HomeMy WebLinkAboutNC0020389_Compliance Evaluation Inspection_20200224 Y
a
ROY COOPER
Governor
MICHAEL S.REGAN
Secretary
S.DANIEL SMITH NORTH CAROLINA
Director Environmental Quality
February 24. 2020
Fredrick D. Nelson, Town Manager
Town of Benson
303 E. Church Street
Benson, NC 27504
Subject: Compliance Evaluation Inspection
Benson WWTP
NPDES Permit NCO020389
Johnston County
Dear Mr. Nelson,
On Monday, February 17, 2020, Zaeh Thomas and Jason Robinson of the Raleigh Regional
Office of the Division of Water Resources conducted a compliance evaluation inspection of tile
treatment facilities located at the Benson WWTP. The purpose of this inspection was to ensure
compliance with the subject NPDES permit. During the inspection. the presence and
cooperation of Brian Leavitt, Operator in Responsible Charge (ORC). Tim Robbins (Director of
PU), Steve Procter(BUORC & Lab Supervisor). Brian Gay and other staff was helpful and
appreciated.
The Benson WWTP is located at 770 Hannah Creek Road. Four Oaks, North Carolina. The
WW-4 facility is permitted and authorized to discharge 1.9 MGD of treated wastewater through
Outfall 001 into Hannah Creek. classified C-NSW, as part of the Neuse River Basin.
This NPDES compliance evaluation inspection consisted of the following:
• Review of the NPDES permit;
• Review of the owner/facility information;
• Review of ORC log books and other operation documents:
• Review of August 2018- January 2020 monitoring data;
• Review of August 2018—January 2020 compliance history;
• On-site inspection of the laboratory;
• On-site inspection of the wastewater treatment units.
Findings during the inspection were as follows:
I. The current NPDES permit was issued effective on September 1, 2013, and expired on April 30,
2018. A copy was available on-site. The Division received the permit renewal application for the
facility on September 18, 2017 and is currently under review,
M ,,A
North Carolina Department of Environmental Quality I Division of Water Resources
_ Raleigh Regional Offi,e 13800 Barrett Drive I Raleigh.North Carolina 27bO9
919.7914200
2. As listed in the subject permit, the treatment components include: one(I)are bar screen, grit removal
system,dual manual bar screens, parshall flume with flow measurement, influent composite sampler,
three(3) influent screw pumps,three(3)oxidation ditches(Ditches #1 & #3 are used for aeration and
ditch#2 is kept anoxic for nutrient removal), five(5)secondary clarifiers,a return and waste sludge
pump station, five(5)tertiary filters, a chlorine contact basin (changed from gas to liquid since last
inspection), a dechlorination basin with post aeration, an effluent flow meter(used for reporting;),
effluent composite sampler, one(1) concrete lined sludge lagoon(not currently aerated), and two(2)
stabilization lagoons/influent flow storage,and backup generator. Chemical feed systems(alum and
lime)are no longer used in treatment process.
3. For the review period August 2018—January 2020, DMR violations and enforcement actions
(Notices of Deficiency,Notices of Violation, or Civil Penalty Assessments)were issued. These
actions were handled in separate correspondence. During this inspection, DWR staff also evaluated
whether the remediation efforts requested from last inspection were performed. Many improvements
were made to the facility and are detailed in item t•7 below.
'I. The inspector compared February 2019 and July 2019 DMR data against the bench and analytical
data. No discrepancies were noted. For the review period, Benson WWTP has been compliant with
its Whole Effluent Toxicity limit and monitoring requirements(July 2019 results indicated a"fail",
samples were collected the two following months and results indicated a"pass''.).
5. The laboratory at Benson WWTP operates under field certification#196 and analyzes the following
parameters: pl-1, temperature, dissolved oxygen, chlorine,TP, TSS, local coliform, and conductivity.
All other parameters are analyzed by Environment I or Meritech Inc. A brief inspection of the meter
calibration logs and standards showed the Benson WWTP laboratory to be compliant with record-
keeping;requirements. Disposable NISI certified thermometers, which are good for I year, are used
by the operators to measure temperature.
