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HomeMy WebLinkAboutNC0001970_Report_20200402 Draper Aden Associates D [ C 2 p d NZ, Engineering • Su-vexing • Environmental Services 114 Edinburgh South Drive APR - 2 2020 Suite 200 Cary,North Carolina 2751 I 919.827.0864 DIVISION OF WATER RESOURCES www.daa.com DIRECTOR'S OFFICE March 31, 2020 Mr. Danny Smith, Director Division of Water Quality Via email:danny.smith@ncdenr.gov North Carolina Department of Environmental Quality 1617 Mail Service Center Raleigh, North Carolina 27669-1617 Re: 2019 Annual Chloride Reduction Report Bay Valley Foods, LLC—Faison, North Carolina 354 N. Faison Avenue, Faison, North Carolina NPDES Permit No. NC0001970 Draper Aden Associates Project No.: 20080165-010103 Dear Mr. Smith, On behalf of Bay Valley Foods, LLC(Bay Valley), Draper Aden Associates (DAA) is pleased to present 2019 Annual Chloride Reduction Report. In accordance with Special Condition A. (5) b.: NPDES Permit No. NC0001970, Bay Valley Foods, LLC-Faison, NC, continues efforts to study and evaluate chloride removal technologies and chloride reduction strategies. Enclosed please find a copy of the facility's 2019 Annual Chloride Reduction Report. As stated in previous reports,through the 1980's, 1990's and 2000's significant investments were made on process improvements, new equipment purchases, and process change strategies aimed at reducing salt use and subsequent chloride discharges. Notable investments and process changes include the replacement of wooden fermentation tanks, reduction of salt concentration in brines, process automation, and brine recycling technology. The early efforts resulted in substantial reduction in salt use with subsequent focus on pollution prevention efforts further reducing chloride discharges to surface water. As noted in our Chloride Variance Request and previous Annual Chloride Reduction Evaluation Reports,there have been no economically feasible scientific breakthroughs in chloride removal technologies applicable to the production processes employed at Bay Valley Foods, LLC— Faison, NC. Efforts continue to improve process control/automation focused on reducing brine loss and salt waste. If you have any questions or comments, please contact us at 919-582-7271. Sincerely, Draper Aden Associates c.77,9/cr" James Y.Joyner, II, RSM Candy E. Elliott, P.G. Senior Consultant Project Geologist Enclosure cc: Mr. Donovan Brock (1 HC) Blacksburg•Charlottesville•Manassas •Newport News•Richmond• Virginia Beach Fayetteville•Raleigh ANNUAL CHLORIDE REDUCTION EVALUATION REPORT YEAR 2019 Bay Valley Foods, LLC (former Dean Pickle and Specialty Products) NPDES Permit No. NC0001970 DAA Project No.: 20080165-010103 March 30, 2020 Prepared for Bay Valley Foods, LLC 354 N. Faison Avenue Faison, North Carolina 28341 Prepared by Draper Aden Associates 114 Edinburgh South Drive Cary, North Carolina 27511 Draper Aden Associates I:nXineerArk Sirverin,Y l.nru•uunrnral Sen•icrs 3RD PARTY REVIEW This Report has been subjected to technical and quality reviews by: Billy Newcomb, PG March 26, 2020 Name: Printed Signature Date Senior Program Manager Candy Elliott March 30, 2020 Name: Printed Signature Date Project Geologist q74'-7.#vot James Joyner, II, RSM March 30, 2020 Name: Printed Signature Date Quality Reviewer/ Environmental Team Leader TABLE OF CONTENTS 3`d Party Review i Executive Summary ii 1.0 Basic Information 1 2.0 Production 5 3.0 Evaluated and/or Implemented Technologies and Approaches 6 4.0 Technologies &Approaches Considered For 2020 and Beyond 8 4.1 Bypass Salting/No Fermentation Process 8 4.2 Desalt Process Improvements 8 4.3 Brine Reclaim Process Improvement - 5-gallon Pail Line 8 4.4 Wastewater Treatment Process Improvements 8 4.5 Pickle Packers International (PPI) 9 4.6 Treatment Technologies 9 5.0 Waste Reduction 10 TABLES Table 1.0 2019 Chloride