type of Waste: 99.8 % Industrial, 0.2% - domestic Facility/ Permit Status: Existing/ Renewal County: Person Miscellaneous Receiving Stream: Hyco Reservoir Stream Classification: WS-V, B Subbasin: 03-02-05 303 d Listed?: No Drainage Area mil : N/A Primary SIC Code: 4911 Summer 7Q10 cfs 0 Regional Office: RRO 30Q2 (cfs): 0 Quad Olive Hill Average Flow cfs): 0 Permit Writer: Ser ei Chernikov, Ph.D. IWC (%): 100% Date: 04/11/2019 Summary The Roxboro Steam Electric Plant is an electric generating facility that uses steam turbine generation via four coal-fired units with a with a combined electric generating output of 2558 MW: Unit No.1 (385 MWe), Unit No. 2 (670 MWe), Unit No. 3 (707MWe) and Unit No. 4 (700 MWe). The facility discharges to subbasin 030205 in the Roanoke River Basin. The facility operates five internal outfalls and two outfalls to Hyco Reservoir. Discharges are mostly industrial, with a very small domestic flow (internal Outfall 008) piped to the on -site ash pond. Discharges from the ash pond (internal Outfall 002), once -through cooling water and FGD treatment system (internal outfall 010) are discharged to the Heated Water Discharge Pond (outfall 003). The Heated Water Discharge Pond and Coal Pile Runoff (outfall 006) both discharge to Hyco Reservoir. The Hyco Reservoir is a 17.6 km2 waterbody constructed in 1963 by CP&L to serve as a cooling water source. The receiving waterbody is class WS-V; B. The facility is located in the Lower Piedmont area of the state, the applicable state water quality temperature standard is 32°C (89.6° F). This facility is subject to EPA effluent guideline limits per 40 CFR 423 - Steam Electric Power Generating Point Source Category which were amended November 3, 2015. The facility is also subject to the Cooling Water Intake Structures Rules (40 CFR 125) effective October 14, 2014. The intake flow is > 125 MGD. Duke requested the addition of three new outfalls on the permit; two to reflect the future treatment systems for the low volume wastes as the ash basin will be closed and one for the overflow from the east ash basin extension and stormwater runoff. Description of existing outfalls: Outfall 003 - Heated Water Discharge Pond to Hyco Reservoir. This pond combines all internal outfalls (002, 005, 008, 009, 010) before discharging to Hyco Reservoir. In addition, once -through cooling water from condensers for units 1, 2, and 3, once -through cooling water from heat exchangers, seepage from ash pond, and stormwater runoff from plant drainage areas are discharged to the discharge pond. NPDES PERMIT FACT SHEET Page 2 Roxboro Steam Electric Plant NPDES No. NC00003425 Outfall 006 - Coal Pile Runoff discharges directly to Hyco Reservoir. Coal pile runoff wastewaters include runoff from the coal pile, limestone pile and gypsum pile, truck wheel wash area and coal handling areas. Treatment is accomplished by neutralization, sedimentation and equalization. This is an episodic discharge. Internal Outfall 002 - Ash Pond discharging to the heated water discharge pond. The ash pond receives wastewater from the following source: • Bottom ash transport waters • Silo wash water • Ash landfill leachate and runoff (this landfill receives CCR from Mayo and Roxboro plants) • Dry -ash handling system wash water • Blowdown from Unit 4 cooling tower • Coal mill rejects and pyrites • Sewage treatment plant effluent • Low volume waste consisting of boiler blowdown, equipment maintenance cleaning wastewaters, RO reject wastewater and floor drains. Low volume wastes are treated by neutralization. • Emergency overflow from FGD system blowdown. Internal Outfall 005 - Cooling tower blowdown from Unit 4. Internal Outfall 008 - Treated domestic wastewater. The treatment system consists of a screen, communitor, surge tank, aeration tank, clarifier, chlorine contact chamber and sludge holding tank. A new package plant will be installed to replace the existing plant. Internal Outfall 009 - Chemical metal cleaning waste. Wastewaters from cleaning of the boilers is generated every five to eight years. Every three to five years wastewaters are generated from cleaning the heat exchangers. The wastewaters generated can be treated by evaporation or by neutralization and precipitation. Internal Outfall 010 - Flue Gas Desulfurization (FGD) treatment system discharging to the discharge canal. The scrubber system removes SOx by mixing flue gas with a limestone slurry. The blowdown from the scrubber is discharged to a gypsum settling pond system then to a bioreactor which utilizes microorganisms to reduce soluble contaminants to insoluble forms (under anaerobic conditions) that then precipitate from solution. Wastewater is discharged to the ash pond effluent channel. An emergency overflow from the FGD system blowdown discharges to the ash pond. Proposed Outfalls: Outfall 001- Stormwater and the oveflow from the east ash basin extension. The east ash basin was closed and subsequently a landfill was built over the old basin. A portion of the basin remained as an open pond. It has come to the attention of the Division that there are some coal combustion residuals within the pond. The Division has requested that Duke removes the residuals. In addition to the pond overflow this outfall discharges stormwater runoff. Internal Outfalls 012A, 012B and 012C - Low volume waste and other