6. The ORC logbook was complete and contained detailed information that included daily clarifier
sludge levels, freeboard levels,etc. The 2019 Annual Report was provided and is available as of
January 2020 for review on the Town's website in addition to being posted at Town Mall.
7. The following treatment units.were evaluated during this inspection:
a) Arc/manual bar screens: Debris is collected in a rolling;trash bin, then placed in a dumpster and
picked up by waste management. The ORC has implemented a higher frequency of observation to
mitigate issues. During;the inspection,the chain inside of the unit came undone and was attended
to immediately. The unit is noticeably older, rusted, and staff expressed a want to replace the
entire arc bar unit to increase efficiency.
b) Grit removal system: The unit«as offline and actively being rehabbed on the day of inspection.
It was scheduled to be brought back online that afternoon. Repairs were made to the concrete
floor and walls,surfaces of unit and motor were painted and coated to help prevent breakdown.
Please notify this office tit-hen the writ is filly brought hack online.
c) Influent flow meter& sampler: The influent flow meter was last calibrated 8-30-2019 by
Clearwater. The sampler temperature was noted as 3.1 degrees Celsius. The previous inspection
noted that samples were being collected at a rate that did not meet permit requirements. The
sampler is now set to collect 120 mL samples and is flow proportional.
d) Screw pumps: 2 of the 3 screw pumps .vere in operation. The other scree pumps motor was to
be replaced and staff are waiting on the part to arrive. Please not f►,this office when the third
screir pump is brought back online.
e) Oxidation ditches: Ditches#1 & #3 are used for aeration and Ditch #2 is kept anoxic for nutrient
removal. The previous inspection noted that multiple rotors were inoperable. Rotor#1 in Ditch
#1 has been rehabbed. Concrete has been repaired and the motor has been replaced. An
electrical part is on order and will be installed shortly after to bring the rotor back online. All
other rotors appeared to be in working order; Ditch 92 did not have any rotors running due to it
being the designated anoxic zone.
f) Clarifiers: The previous inspection revealed only 3 of the 5 clarifiers were operable. Repairs
have been made and now all five clarifiers are in good working order. Sludge blankets are
measured and documented once per day and more frequently under inclement weather. Blanket
levels appeared to be compliant. Of the 5 clarifiers, 2 are 10 ft. in depth, 2 are 12 ft. in depth and
the larger is 1511. in depth. Algae is cleaned from the weirs weekly or as needed and placed in the
sludge wasting pit to be sent to the sludge holding lagoon.
g) Sludge Pump Station: New pumps and electrical equipment were added or replaced in the pump
house to better regulate flow to the different treatment units and the lagoon.
h) Tertiary Filters: The previous inspection revealed that only 3 of the 5 filters were operable.
Repairs have been made and 4 of 5 are back online. The 5"' filter contains broken plates that are
no longer manufactured. Staff are looking into best options for bringing this unit back online.
All operable filters are backwashed on NI, W, F or as needed and appeared to be operating
sufficiently.
i) Disinfection: Per the ORC,the plant has changed from using gas to liquid sodium hypochlorite
after discussing the change with Central Office staff. Waterguard is scheduled to supply material
every two weeks. The facility keeps a powder mix as a back-up. Estimated contact time in the
chamber is 30 minutes.
j) De-chlorination and post aeration: Calcium thiosulfate is added and the effluent is post aerated
by units from the bottom of the chamber. Waterguard also supplies this material.
k) Effluent flow meter& sampler: The effluent flow meter is used for reporting and was last
calibrated 8-30-2019 by Clearwater. The meter display showed 1.88 MGD at approximately
1 1:40 AM. The sampler temperature was noted as 3.0 degrees Celsius. The previous inspection
noted that samples were being collected at a rate that did not meet permit requirements. The
sampler is now set to collect 120 rnL samples and is flow proportional.