Discharge Data 1 Table 2.0 Annual Production Units and Chloride to Production Ratio (1996-2019) ' 2 Table 3.0 Annual Average Stream Chloride Levels 1997-2019 3 Table 4.0 Comparison of All Data 4 CHARTS Chart#1 Average Cl- Discharge per Day (lbs/day) Chart#2 Annual Production (Millions of Equivalent Units Produced) Chart#3 Average Instream Chloride Concentrations (lbs per day) Chart#4 Cl- Discharge per Equivalent Unit (Ibs) Chart#5 Annual Chloride Discharge (lbs/year) Chart#6 2019 Chloride Limits EXECUTIVE SUMMARY This report is being submitted in accordance with Special Condition A. (5) b, which states; "The permittee shall continue to study and evaluate new and emerging chloride removal technologies and reduction methods and shall report its findings directly to the Division of Water Quality annually on or before March 31st of each year." The annual report shall include a summary of findings from a qualified waste reduction specialist employed to specifically evaluate source reduction of chloride." This report will be limited to chloride, chloride discharges and approaches/technologies researched, evaluated, and/or implemented for the reduction of chloride discharges during the calendar year 2019. Comparisons are made to previous years including 1996, the benchmark year. Table 1.0 and Chart#1 summarize annual average chloride discharges in pounds per year. There were no exceedances of either the "Monthly Average Discharge Limit" or the "Daily Maximum Chloride Discharge Limit" in 2019. (Refer to Chart#6) Table 2.0 and Chart# 2 provide annual production information for 2019 and for previous years, measured in equivalent production units (eq. units), as well as the pounds of chloride discharged per equivalent production unit. Production volume in 2019 decreased 11.9% compared to 2018. The 2019 chloride lbs. discharged per production unit ratio decreased 44% from 0.34 in 2018 to 0.19 in 2019. Over the past five years (2015 through 2019), the average chloride lbs. per equivalent unit of production is 0.24 lbs./eq. units. Table 3.0 and Chart#3 summarize the in-stream chloride concentrations at the established monitoring points located both upstream and downstream of the facility's treated process wastewater discharge outfall. Data are provided from 1997, when in-stream chloride concentration monitoring became an NPDES permit requirement. In-stream chloride concentrations at all monitoring locations, including upstream from the facilities wastewater discharge outfall, peaked in 2007 due to an extended drought in the Faison area resulting in low flow in the receiving stream. Increased precipitation in subsequent years has resulted in in-stream sampling data that show a long-term decline in chloride concentrations at all monitoring locations. Chloride concentrations at downstream monitoring location Downstream #1 decreased between 2018 and 2019 and Downstream #2 and Downstream #3 increased. Table 4.0 summarizes data pertinent to chloride discharges from 2005 through 2018. • Bay Valley Foods, LLC - Faison, NC did not exceed the "Daily Maximum Chloride Discharge Limit" or the "Monthly Average Discharge Limit" in 2019. (Refer to Chart#1) • The 2019 annual production total of 4.83 million equivalent production units represents an 11.9% decrease from 2018 production. (Refer to Chart#2) • Chlorides discharged per equivalent production unit in 2019 decreased 44% compared to 2018 and decreased 66% compared to the benchmark year of 1996. In 2019 the ratio was calculated at 0.19 pounds of chlorides discharged per equivalent production unit. (Refer to Chart#4) • The calculated annual pounds of chlorides discharged (903,820 lbs.) in 2019 is 74.8% less than the largest amount discharged in 2007. (Refer to Chart#5) iii 1.0 BASIC INFORMATION Bay Valley Food, LLC— Faison, NC (BVF), remains committed to continue efforts to maintain the