wastewaters. Duke will build two basin treatment systems to treat wastewaters that now go to the ash basin. The basins will discharge to the heated discharge pond and an emergency overflow from one of the basins will discharge to Hyco Lake (012C). W NPDES PERMIT FACT SHEET Roxboro Steam Electric Plant Page 3 NPDES No. NC00003425 CWA 316 (b) The permittee shall comply with the Cooling Water Intake Structure Rule per 40 CFR 125.95. The Division approved the facility request for an alternative schedule in accordance with 40 CFR 125.95(a)(2). The permittee shall submit all the materials required by the Rule by May 31, 2022. This is an accelerated schedule that includes: 1 year for the development of the sampling plan and obtaining approval from the Division, 2 years of sampling to adequately characterize seasonal variation, and 1 year for the report development. Based on the results of the studies, the Division may require an implementation of the additional measures to reduce impingement and entrainment of the aquatic organisms. The facility's total intake is designed for approximately 1,114 MGD. Units No.1 and 2 use condensers as cooling devices. Units No. 3 and 4 use cooling towers as cooling devices. Units 1 and 2 operate in a once - through cooling mode year round. Unit 3 operates in a once -through cooling mode part of the year (October 15th - April 30th) and during summer months (May 1st - October 14th) condenser cooling water is routed to once -though mechanical draft cooling tower. Unit 4 is equipped with closed -cycle evaporative cooling towers that operate year-round. The CWIS for Unit 4 (CWIS 4) is located on the north bank of the heated water discharge pond, adjacent to the Unit 4 closed -cycle cooling tower. As a result, there is no net increase in cooling water withdrawal for the Unit 4 cooling tower make-up water. The CWIS for Units 1-3 (CWIS 1) is located at the intake forebay immediately east of the Unit 1 turbine - generator. Cooling water for Units 1-3 is withdrawn through eight bays in CWIS 1 via a 1.7-mile intake canal located east north-east of the plant. The intake canal directs water to an intake pond which is connected to the CWIS 1 intake forebay area via a submerged culvert. Unit 1 consists of two intake bays equipped with one circulating water pump per bay. Units 2 and 3 each consist of three intake bays equipped with one circulating water pump per bay. Each of the eight intake bays for CWIS 1 is equipped with trash racks and coarse -mesh (3/8-inch mesh size) vertical traveling screens with a debris spray wash system and debris collection trough. Duke Energy provided the following justification as Basis for Designation Belews Station as a Closed Cycle Recirculation System: A "closed -cycle recirculating system' is defined at 40 CFR 125.92 (c). The definition addresses facilities with CCRS that withdraw from waters of the United States where the impoundment was constructed for the purpose of providing cooling water for the facility: "Closed -cycle recirculating system also includes a system with impoundments of waters of the U.S. where the impoundment was constructed prior to October 14, 2014 and created for the purpose of serving as part of the cooling water system as documented in the project purpose statement for any required Clean Water Act section 404 permit obtained to construct the impoundment. In the case of an impoundment whose construction pre -dated the CWA requirement to obtain a section 404 permit, documentation of the project's purpose must be demonstrated to the satisfaction of the Director. This documentation could be some other license or permit obtained to lawfully construct the impoundment for the purposes of a cooling water system, or other such evidence as the Director finds necessary." 40 CFR 125.92 (c)(2). Impoundments are further defined and discussed as a closed -cycle cooling system in the rule's preamble, stating that: "Impoundments are surface waterbodies that serve as both a source of cooling water and a heat sink. As with cooling towers, impoundments rely on evaporative cooling to dissipate the waste heat; a facility withdraws water from one part of the impoundment and then discharges the heated effluent back to the impoundment, NPDES PERMIT FACT SHEET Page 4 Roxboro Steam Electric Plant NPDES No. NC00003425 usually in another location to allow the heated water time to cool. Depending on local hydrology, impoundments may also require makeup water from another waterbody. Impoundments can be man-made or natural, and can be offset from other water bodies or as part of a "run of the river" system (the latter are sometimes referred to as cooling lakes)." 