1) Standby Power: The generator on site is equipped to provide power for the entire plant. The unit
is manually tested. The ORC stated that it has been several months since a test was last
performed. D1PR staff reconuireilded testirtg7rttto-te.stiiig the generator on a regular basis and
periodically under load 6virh crppropricrre clactopienlation) to ensure that it will ftoiction properly:
when necessctrj�
rm) Treatment lagoons: The facility contains three(3) lagoons. Lagoon I is the larger lagoon
located on the SW side of the plant. It is clay lined with a concrete curtain and is used as an
equalization basin (flow is diverted from the headworks unit). Lagoon 2 is the smaller lagoon
located on the SE side of plant. It is clay lined with a concrete curtain and is also used as an
equalization basin. The third lagoon is completely concrete and is used as sludge waste
containment with a capacity of approximately 3MG. It contains aerators, but are currently not in
use until more sludge can be removed. A previous inspection revealed an overflow that occurred
from the sludge lagoon, high freeboard levels,and excessive amounts of vegetation growing
inside of the units; this resulted in PC-2018-0019. Sludge has since been extracted from the
lagoons and cleanup efforts have been performed. Staff stated that approximately 1500 tons of
sludge and vegetation have been removed from Lagoon #2. In addition, debris and sludge has
been removed from the sludge wasting lagoon itself. Facility staff stated that they anticipate
another round of debris removal from the lagoons in the coming months. Freeboard levels in
both EQ basins are checked daily and documented. At the time of inspection, freeboard levels in
the sludge lagoon were compliant. Please describe the location cued process in tivhichfcrcifY stuff
checkft•eebocu•d levels daily to ensure comj)ha rce ivith the?fool fi•eebocrrd requirements Stated
in A. (6). of the issued permit.
8. The inspector observed the effluent discharge to Hannah's Creek via the outfall pipe to be clear with
no observable solids or foam. No detrimental impacts from the effluent discharge were observed.
The area around the outfall pipe was clear and accessible. It appears to have a ''Y-split''and
discharges from two separate outlets in the same location. Please verify this crud describe location af'
split.
9. The ORC and Public Utility Director stated that in addition to the cleanup of the lagoons, repair of the
rotors inside of the oxidation ditches and maintenance/replacement of'screen units are a top priority.
Prioritizing these items will help ensure efficiency, help prevent damage to downstream units, and
protect the Town's recent investments at the treatment facility.
Please address the conditions outlined in numbers 7 (b, d, c, 1, m) & 8 of this letter and
notify the inspector at the contact information below within 45 days of receipt of this letter.
If you have questions or comments about the inspection, this report or the requirements to take
corrective action (if applicable),please contact:
Zach Thomas at 919-791-4247 or via email at zacharn.thonias a ncdenr.aov.
Sincerely,
Scott Vinson
Regional Supervisor
Water Quality Regional Operations Section
Raleigh Regional Office
Division of Water Resources, NCDEQ
Attachments: EPA Water Compliance Inspection Report
Cc: Brian Leavitt, ORC (via email: bleaN itt et to«nofbenson.coni)
Tim Robbins, Public Utilities Director(via email: trobbins-a to«notbenson.com)
RRO Files
Laserliche
Uniled States Environmental Protect'. n Agen.y
Form Approved.