downward trend in chloride discharges from its production facility. Through emphasis on its comprehensive pollution prevention; advanced process control and automation aimed at reducing brine loss; replacement of inefficient equipment; and ongoing efforts in the identification and implementation of new and innovative reduction opportunities, BVF maintains its focus on the reduction of chlorides from its waste stream (Refer to Chart#1). BVF will continue to investigate and monitor technological advances that may have potential application to the pickle processing industry and supports research efforts in this area through its membership in professional trade organizations such as Pickle Packers International. BVF is willing to implement cost-effective chloride removal technologies and pollution reduction measures that can be proven effective and not compromise or impair finished product quality and/or characteristics. Table 1.0. 2019 Chloride Discharge Data Monthly Average = 13,476 lb/day Current Chloride Discharge Limits: Daily Maximum = 19,120 lb/day Chloride Discharge (lb/day) Month Max Min Avg. January 3129 12 1140 February 1057 180 794 March 1250 975 1114 April 3211 723 1523 May 6267 829 3635 June 6194 2184 4290 July 8195 2399 4515 August 9992 2176 5094 September 6588 850 2464 October 3004 732 1860 November 1995 163 940 December 3229 863 2135 1 Table 2.0 Annual Production Units and Chloride to Production Ratio (1996-2019) Production Production Year Equivalent Units Chloride to Units (millions) Produced Ratio 1996 5.74 0.51 1997 NA NA 1998 NA NA 1999 7.09 0.42 2000 7.28 0.38 2001 7.59 0.33 2002 7.84 0.37 2003 8.52 0.37 2004 8.75 0.3 2005 7.86 0.35 2006 9.04 0.35 2007 8.98 0.4 2008 8.57 0.38 2009 8.82 0.35 2010 8.23 0.39 2011 7.85 0.25 2012 7.26 0.2 2013 6.82 0.19 2014 6.6 0.21 2015 7.01 0.17 2016 6.84 0.22 2017 5.89 0.26 2018 5.49 0.34 2019 4.83 0.19 NA:data are not available 2 en E a&+ m N l0 N O0 O Ln 6- al O inO O1 o O (.0 m f— y Ol l0 lD Ol f� N V N m Lfl I� LID NLIDLfl N 0 • \ E 01 to Ol N re) O N '- a l�YLC) I- N O V N 1 I- rn N rn '- N O '- m 01 O- in m Q1 N N Lfl m N m N N 0 Q1 01 d f0 J M l0 rn O 'Cl" 00 Ln N 00 m O '- 1� O O N N lD N �+ lfl O Lfl Ol in N lO lO N- O M CO N O CO N re) "0 C N- Ol lD LO N- N m N lfl N O � Ol dl N Ln M m - V N Lfl O t p E m as H E ai 1a 171 L -. , m N L l O O N m N- L0 00 m Ol N L l o V Ol m m to N Ol N N N N rn N N N N ff N rn rn N l0 N N N N '- N N O. 10 C C N- co Ol O N m V Lfl LD N CO Ol O - N M V Lfl lO N- 00 Ol 0 f0 Ol Ol Ol O O O O O 00 O O O M a/ Ol Cr) Cl O O O O O O O 0 0 0 0 0 0 0 0 0 0 0 0 0 N N N N N N N N N N N N N N N N N N N N al fa H Table 4.0. Comparison of All Data (2005-2019) Data Description 2005 2006 2007 2008 2009 2010 2011 2012 2013 2014 2015 2016 2017 2018 2019 Annual Chloride Discharge 2,731,749 3,133,189 3,588,806 3,250,525 3,090,730 3,193,908 1,962,923 1,464,092 1,273,754 1,418,341 1,218,420 1,497,130 1,542,683 1,869,489 903,820 (Ibs) Annual Production 8,234,700 9,039,500 8,981,990 8,572,000 8,821,135 8,226,346 7,846,314 7,258,154 6,816,632 6,602,658 7,012,627 6,837,706 5,896,035 5,486,941 4,834,657 (Equivalent Units) Chloride Per Equivalent Unit 0.33 0.35 0.40 0.38 0.35 0.39 0.25 0.2 0.19 0.21 0.17 0.22 0.26 0.34 0.19 Annual Water Use 119.2 98.03 109.11 94.3 101.78 107.7 115.32 97.6 91.61 114.47 133.6 133.77 114.29 118.23 92.34 (MG) Annual NaCI &CaCI Purchases 4,409,000 4,929,000 6,652,000 6,104,000 4,913,000 4,020,000 1,998,000 3,702,000 3,805,000 3,228,325 2,603,393 4,259,319 6,471,116 6,578,677 3,027,909 (Ibs) Salt Use Per Equivalent Unit 0.54 0.55 0.74 0.71 0.56 0.49 0.25 0.51 0.56 0.49 0.37 0.62 1.1 1.2 0.63 4 2.0 PRODUCTION Bay Valley Foods, LLC - Faison, NC uses an established formula whereby all production types, in all facilities, are normalized. The unit of measure is referred to as an "Equivalent Production Unit" and allows for a fair