79 Fed. Reg. 48,334 (August 15, 2014) The system at Roxboro meets the criteria for classification as a CCRS. Roxboro withdraws cooling water from Hyco Lake which was constructed in a water of the United States for the purpose of providing cooling water for the Carolina Power & Light Company (now Duke Progress, LLC) Roxboro Steam Electric Plant prior to the Clean Water Act 404 permitting program. The Carolina Power & Light Company received authorization for the creation of Hyco Lake in April 1964 for the Roxboro facility. Numerous documents issued by the State contain several statements and commensurate justification that the purpose of Hyco Lake was to be "operated ... to reduce pollution [via condenser cooling water recirculation] in the Hyco River" and is a "cooling pond": • State of North Carolina Department of Water and Air Resources Permit 522 issued May 4, 1964 • Carolina Power & Light Company, North Carolina State Stream Sanitation Committee "Application for Approval of Plans" dated April 13,1964 • North Carolina Board of Water and Air Resources Permit 522 Certification dated October 1, 1971 • North Carolina Environmental Management Commission Permit 2523 issued July 22,1974 The permit issued by the State of North Carolina Department of Water and Air Resources (the predecessor Agency to the North Carolina Department of Environmental Quality) authorized "...operation of a 3,800 acre cooling lake for a design flow of 2,400,000,000 G.P.D., and the discharge of the effluent into the Hyco River, a tributary in the Roanoke River Basin". The dam was completed in 1964 and Hyco Lake reached full pool elevation in 1965. As also required by the definition, make-up water withdrawals attributable to the cooling portion of the Roxboro cooling system have been minimized. The source of all makeup water is the approximately 300 square mile Hyco Lake watershed. No other sources of makeup water are currently available and none are planned. In addition to minimizing withdrawals for make up water to Hyco Lake, Roxboro also minimizes cooling water withdrawals from Hyco Lake in multiple ways. First, Unit 4 operates on recirculating cooling towers that require only small volumes of makeup waters. Those make up waters are taken from internal process areas consisting of Unit 1-3 cooling water discharge and the ash basin discharge flows. Second, the cooling water system for Units 1-3 has several design features that increase their efficiency, including (a) directing deeper, cooler water to the intake as needed to maintain efficiency by using cooler water from deeper in the reservoir; (b) routing of cooling water discharges as far as possible upstream from the cooling water intake (subject to constraints imposed by the Department for thermal impact reasons); and (c) utilization on Unit 3 of a helper cooling tower seasonally which reduces the thermal discharge load to the lake and allows for more efficient cooling during the summer months. Third, as reflected in the company's Integrated Resources Plans, filed with the North Carolina Utilities Commission, Roxboro has operated since 2016 as an "Intermediate" rather than "Baseload" generation source. The reduction in operating time has resulted in a reduction of average daily withdrawals from greater than 800 MGD when the plant operated as Baseload to 592 MGD in 2018, as reported in the station's annual water withdrawal reports. al NPDES PERMIT FACT SHEET Page 5 Roxboro Steam Electric Plant NPDES No. NC00003425 The Division concurs with the justification provided by Duke on a provisional basis. Based on 40 CFR 125.92 (c) the Director has determined that operating and maintaining the existing closed - cycle recirculating system meets the requirements for a provisional BTA. The final determination will be made upon review of the materials submitted by the permittee. This determination is consistent with the EPA Region IV decision regarding Robinson station and Belews station, and the EPA Region III decision regarding North Anna station. Temperature Mixing Zone - Outfall 003 The facility is located in the Lower Piedmont area of the state, the applicable state water quality temperature standard is 32°C (89.6° F). The authorized temperature mixing zone for outfall 003 includes the North Hyco Arm downstream of NC Hwy 57, the main body of Hyco Reservoir downstream of the confluence of the Cobbs Creek Arm and the North Hyco Arm and the entire after bay lake. USGS data at the after bay monitoring station (USGS Station 02077303) was reviewed for the period of January 2011 to April 2016. Data shows that the temperature water quality standard was not exceeded for this period. Maximum temperature recorded was 30.5°C. Instream Monitoring The permit requires monitoring of Hyco Reservoir in accordance to the Biological Monitoring Program as approved by the Division. Based on the Divisions review of the reports the fish community is comparable to other piedmont reservoirs and no problems were noted. The draft permit includes instream monitoring for total arsenic, total selenium, total mercury, total chromium, dissolved lead, dissolved cadmium, dissolved copper, dissolved zinc, total bromide, total hardness (as CaCO3), turbidity, and total dissolved solids (TDS). The draft permit also includes annual fish tissue monitoring. DATA REVIEW/PERMIT REQUIREMENTS Internal Outfall 002 - Ash Pond This outfall is subject to the Effluent Limitations Guidelines (ELG) in Table 1. Table 1. ELG Outfall 002 (Prior to November 1, 2018) Pollutant Daily Maximum Monthly Average ELG TSS 100 m /L 30 m /L 40 CFR 423.12 (b) (4 Oil & Grease 20 mg/ L 15 m /L 40 CFR 423.12 (b) (4 The current permit requires monitoring for flow and total selenium, limits for Oil & Grease and TSS. A summary of DMR data for the period of January 2011 to January 2016 is included in Table 2. There have been no violations of permit limits or conditions. Table 2. DMR Summary Outfall 002 Parameter Average Maximum Minimum Flow 10.8 MGD 48.3 MGD 3.1 MGD TSS 5 m /L 21 m /L < 2.5 m /L Total