EPA Washmgtan 0 C 20460 OMB No 204MO57
Water Compliance Inspection Report Approval expires 8-31-98
Section A:National Data System Coding(i.e..PCS)
Transaction Code NPDES yrrmolday Inspection Type Inspector Fac Type
' U 2 u 3 1 NC0020389 11 121 20102:17 I17 18 [1 c` 19 I LJ L! I 201J
21L_Ll J 6
Inspection Work Days Facility Self-Monitoring Evaluation Rating B1 oA ••-• Reserved
67 70 L—I 71 t J 72 u ) 73 !74 751 I I I I I I80
Section B:Facility Data
L
Name and Location of Facility Inspected(For industrial Users discharging to POTW.also inc3udo Entry Time/Dale Perm I Effective Date
POTW name and NPDES Permit Number) 10 00AM 20/02/17 13/09/01
Benson WWTP
770 Hannah Creek Rd Exit TimofDate Permit Expiration Date
Benson NC 27504 12 15PM 20/02/17 18104-30
Name(s)of Onsile Representative(s)1Tittes(s)IPhone and Fax Number(s) Other Facility Data
111
Brian Peter Leavitt/ORC1919-894-2373/
Name,Address of Responsible Ol6ciallTitlelPhone and Fax Number
Keith Ryker Langdon,PO Box 69 Benson NC 2750400691Town Ccntacled
Manager191 9-894-4 953191 9894 1 28 3 No
Section C:Areas Evaluated During Inspection(Check only those areas evaluated)
Permit N Flow Measurement Operations&Maintenance Records/Reports
Self-Monitoring Program Sludge Handling Disposal Facility Site Review i Compliance Schedules
Ef(IuentlReceiving Waters Laboratory
Section D:Summary of Finding/Comments(Attach additional sheets of narrative and checklists as necessary)
(See attachment summary)
Name(s)and Signature of I`nssppector s) 4 Agency/Office/Phone and Fax Numbers Date
Jason T Robinson 4 ! ✓r- DWRIRRO WOI919-791-42001
Zachary ThomasDWRIRRO Wo1919-791.42001 fj L'{-il"`f
Signature of M nagement 0 A Reviewer Agency/Office/Phone and Fax Numbers Date
y120 20
EPA Form 3560-3(Rev 9-94)Previous editions are obsolete.
Page# 1
NPOES yrlmolday Inspection Type 1
31 NCO020389 11 1 12+ 20102/17 117 18 1 C 1
Section D:Summary ofl Find ing/Comments(Attach additional sheets of narrative and checklists as necessary)
Please see report for details.
f>ageN 2
Permit: NCO020389 Owner-Facility: Benson WWTP
Inspection Date: 021M2020 Inspection Type: Compliance Evaluation
Compliance Schedules Yes No NA NE
Is there a compliance schedule for this facility? ❑ ❑ ❑ a
Is the facility compliant with the permit and conditions for the review period'? 0 ❑ ❑ ❑
Comment:
Permit Yes No NA NE
(If the present permit expires in 6 months or less). Has the permittee submitted a new 0 ❑ ❑ ❑
application?
Is the facility as described in the permit? ■ ❑ ❑ ❑
#Are there any special conditions for the permit? ❑ 0 ❑ ❑
Is access to the plant site restricted to the general public? M ❑ ❑ ❑
Is the inspector granted access to all areas for inspection? 0 ❑ ❑ ❑
Comment: The Division received the permit renewal application for the facility on September 18, 2017
and is currently under review.
Record Keepina Yes No NA NE
Are records kept and maintained as required by the permit? M ❑ ❑ ❑
Is all required information readily available, complete and current? 0 ❑ ❑ ❑
Are all records maintained for 3 years(tab, reg. required 5 years)? 0 ❑ ❑ ❑
Are analytical results consistent with data reported on DMRs? 0 ❑ ❑ ❑
Is the chain-of-custody complete? Cl ❑ ❑
Dates, limes and location of sampling ❑
Name of individual performing the sampling ❑
Results of analysis and calibration ❑
Dates of analysis ❑
Name of person performing analyses ❑
Transported COCs ❑
Are DMRs complete:do they include all permit parameters? a ❑ ❑ ❑
Has the facility submitted its annual compliance report to users and DWQ? 0 ❑ ❑ ❑
(If the facility is=or> 5 MGD permitted flow)Do they operate 2417 with a certified operator ❑ ❑ M ❑
on each shift?
Is the ORC visitation log available and current? ❑ ❑ ❑
Is the ORC certified at grade equal to or higher than the facility classification? ❑ ❑ Cl
Is the backup operator certified at one grade less or greater than the facility classification? ❑ ❑ ❑
Is a copy of the current NPDES permit available on site? ❑ ❑ ❑
Page# 3
Permit: NCO020389 Owner-Facility: Ronson WWTP
Inspection Date: 02/17/2020 Inspection Type: Compliance Evaluation
Record Keeping Yes No NA NE
Facility has copy of previous year's Annual Report on file for review? No ❑ ❑
Comment
Operations & Maintenance Yes No NA NE
Is the plant generally clean with acceptable housekeeping? 0 ❑ ❑ ❑
Does the facil.ty analyze process control parameters,for ex:MLSS, MCRT, Settleable ❑ ❑ ❑
Solids, pH,DO,Sludge Judge,and other that are applicable?