and equal comparison of differing sized containers from 10-ounce jars to 5-gallon bucket. The equivalent production unit brings all production to a case equivalent volume and enables a fair comparison of production between facilities and production years and provides a balanced method to evaluate performance. The Faison, NC facility production requirements increased annually between the benchmark year of 1996 and 2006, at which time production peaked at 9.04 million eq. units. Since 2006, the trend indicates a reduction in production throughput (Refer to Chart#2). The 2019 production volume was 4.834 million eq. units, a 6.9% decrease from the 2018 volume (5.487 million eq. units). The 2019 average ratio of chloride discharged in pounds per equivalent production units (0.19) is below the 1996 — 2019 average ratio (0.32) and below the 2015 - 2019 five-year average ratio (0.24). Due to the ongoing commitment from facility leadership, the pounds of chloride discharged per equivalent production unit continue to show a long-term downward trend (Refer to Chart#3). 5 3.0 EVALUATED AND/OR IMPLEMENTED TECHNOLOGIES AND APPROACHES Summary of Chloride Reduction Strategies Implemented and/or Evaluated at Faison, NC • 1982 through 1990— Replace all wood fermentation tanks with fiberglass or plastic; • 1982 through 1994—Salt Use Reduction in Brining - %salt reduced from 15.8%to 6.3% salt; (Substitute calcium chloride and acetic acid in brine prep) • 1987 to 1989— Recycle Brine—Currently recycle 100%of brine; • 1988 — Desalting Operation Moved to Brine Yard; • 1991 — Enhanced Automation of 5-Gallon Production Line; • 1991 — Enhanced Automation of Major Customer Brine System; • 1992 — Replace Open-Top Blancher with Rotary Blancher; • 1992 — Enhanced Bulk Product Handling Processes; • 1993 — Upgrade Brine-making Station; • 1993 — Replace Brine Yard Pickle Pump; • 1994— Install Titanium Heat Exchanger— Brine Recycling/Pasteurization Process; • 2002- Increase Brine Reclaim; • 2003, 2004, 2005, 2006 —Evaluate Use of De-Salt Water for Brining and/or Product Fluming; • 2003, 2004, 2005, 2006—Evaluate Use of De-Salt Water for Subsequent De-Salting Operations; • 2003, 2004— Evaluate Recovery of Bottom 2-inches of Concentrated Brine Left in Fermentation Tanks After Cleaning; • 2004— Install De-Salt Flume Conveyor; • 2004— Evaluate De-Salt Brine Filtering for Possible Reuse; • 2004, 2005 — Evaluate De-Salting through the Lyco Blancher (Continuous Process vs. Batch Process); • 2004, 2005 — Evaluate Rapid De-Salt Process; • 2005, 2006— Evaluate Improvement in Cover Brine Recovery/Blow Lines; • 2005 — Evaluate New De-Salting Operation Located in Tank Yard; • 2005 — Install WW Sludge Filter Press and Clean Sludge from WW Treatment Ponds; • 2005, 2006, 2007, 2008 — Evaluate In-Line De-Salting; • 2005 — Implemented By-Pass Salting / No Fermentation Process; • 2005 (2006, 2007, 2008 2009)— Begin 4-Phase Storm Water Management Project; • 2007, 2008 — Improvements to Cover Brine Efficiency& Recovery Line 1 and 2; • 2008— Implemented Enhanced Relish Desalting Control; • 2009—Implemented Replace Pickle Conveyor Pump; • 2009— Implemented Upgrade Desalting Operation by Installing Four Additional De-Salt Tanks; • 2011 —Implemented a project to remove excess biomass from Pond 1 of its wastewater treatment system. 1500 tons of biomass was dewatered and removed at a cost of$143,000. • 2012 —Continued the removal process of excess biomass from Pond 1 with an additional removal and dewatering of 3000 ton at a cost of$249,000. • 2014 - Continued the removal process of excess biomass from Pond 1 with an additional removal and dewatering of 3643 ton at a cost of$368,000. 