Selenium 14.6 µ /L 68.8 µ /L < 10 µ /L O&G <5m /L 13.5m /l <5m /L Table 3. Monitoring Requirements/Proposed Changes Outfall 002 Parameter W Monitoring requirements Changes Basis Flow Monitor No changes 15A NCAC 2B.0505 TSS 30 mg/L monthly aver 100 m /L daily max No changes 40 CFR 423.12(b)(4) 5 NPDES PERMIT FACT SHEET Page 6 Roxboro Steam Electric Plant NPDES No. NC00003425 Oil & Grease 15 mg/L monthly aver No Changes 40 CFR 423.12(b)(4) 20 m /L daily max Total Selenium Monthly monitoring No changes Pollutant of concern Turbidity, pH No requirement Monitor Pollutant of concern for dewatering/ decanting Schedule of Compliance Fly Ash/Bottom Ash: As per 40 CFR 423.13 (k) (1) (i) bottom ash transport water shall not be discharged, compliance with this section shall be as soon as possible beginning on November 1, 2020, but no later than December 31, 2023. Duke utilizes wet bottom ash transport system. Duke is proposing to install a remote mechanical drag chain system. Design of the system is expected to be completed in 8 months, followed by procurement in 12 months. Construction is expected to be completed in 13 months. Duke proposes a 16 month window to optimize the system at full load and additional 6 months for potential permitting delays. Consideration was given to the fact that Duke will be undertaking design, procurement and installation activities in multiple facilities simultaneously. Duke will meet the no discharge of bottom ash requirement by April 30, 2021. Fly ash transport water is no longer discharged therefore Duke meets the compliance date of November 1, 2018. Internal Outfall 002 - Dewatering To meet the requirements of the Coal Ash Management Act of 2014, the facility needs to dewater two ash ponds by removing the interstitial water and excavate the ash to deposit it in landfills. The facility's highest discharge rate from the dewatering process will be 2 MGD. The facility submitted data for the standing surface water in the ash ponds, interstitial water in the ash, and interstitial ash water that was treated by filters of various sizes. The following pollutants were detected at concentrations higher than the water quality standards: selenium, arsenic and molybdenum. A new effluent and monitoring sheet is included in the permit for the ash pond dewatering phase. As this is an internal outfall the water quality standards are not applied. Monitoring will be required for selenium, arsenic, molybdenum, antimony, mercury and copper. Outfall 003 - Heated Water Discharge Pond (Combined outfalls) DMR/ Compliance Review Data were reviewed for the period of January 2011 to March 2016. There have been no violations of permit limits or conditions. Table 4. DMR Summary Outfall 003 Parameter Average Maximum Minimum Flow MGD 840 1130 6.9 TRC Not discharged TP m /L < 0.036 < 0.05 < 0.05 TN m /L 0.68 1.08 0.44 Temperature (°C) 29 41 130C Total Arsenic (µ /L) 6.2 17.1 < 2.8 H SU 7.34 8 6.38 Toxicity Testing (003): Current Requirement: Acute P/F at 90%, February, May, August, November. Proposed Requirement: Acute P/F at 90%, February, May, August, November. The facility passed 21 tests out of 21 tests performed for the period of January 2011 to January 2016. Co NPDES PERMIT FACT SHEET Roxboro Steam Electric Plant Page 7 NPDES No. NC00003425 Reasonable Potential Analysis Outfall 003: The Division conducted EPA -recommended analyses to determine the reasonable potential for toxicants to be discharged at levels exceeding water quality standards/EPA criteria by this facility from outfall 003. For the purposes of the RPA, the background concentrations for all parameters were assumed to be below detection level. The RPA uses 95% probability level and 95% confidence basis in accordance with the EPA Guidance entitled "Technical Support Document for Water Quality -based Toxics Control." With the approval of the Triennial Review (2007-2014) of the NC Water Quality Standards by the Environmental Management Commission (EMC) in 2014 and US -EPA (with some exceptions) on April 6, 2016, the NPDES Permitting Unit is required to implement the new dissolved metal standards in all permits public noticed after April 6, 2016. The RPA included evaluation of dissolved metals' standards, utilizing measured hardness value of 100 mg/L CaCO3 for hardness -dependent metals. A reasonable potential analysis was conducted for arsenic, copper, nickel, selenium, strontium, thallium, chlorides and zinc. Arsenic data used for the RPA was collected between 2011 and 2016. Data for the remaining parameters was from a special study for the period of March 2010 to August 2011. Based on this analysis, the following permitting actions are proposed for this permit: • Monitoring Only. The following parameters will receive a monitor -only requirement since they did not demonstrate reasonable potential to exceed applicable water quality standards/criteria, but the maximum predicted concentration was >50% of the allowable concentration: Arsenic, selenium, chloride. • No Limit or Monitoring: The following parameters will not receive a limit or monitoring, since they did not demonstrate reasonable potential to exceed applicable water quality standards/criteria and the maximum predicted concentration was <50% of the allowable concentration: copper, nickel, strontium, and zinc. Mercury Evaluation Outfall 003: A mercury evaluation