Comment:
Laboratory Yes No NA NE
Are field parameters performed by certified personnel or laboratory? M ❑ ❑ ❑
Are all other parameters(excluding field parameters)performed by a certified lab? M ❑ ❑ ❑
#Is the facility using a contract lab? a ❑ ❑ ❑
#Is proper temperature set for sample storage(kept at less than or equal to 6.0 degrees 0 ❑ ❑ ❑
Celsius)?
Incubator(Fecal Coliform)set to 44.5 degrees Celsius+/_0.2 degrees? a ❑ ❑ ❑
Incubator(BOD)set to 20.0 degrees Celsius+1- 1.0 degrees? ❑ ❑ M ❑
Comment: Field Cert# 1969 some parameters are analyzed by Environment 1 or Meritech.
Influent Sampling Yes No NA NE
#Is composite sampling flow proportional? 0 ❑ ❑ ❑
Is sample collected above side streams? M ❑ ❑ ❑
Is proper volume collected? 8 ❑ ❑ ❑
Is the tubing clean? 0 ❑ ❑ ❑
#Is proper temperature set for sample storage(kept at less than or equal to 6.0 degrees M ❑ ❑ ❑
Celsius)?
Is sampling performed according to the permit? ❑ ❑ ❑
Comment: The sampler temperature was noted as 3.1 decirees Celsius.
Flow Measurement - Influent Yes No NA NE
#Is Flow meter used for reporting? ❑ M ❑ ❑
Is flow metcr calibratcd annually? M ❑ ❑ ❑
Is the flow meter operational? o ❑ ❑ ❑
(if units are separated)Does the chart recorder match the flow meter? ❑ ❑ M ❑
f age# 4
Permit: NCO020389 Owner-Facility: Berison WWTP
Inspection Date: 02117.-2020 Inspection Type: Compliance Evaluation
Flow Measurement-Influent Yes No NA NE
Comment. The influent flow meter was last calibrated 8-30-2019 by Clearwater.
Bar Screens Yes No NA NE
Type of bar screen
a.Manual
b.Mechanical
Are the bars adequately screening debris? M ❑ ❑ ❑
Is the screen free of excessive debris? 0 ❑ ❑ ❑
Is disposal of screening in compliance? 0 ❑ ❑ ❑
Is the unit in good condition? 0 ❑ ❑ ❑
Comment: Debris is collected in a rolling trash bin,then iced in a dumpster and picked up by waste
management.
The ORC has imalemented_a_higher frequency of observation to mitigate issues.
During the inspection, the chain inside of the unit came undone and was attended to
immediately.
The unit is noticeably older, rusted, and staff expressed a want to replace the entire arc bar
unit to increase efficiency.
Grit Removal Yes No NA NE
Type of grit removal
a.Manual ❑
b.Mechanical
Is the grit free of excessive organic matter? ❑ ❑ ❑ ■
Is the grit free of excessive odor? ❑ ❑ ❑ a
#Is disposal of grit in compliance? ■ ❑ ❑ ❑
Comment: The unit was offline and actively being rehabbed on the day of inspection. It was scheduled
to be brought back online that afternoon. Repairs were made to the concrete floor and
walls, surfaces of unit and motor were painted and coated to help prevent breakdown. Staff
is to notify DWR when brought back online.
Equalization Basins Yes No NA NE
Is the basin aerated? ❑ ❑ 0 ❑
Is the basin free of bypass lines or structures to the natural environment? ❑ ❑ ❑
Is the basin free of excessive grease? 0 ❑ ❑ ❑
Are all pumps present? M ❑ ❑ ❑
Are all pumps operable? 0 ❑ ❑ ❑
Are float controls operable? ❑ ❑ ❑
Page# 5
Permit.' NCO020389 Owner-Facility: Benson W WTP
Inspection Date: 0 211 712 02 0 Inspection Type: Compliance Evaluation
Equalization Basins Yes No NA NE
Are audible and visual alarms operable? ❑ ❑ ❑ 0
#Is basin size/volume adequate? M ❑ ❑ ❑
Comment: Freeboard levels in both EQ basins are checked daily and documented. Staff are to
describe location and process in which freeboard levels are checked to ensure permit
compliance. See report for more details.