6 ♦ 2016 - Implemented removal process of excess biomass from Pond 2 with removal and dewatering of 3727 tons at a cost of $230,000. ♦ 2016 — Implemented removal and replacement of Pond 2 liner and begin construction and lining of Pond 3 at a cost of$500,000. ♦ 2016— Evaluate Reverse Osmosis and Electrodialysis/Electrodialysis Reversal to Reduce Chloride at End-of-Pipe. Neither technology was considered feasible due to cost considerations. ♦ 2017 —Completed the excess biomass removal from Pond 3 with removal and dewatering of 1,963 tons at a cost of$336,000. ♦ 2017 —Completed installing the new liner at Pond 3 on April 1, 2017 at a cost of $100,000 ♦ 2018 —Completed lining Pond 1. Sludge removal cost totaled $285,000.The three ponds have been relined. 7 4.0 TECHNOLOGIES & APPROACHES CONSIDERED FOR 2020 AND BEYOND Many projects, programs, process changes and chloride reduction strategies implemented in the past continue to be utilized into 2019, such as: 4.1 Bypass Salting/No Fermentation Process The proprietary "No Fermentation" process continues to be a significant process improvement and chloride reduction strategy and will be considered for all future production opportunities where applicable. 4.2 Desalt Process Improvements The Faison facility added four portable de-salt tanks for product de-salting. The de-salting process must be accomplished quickly to support the production schedule, which can result in over de-salting of the product necessitating the re-addition of salt. The result is excess water use, increased salt use and ultimately additional chloride discharges. The four portable de-salt tanks enabled the facility to extend the duration of the de-salt process, which provided improved process control. Status: Successful process improvements were made to the de-salt process in 2009. Cost Associated with Improvements - $350,000. 4.3 Brine Reclaim Process Improvement - 5-gallon Pail Line The installation of catch pans, filter screens, and a brine reclaim tank on the 5-gallon pail line allows for the capture of overflow brine and eventual reuse, rather than discharged as high chloride concentrated wastewater. Status: Successful improvements were made to the brine reclaim system on the 5-gallon pail processing line in 2009. Cost Associated with Improvements - $4,500. 4.4 Wastewater Treatment Process Improvements Excess biomass accumulation in Pond 3 was removed and the pond was relined. This project was completed in April 2017. In 2017, Bay Valley Foods removed biomass accumulation from Pond 1 and 8 began the process to reline Pond 1. Sludge removal was completed in March 2018, and the liner replacement was completed. Pond 1 aerators were re-wired, and the pond was returned to normal operations on May 1, 2018. Status: Successful improvements were made to the wastewater ponds. Sludge removal costs - $285,000. 4.5 Pickle Packers International (PPI) Bay Valley Foods is a member of, and continues to participate in, the Pickle Packers International organization. Through participation in this organization, Bay Valley Foods remains current on new processing technologies which may include reduced salt use, and wastewater treatment strategies others in the pickle processing industry may have implemented that result in reduced chlorides in wastewater discharges. 4.6 Treatment Technologies Ramboll Environ prepared a Chloride Removal Technology Evaluation Report dated January 12, 2017. The report identified several technologies potentially applicable to the BV-Faison facility. The technologies included reverse osmosis, electrodialysis/electrodialysis reversal, chemical precipitation, product substitution, flow augmentation, and residuals management. Bay Valley Foods, LLC is committed to investigating and evaluating any new treatment technology based on technical applicability and feasibility. 