was conducted in accordance with the permitting guidance developed for the implementation of the statewide Mercury TMDL to determine the need for a limit and Mercury Minimization Plan (MMP). Monitoring for mercury is not required for outfall 003 but mercury data was collected during a special study during the period of March 2010 to August 2011. The water quality based effluent limitation (WQBEL) for mercury is 12 ng/1. The technology based effluent limit (TBEL) is 47 ng/1. None of the annual averages exceeds the WQBEL or TBEL, no limit is required. See the attached mercury evaluation spreadsheet. Table 5. Mercury Evaluation 2010 2011 # of Samples 20 16 Annual Average, n /L 3.6 4.4 Maximum Value, n /L 7.63 6.92 TBEL, n /L 47 WQBEL, n /L 12.0 7 NPDES PERMIT FACT SHEET Page 8 Roxboro Steam Electric Plant NPDES No. NC00003425 TRC 200 µg/L Modified limit to State WQ standards, 15A NCAC instantaneous max 28 µg/L daily max 2B .0200. The water quality standard is more stringent than the effluent guidelines limit. TP Monitor No changes 15A NCAC 2B .0500 TN Monitor No changes 15A NCAC 2B .0500 Temperature Monitor No changes Approved Mixing zone Total Arsenic Monitor No changes Based on results from RPA, Predicted concentration greater than 50 % of allowable. Total Selenium No requirement Quarterly monitoring Based on results from RPA, Predicted concentration greater than 50 % of allowable. Total Thallium No requirement Quarterly monitoring Pollutant of concern. Chloride No requirement Quarterly monitoring Based on results from RPA, Predicted concentration greater than 50 % of allowable. pH 6 to 9 SU No changes State WQ standards, 15A NCAC 2B .0200 Acute toxicity P/F 90% No changes State WQ standards, 15A NCAC 2B .0200 Internal Outfall 005 - Cooling Tower Blowdown from Unit 4 This outfall is subject to the ELGs in Table 7. Table 7. ELG Outfall 005 Pollutant Daily Maximum Monthly Average ELG Free Available Chlorine 0.5 mg/L 0.2 mg/L 40 CFR 423.12 (d) (1) 126 Pollutants No detectable amounts 40 CFR 423.13 d 1 Total Chromium 0.2 m /L 0.2 m /L 40 CFR 423.13 (d) (1) Total Zinc 1.0 m /L 1.0 m /L 40 CFR 423.13 (d) (1) The permit includes monitoring for flow and Total Residual Chlorine (TRC), limits for Free Available Chlorine, Total Chromium, Total Zinc and 126 priority pollutants. Special condition A. (14) in the current permit doesn't allow the discharge of the cooling tower blowdown to the discharge pond, it has to be discharged to the ash pond. With the modifications planned to the site and the future closure of the existing ash pond Duke will like to have the option to discharge the blowdown to the discharge pond. This will continue to be an internal outfall subject to the same limits under 40 CFR 423. The limits apply before it comingles with any other waste stream so there is no change in limits or other permit conditions by allowing the cooling tower blowdown to discharge into the discharge pond. DMR/ Compliance Review: Data were reviewed for the period of January 2011 to January 2016. There have been no violations of permit limits or conditions. Flow was the only parameter monitored at this outfall since the facility did not chlorinate or added chromium or zinc for maintenance activities. Flow is reported as 7.2 MGD on a daily basis. NPDES PERMIT FACT SHEET Page 9 Table 8. Monitoring Requirements/Proposed Changes Outfall 005 Roxboro Steam Electric Plant NPDES No. NC00003425 Parameter Monitoring Requirements/Limits Changes Basis Flow Monitor No changes 15A NCAC 2B.0505 Free available 500 µg/L daily max No changes 40 CFR 423.13 (d)(1) chlorine 200 µ /L monthly average Total Residual Chlorine Monitoring No changes 40 CFR 423.13 (d) (2) Total chromium 200 µg/L daily max No changes 40 CFR 423.13 (d)(1) 200 µ /L monthly average Total Zinc 1.0 mg/L daily max No changes 40 CFR 423.13 (d)(1) 1.0 m /L monthly average The 126 priority pollutants No detectable amount No changes 40 CFR 423.13 (d)(1) Outfall 006 - Coal Pile Runoff This outfall is subject to the ELG in Table 9. Table 9. ELG Outfall 006 Pollutant Daily Maximum Monthly Average ELG TSS 50 m /L 40 CFR 423.12 b 9 pH 6 to 9 SU 40 CFR 423.12 b 1 DMR/ Compliance Review: Data were reviewed for the period of January 2008 to March 2013. There have been no violations of permit limits or conditions. Table 10. DMR Su ary Outfall 006 Parameter Average Maximum Minimum Flow (MGD) 0.23 0.05 0.002 TSS (m / L) 2.6 76.6 < 2.5 pH (SU) 7.39 8.9 6.04 Priority Pollutant Scan: The application included the results of one scan. Selenium was detected above the water quality standard. This is an episodic discharge. The pond only discharges under heavy rain events, therefore limits will be applied as acute limits. Table 11. Monitoring Requirements/Proposed Changes Outfall 006 Parameter Monitoring Changes re uirements/Limits Flow Monitor No changes 15A NCAC 2B .05 TSS 50 mg/L instantaneous No changes 40 CFR 423.12(b)(9) max H 6 to 9 SU No changes 40 CFR 423.12 b 1 Total selenium No requirement 56 µ /L Daily Max RPA Acute toxicity P/F 90% No changes State WQ standards, 15A NCAC 2B .0200 9 NPDES PERMIT FACT SHEET Page 10 Internal Outfall 008 - Domestic WWTP Table 12. DMR Review Outfall 008 Roxboro Steam Electric Plant NPDES No. NC00003425 Parameter Average Maximum Minimum Flow (MGD) 0.007 0.01 0.002 TSS (m /1) 14.7 30 5 H SU 6.8 7.3 6.5 BOD m /L 10.4 28 2.1 