Lagoons Yes No NA NE
Type of lagoons? Facultative
#Number of lagoons in operation at time of visit? 3
Are lagoons operated in? Parallel
#Is a re-circulation line present? M ❑ ❑ ❑
Is lagoon free of excessive floating materials? ■ ❑ ❑ ❑
#Are baffles between ponds or effluent baffles adjustable? ❑ ❑ IN ❑
Are dike slopes clear of woody vegetation? 0 ❑ ❑ ❑
Are weeds controlled around the edge of the lagoon? 0 ❑ ❑ ❑
Are dikes free of seepage? ■ ❑ ❑ ❑
Are dikes free of erosion? M ❑ ❑ ❑
Are dikes free of burrowing animals? ❑ ❑ ❑
#Has the sludge blanket in the lagoon(s)been measured periodically in multiple ❑ ❑ ❑
locations?
#If excessive algae is present, has barley straw been used to help control the growth? ❑ ❑ E ❑
Is the lagoon surface free of weeds? 0 ❑ ❑ ❑
Is the lagoon free of short circuiting? M ❑ ❑ ❑
Comment: An evaluation of the lagoon depths was performed on 4-23-2019._
Grass area along edge is well maintained.
See report for more details.
Aerobic Digester Yes No NA NE
Is the capacity adequate? a ❑ ❑ ❑
Is the mixing adequate? ❑ ❑ M ❑
Is the site free of excessive foaming in the tank? 0 ❑ ❑ ❑
#Is the odor acceptable? M ❑ ❑ ❑
#Is tankage available for properly waste sludge? ❑ ❑ ❑
Comment:
Permit: NC0420jag Owner-Facility: S"son WWTP
Inspection Date: 02l17r2020 Inspection Type: Compliance Evaluation
Secondary Clarifier Yes No NA NE
Is the clarifier free of black and odorous wastewater? M ❑ ❑ ❑
Is the site free of excessive buildup of sol ds in center well of circular clarifier? M ❑ ❑ ❑
Are weirs level? 0 ❑ ❑ ❑
Is the site free of weir blockage? 0 ❑ ❑ ❑
Is the site free of evidence of short-circuiting? 0 ❑ ❑ ❑
Is scum removal adequate? 0 ❑ ❑ ❑
Is the site free of excessive floating sludge? N ❑ ❑ ❑
Is the drive unit operational? 0 ❑ ❑ Cl
I's the return rate acceptable(low turbulence)? 0 ❑ ❑ ❑
Is the overflow clear of excessive solids?pin floc? ❑ ❑ ❑
Is the sludge blanket level acceptable?(Approximately ,of the sidewall depth) ❑ ❑ ❑
Comment: All five clarifiers are in good working order, Sludge blankets are measured once Per day and
more frequently under inclement weather. Blanket levels appeared to be compliant. Of the
5 clarifiers 2 are 10 ft. in de th 2 are 12 ft. in depth and the larger is 15ft. in depth. Algae is
cleaned from the weirs weekly or as needed and placed in the sludge wasting it to be sent
to the sludge holding lagoon.
Oxidation Ditches Yes No NA NE
Are the aerators operational? M ❑ ❑ ❑
Are the aerators free of excessive solids build up? 0 ❑ ❑ ❑
#Is the foam the proper color for the treatment process? 0 0 ❑ ❑
Does the foam cover less than 25%of the basin's surface? ❑ ❑ ❑
Is the DO level acceptable? ❑ ❑ ❑
Are seltleometer results acceptable(> 30 minutes)? ❑ ❑ ❑ 0
Is the DO level acceptable?(1.0 to 3.0 mg11) ■ ❑
Are settelometer results acceptable?(400 to 800 mill in 30 minutes) ❑ ❑ ❑
Comment: Rotor#1 in Ditch#1 has been rehabbed. Concrete has been repaired and the motor has
been replaced. An electrical part is on order and staff is to notify DWR when it is back
online. All other rotors a0peared to be in working order,• Ditch#2 did not have any rotors
running due to it being the designated anoxic zone.