9 5.0 WASTE REDUCTION The ongoing waste reduction efforts at the Facility will continue through 2020. The facility has formed a cross-functional Pollution Prevention Team which meets on a regular basis to discuss and evaluate waste generation and chloride reduction opportunities. A comprehensive pollution prevention program is in place which includes educating employees regarding best waste management practices and the importance of identifying strategies that can reduce chloride discharges. Chloride reduction is a primary focus of the Team along with water conservation, efficient utilization of energy, and waste generation. In addition, the Team considers maintenance practices and other protocols that may result in brine loss. Finally, the Team is continually evaluating processes for redesign consideration with respect to improved efficiency and chloride discharge reduction opportunities. In combination with waste reduction and pollution prevention efforts, Bay Valley Foods, LLC - Faison, NC continues to focus on preventive maintenance programs and giving a priority assignment to any maintenance work order involving process equipment that could result in increased discharge of chlorides. These activities along with employee training help foster and expand a work ethic focused on waste reduction as well as process improvements. The maximum daily discharge for each month in 2019 were below the daily maximum limits and the average monthly discharge was below the monthly average limit (Table#1 and Chart#6). Upstream chloride concentrations represent background values. An anomalous peak in downstream chloride concentrations observed in 2007 was attributed to low stream flow conditions throughout the year, a result of drought conditions. Linear regressions performed on chloride stream concentrations indicate decreasing trends in Downstream Point#1 and Downstream Point#3, and an increasing trend in Downstream Point#2. While long-term concentrations are decreasing in Downstream Points #1 and #3, analysis of the past five years (2015 — 2019) indicate increasing concentrations in Downstream Point #1. Chart#5 shows that the average annual chloride discharge decreased from 2007 to 2019. From 2015 to 2019, the concentrations have fluctuated, but have remained lower than the 2007 chloride concentrations. The provided charts demonstrate that waste reduction efforts at the BVF facility are effective. 10 Charts Chart #1 Average Cl- Discharge per Day (lbs/day) 12,000 10,000 8,000 6,000 4,000 ‘114111111111111111111111V - 111114111111111k 2,000 0 2004 2005 2006 2007 2008 2009 2010 2011 2012 2013 2014 2015 2016 2017 2018 2019 Chart #2 Annual Production (Millions of Equivalent Units Produced) 10.000 9.000 - 8.000 1.1111.1111111111 7.000 - �r 6.000 - ♦ 5.000 4.000 - 3.000 1996 1997 1998 1999 2000 2001 2002 2003 2004 2005 2006 2007 2008 2009 2010 2011 2012 2013 2014 2015 2016 2017 2018 2019 Chart#3 Average Instream Chloride Concentration (lbs per day) 2500 -- — ---- - ° Upstream (Background) - o Downstream Point#1 ❑ Downstream Point#2 o Downstream Point#3 2000 Linear(Downstream Point#1) ----Linear(Downstream Point#2) — — Linear(Downstream Point#3) 1500 _ 1000 - >13A\ - - 500 0 0 Ts 95 0 a ® e ® a e ° e ° a °---4-8 ° , 1996 1997 1998 1999 2000 2001 2002 2003 2004 2005 2006 2007 2008 2009 2010 2011 2012 2013 2014 2015 2016 2017 2018 2019 Chart #4 Cl- Discharged per Equivalent Unit (Ibs) 0.60 - • 0.50 0.40 r 0.30 IPP .41111kik 0.20 0.10 0.00 1996 1997 1998 1999 2000 2001 2002 2003 2004 2005 2006 2007 2008 2009 2010 2011 2012 2013 2014 2015 2016 2017 2018 2019 Chart #5 Annual Chloride Discharge (lbs/year) 4,000,000 3,500,000 3,000,000 2,500,000 2,000,000 1,500,000 1,000,000 500,000 0 1999 2000 2001 2002 2003 2004 2005 2006 2007 2008 2009 2010 2011 2012 2013 2014 2015 2016 2017 2018 2019 Chart #6 2019 Chloride Limits 30,000 _ —•—Average CL-lbs./day —is—Max Daily Cl- Lbs. 25,000 20,000 Max Daily Limit 19,120 lbs 15,000 - Monthly Avg Limit 13,476 lbs 10,000 5;000 11A\N 0 January February March April May June July August September October November December