NH3N m /L 0.8 1.6 < 0.1 Table 13. Monitoring Requirements/ Proosed Changes Outfall 008 IP Parameter Monitoring Changes 6k- re uirements/Limits Flow 0.015 MGD 0.025 MGD WWTP was upgraded TSS 30 mg/L monthly No changes NPDES rules for secondary aver treatment of domestic 45 m /L daily max wastewater,15A 2B .0400 pH 6 to 9 SU No changes State WQ standards,15A 2B .0200 BOD 30 mg/L monthly No changes NPDES rules for secondary aver treatment of domestic 45 m /L daily max wastewater,15A 2B .0400 Total ammonia Monitor No changes DWQ Policy Internal Outfall 009 - Chemical cleaning waste Table 14. Monitoring Requirements/Proposed Changes Outfall 009 Parameter Monitoring requirements/Limits Changes Flow Monitor No changes 15A NCAC 2B.0505 Total Copper 1.0 mg/L monthly aver No changes 40 CFR 423.13 (e) 1.0 m /L daily max Total Iron 1.0 mg/L monthly aver No changes 40 CFR 423.13 (e) 1.0 m /L daily max TSS 30 mg/L monthly aver No changes 40 CFR 423.13 (e) 100 m /L dail max Oil & Grease 15 mg/L monthly aver No changes 40 CFR 423.13 (e) 20 mg/ L daily max Internal Outfall 010 - FGD This outfall is subject to the Effluent Limitations Guidelines (ELG) in Table 15. These are new limitations promulgated November 3, 2015. Table 15. ELG Outfall 010 Pollutant Daily Maximum ff I Monthly Average ELG H 6 to 9 SU 40 CFR 423.12 b 1 TSS 100 m / L 30 m / L 40 CFR 423.12 b 11 Oil and grease 20 m /L 15 m /L 40 CFR 423.12 b 11 Total Arsenic 11 µ /L 8 µ /L 40 CFR 423.13 1 i Total Mercury 788 n /L 356 n /L 40 CFR 423.13 1 i Total Selenium 23 µ /L 12 µ /L 40 CFR 423.13 1 i Nitrate/nitrite 17 m /L 4.4 m /L 40 CFR 423.13 () (1) (i) 10 NPDES PERMIT FACT SHEET Page 11 Roxboro Steam Electric Plant NPDES No. NC00003425 The current permit includes monitoring for flow, total beryllium, total mercury, total antimony, total selenium, total silver and total vanadium. Table 16 includes a summary of DMR data for the period of January 2011 to January 2016. There have been no violations of permit limits or conditions. Table 16. DMR Summary Outfall 010 Parameter Average Maximum Minimum Flow (MGD) 0.84 1.77 0.01 Total Beryllium µ /L 3.9 10 < 1 Total Mercury µ /L 1.08 9.6 < 1 Total Selenium µ /L 102 712 < 50 Total Silver µ /L 6 8.4 < 5 Total Antimony µ /L 31 70 < 25 Total Vanadium (µ /L) < 25 < 25 < 5 Table 17. Monitoring Requirements/Propose Changes Outfall 010 Parameter Monitoring Changes Basis requirements/Limits Flow Monitor No changes 15A NCAC 2B.0505 Total Beryllium Monitor Remove monitoring Internal outfall, not a parameter of concern. Total Vanadium Monitor Remove monitoring Internal outfall, not a parameter of concern. Total Antimony Monitor Remove monitoring Internal outfall, not a parameter of concern. Total Silver Monitor Remove monitoring Internal outfall, not a parameter of concern. Total Arsenic No monitoring 11 µg/L daily max and 8 µg/L monthly 40 CFR 423.13 (g) (1) (i) average Total Selenium Monitor 23 µg/L daily max and 12 µg/L monthly 40 CFR 423.13 (g) (1) (i) average Nitrate/Nitrite No monitoring 17 mg/L daily max and 4.4 mg/L monthly 40 CFR 423.13 (g) (1) (i) average Total Mercury Monitoring 788 ng/L daily max and 356 ng/L monthly 40 CFR 423.13 (g) (1) (i) average. Schedule of Compliance FGD: 40 CFR 423 establishes compliance dates for the new limitations. Permittee must meet limits as soon as possible beginning on November 1, 2020 but no later than December 31, 2023. Duke utilizes a biological treatment system to treat FGD wastewaters. Duke anticipates that it will be required to install physical/chemical treatment followed by selenium reduction technology to meet the FGD guidelines. Evaluation of new technologies, design, and siting of the system is expected to take 30 months. The evaluation phase includes evaluation of existing treatment system, flow optimization, siting of the new system within the plant, selection of technology and permitting. Procurement is expected to be completed in 20 months, construction and tie-in expected to be completed in 16 months considering that tie-in has to be done during outages. Startup and optimization under all expected operating conditions is estimated for 15 months. An additional 6 months is included in the schedule for potential permitting delays. Duke will meet the FGD ELG by December 31, 2021. As the new treatment system will be placed 11 NPDES PERMIT FACT SHEET Page 12 Roxboro Steam Electric Plant NPDES No. NC00003425 in operation and the old pond may still discharge until it is decommissioned a new outfall is included in the permit for the new system. Proposed Outfalls Requirements: OlItfall 001 RPA: An RPA was conducted for proposed outfall 001. RPA was conducted for total arsenic, cadmium, chlorides, total chromium, total copper, total lead, total mercury, total molybdenum, total nickel, selenium, total zinc, antimony, sulfate and total thallium. As a result of the RPA limits are required for the following parameters: arsenic, fluoride, sulfides and selenium. Mercury Mercury data was collected during 2014 and 2015. 2014 data was collected using method 245 which has a higher detection limit that 1631. Data for 2015 was used to evaluate a need for a limit. The annual average was 5.2 ng/1, no limit will be implemented. Table 18. Outfall 001 Proposed Limits/Monitoring: Parameter Monitoring requirements/Limits Basis Flow Monitor 15A NCAC 213.0505 pH 6 to 9 SU State WQ standards, 15A 2B .0200 Total arsenic, total copper, total Monitor Coal ash parameters of concern. antimony, total lead, total zinc, total barium, total iron, total manganese, total nickel, total mercury, and chlorides Total Selenium 5 µg/L Monthly Average RPA 56 µg/L Daily Max Total Arsenic 10 µg/L Monthly Average RPA 340 µg/L Daily Max Fluoride 1.8 mg/L Monthly Average RPA 1.8 mg/L Daily Max Sulfates 250 mg/L Monthly Average RPA 250 mg/L Daily Max TDS, Hardness, Conductivity Monitor Parameters of concern Acute toxicity Quarterly Limit State WQ standards, 15A NCAC 2B .0200 Low Volume Waste Treatment System: Two new treatment systems will be installed to treat wastewaters currently delivered to the ash basin. Low volume wastes, metal cleaning wastes, stormwater, and other miscellaneous wastes that are routed to the ash basin will be rerouted to new treatment systems. Duke proposes two separate treatment systems. The new outfalls will be designated as outfall 012A and outfall 012B. The overflow from the 012B basin will be designated as outfall 012C. Duke estimated that design, construction and start up of the new treatment system will be completed within 30 months of permit issuance. 12 NPDES PERMIT FACT SHEET Page 13 Roxboro Steam Electric Plant NPDES No. NC00003425 Internal Outfall 012A - treatment system for the landfill stormwater, treated extracted groundwater, contact and non -contact storm water and discharging to the discharge pond. Table 19. Outfall 012A Proposed Limits/Monitoring: Parameter Monitoring KVeq Basi uirements/Limits Monitor Flow 15A NCAC 2B.0505 Total Suspended Solids 30 mg/L Monthly Average 40 CFR 423.12 (b)(3) 100 m /L Daily Max Oil & Grease 15 mg/L Monthly Average 40 CFR 423.12 (b)(3) 20 m /L Daily max Total arsenic, total selenium, total Monitor during ash basin Parameters of concern mercury, total molybdenum, total closure antimony, total copper Internal Outfall 012B - treatment system for plant low volume wastes, FGD treatment system effluent, domestic waste treatment system, anhydrous ammonia emergency discharge, metal cleaning wastes, stormwater runoff, and cooling tower blowdown. The discharge from outfall 012B will go to the discharge canal. Table 20. Outfall 012B Proposed Limits/Monitoring: Parameter Monitoring requirements/Limits Basis Flow Monitor 15A NCAC 2B.0505 Total Suspended Solids 30 mg/L Monthly Average 100 m /L Daily Max 40 CFR 423.12 (b)(3) Oil & Grease 15 mg/L Monthly Average 20 m /L Daily max 40 CFR 423.12 (b)(3) Ammonia Monitor Monitor during emergency discharge of anh drous ammonia Emergency Outfall 012C - This is the emergency overflow from the low volume waste treatment system (Outfall 012B) Table 21. Outfall 012C Proposed Limits/Monitoring: Parameter Monitoring re uirements/Limib Basis Flow Monitor 15A NCAC 2B.0505 Total Suspended Solids 30 mg/L Monthly Average 100 m /L Daily Max 40 CFR 423.12 (b)(3) Oil & Grease 15 mg/L Monthly Average 20 m /L Daily max 40 CFR 423.12 (b)(3) Ammonia 1.0 mg/L Monthly average 5.0 mg/L Daily max Monitor during emergency discharge of anhydrous ammonia Arsenic Monitor Parameter of concern Mercury Monitor Parameter of concern Selenium Monitor Parameter of concern Nitrate/ nitrite Monitor Parameter of concern Copper Monitor Parameter of concern Iron Monitor Parameter of concern 13 NPDES PERMIT FACT SHEET Page 14 Public Notice/Public Hearin Roxboro Steam Electric Plant NPDES No. NC00003425 The first draft of this permit was public noticed on August 30, 2016. A public hearing was held on October 4, 2016. A second public notice was done on January 21, 2017 since the first notice went to a newspaper out of the area. Summary of permit modifications: • A separate effluent page for the dewatering of the ash ponds (Outfall 002) was added to the permit. • Outfall 001 was reinstated to monitor discharge of seeps and stormwater. • A new internal outfall (Outfall 011) was added to the permit to monitor the discharge from the proposed FGD treatment system. • Special Condition A. (14) that prohibited the discharge of cooling tower blowdown from outfall 005 to the discharge canal was eliminated from the permit. • A special condition was added to describe Section 316(b) requirements for submittal of applicable information. • A special condition was added to the permit to require an Ash Pond Closure Plan. • A Special Condition was added to the permit to require compliance with Senate Bill 729 (Coal Ash Management Act). • Attachment 1 entitled "Groundwater Monitoring Plan" was added to the permit. • Attachment 2 entitled "Plan for Identification of New Discharges" was added to the permit. Summary of modifications to October 2016 permit: • Condition A. (1) Effluent Limitations and Monitoring Requirements for seeps - monitoring requirements were updated to include the same list of parameters monitored for seeps in other Duke permits. • Condition A. (2) Effluent Limitations and Monitoring Requirements for the ash basin - monitoring was added for arsenic, molybdenum, and chromium. In addition, a statement was added with the requirement to use physical/chemical treatment during dewatering. • Condition A. (2) & A. (3) Effluent Limitations and Monitoring Requirements for the ash basin - Statement regarding no discharge of fly ash was modified to read that no discharge of fly ash is allowed. The statement pertaining to the schedule of compliance with the ELG for zero discharge of bottom ash was corrected to read April 30, 2021 instead of November 1, 2018. • Condition A. (10) & A. (11) Effluent Limitations and Monitoring Requirements for the FGD - footnote 3 was corrected to read December 31, 2023. • Turbidity sampling was eliminated from internal outfall 002. Turbidity monitoring is included at outfall 003. • Supplement to cover sheet was modified to include flows that were not listed and add proposed outfalls and outfalls. • Condition A. (6) Effluent Limitations and Monitoring Requirements outfall 006: o Oil and Grease limits were added since it receives truck wash waters. o The RPA was revised and limits for total selenium were added. • Condition A. (4) Effluent Limitations and Monitoring Requirements for outfall 003: o Footnote 4 was modified to include a statement regarding the addition of temperature limits if the facility is not in compliance with the temperature water quality standard. o Reporting of the temperature at the afterbay station was added to the monitoring requirements for outfall 003, reporting of temperature at 4C, 4D was eliminated. o The RPA was revised and limits for thallium were added. • Condition A. (17)- temperature reporting requirements were modified. 14 NPDES PERMIT FACT SHEET Page 15 Roxboro Steam Electric Plant NPDES No. NC00003425 • A. (8) Effluent Limitations and Monitoring Requirements for outfall 008 - monitoring requirements were modified to require quarterly monitoring for one year after the new plant start operations, annual monitoring is required after one year of quarterly monitoring. • Two new internal outfalls (Outfall 012A and 012B) were added to the permit for the two proposed retention basins for the treatment of low volume wastes that are now sent to the ash basin. Duke will build two separate wastewater treatment systems to handle the wastes that go to the ash pond. These ponds will be in different locations in the site and will require each a separate outfall into the effluent channel. • Outfall 012C was added to the permit for the emergency overflow of the proposed lined retention basin discharging through outfall 012B. • A table including a list of all the seeps locations was added to Condition A. (14). Modifications to January 2017 draft permit: • Seeps special condition was eliminated. Seeps will be addresses through Special Order by Consent EMC SOC WQ S18-005. • The groundwater monitoring well construction and sampling condition was eliminated from the permit. • A footnote was added to outfalls 001 and 003 that requires that the discharge from the decanting/dewatering operations is discontinued if any of the identified pollutants reaches 85% of the allowable concentrations. • Requirements for Outfall 001 were modified. The outfall location was established at the UT to Hyco Lake. Monitoring was increased to weekly during the removal of the ash from the east ash basin extension. • RPA for outfall 003 was revised using updated thallium criteria. As a result of the RPA no limit for thallium is necessary. • Monitoring frequency for arsenic, selenium and mercury at outfall 003 was increased to weekly during dewatering. • The note for outfall 002 that contained the requirement to use physical -chemical treatment during decanting and dewatering was modified. The installation of physical/chemical treatment is not required unless necessary to meet the water quality standards. • Outfall 006 requirements were modified to reflect the nature of the discharge. This pond discharge is episodic, it only discharges if there is a heavy rain event, therefore limits were implemented as daily maximums. • pH limits were eliminated from internal outfalls. • The flow page for 0.15 MGD for the domestic treatment system (outfall 008) was eliminated since the WWTP was upgraded to 0.25 MGD. • Monitoring for arsenic, mercury, antimony, copper, molybdenum and selenium were added to Outfall 012A due to the contribution from ash basin closure flows and treated groundwater. • The schedule of compliance to meet FGD ELG limits was modified to December 31, 2021. • The Groundwater Monitoring Well Construction and Sampling condition was eliminated. • Special condition A. (28) Compliance Boundary was added to the permit. Groundwater compliance boundary maps were added to the permit as Attachment A and B. Attachment A describes the current compliance boundary and Attachment B describes the compliance boundary once the ash is removed from the East Ash Basin Extension. • Special condition for instream sampling was modified to require monthly sampling, to add sulfides to the list of monitored parameters and to specify the sampling location. • Fish tissue monitoring special condition was modified to clarify requirements. • For clarification the identification of outfall 003 was modified to heated water discharge pond. • The special condition for 316(b) requirements was modified to include a schedule to submit the required information in 122.21(r) by May 31, 2022. 15 NPDES PERMIT FACT SHEET Page 16 Public Notice schedule: Draft permit to Public Notice: Permit Scheduled to issue: Roxboro Steam Electric Plant NPDES No. NC00003425 STATE CONTACT If you have any questions on any of the above information or on the attached permit, please contact - Sergei Chernikov at (919) 707-3606. 16