Nutrient Removal Yes No NA NE
#Is total nitrogen removal required? M ❑ ❑ ❑
#Is total phosphorous removal required? 0 ❑ ❑ ❑
Type Biological
#Is chemical feed required to sustain process? ❑ ❑ ❑
Page# 7
Permit: NC0020389 Owner-Facility: Benson WWTP
Inspection Dale: 02/1712020 Inspection Type: Compliance Evaluation
Nutrient Removal Yes No NA NE
Is nutrient removal process operating property? ■ ❑ ❑ ❑
Comment: Alum and time are no longer used at the facility.
Filtration (High Rate Tertiary) Yes No NA NE
Type of operation: Down flaw
Is the filler media present? 0 ❑ ❑ ❑
Is the filter surface free of clogging? ❑ ❑ ❑
Is the filter free of growth? ❑ ❑ ❑
Is the air scour operational? ❑ ❑ ❑
Is the scouring acceptable? ❑ ❑ ❑
Is the clear well free of excessive solids and filter media? M ❑ ❑ ❑
Comment: 4 of 5 filters are online. The 5th filter contains broken plates that are no longer
manufactured. Staff are continuing to look into best options for bringing this unit back online.
All operable filters are backwashed on M W F or as needed and appeared to be operating-
sufficiently.
Solids Handling Equipment Yes No NA NE
Is the equipment operational? ❑ ❑ 0 ❑
Is the chemical feed equipment operational? ❑ ❑ ❑
Is storage adequate? ❑ ❑ N ❑
Is the site free of high level of solids in filtrate from filter presses or varuum filters? ❑ ❑ M ❑
Is the site free of sludge buildup on belts and+or rollers of filter press? ❑ ❑ M ❑
Is the site free of excessive moisture in belt filter press sludge cake? ❑ ❑ a ❑
The facility has an approved sludge management plan? 0 ❑ ❑ ❑
Comment: New pumps and electrical equipment were added or replaced in the pump house to better
regulate flow to the different treatment units and the lagoon.
Disinfection-Liquid Yes No NA NE
Is there adequate reserve supply of disinfectant? 0 ❑ ❑ ❑
(Sodium Hypochlorite)Is pump feed system operational? ■ ❑ ❑ ❑
Is bulk storage tank containment area adequate?(free of leaks open drains) 0 ❑ ❑ ❑
Is the level of chlorine residual acceptable? ❑ ❑ ❑ 0
Is the contact chamber free of growth,or sludge buildup? M ❑ ❑ ❑
Is there chlorine residual prior to de-chlorinat=on? ❑ ❑ ❑ M
Page# 8
Permit: NCO020389 Owner-Facility: Ben-acn WWTP
Inspection Date: 02117,2020 Inspection Type. [>mpl:ance EvaleaGon
Disinfection-Liquid Yes No NA NE
Comment: Per the ORC, the plant has changed from using gas to liquid sodium hypochlorite after
discussing the change with Central Office staff. Waterguard is scheduled to supply material
every,two weeks. The facility keeps a powder mix as a back-up. Estimated contact time in
the chamber is 30 minutes.
De-chlorination Yes No NA NE
Type of system 7 Liquid
Is the feed ratio proportional to chlorine amount(1 to 1)? 0 ❑ ❑ ❑
Is storage appropriate for cylinders? 0 ❑ ❑ ❑
#is de-chlorination substance stored away from chlorine containers? 0 ❑ ❑ ❑
Are the tablets the proper size and type? 110 0 ❑
Comment: Calcium thiosulfate is added and the effluent is post aerated-by units from the bottom of the
chamber. Waterguard also supplies this material.
Are tablet de-chlorinators operational? ❑ ❑ 0 ❑
Number of tubes in use? 0
Comment:
Flow Measurement - Effluent Yes No NA NE
#Is flow meter used for reporting? M ❑ ❑ ❑
Is flow meter calibrated annually? M ❑ ❑ ❑
Is the flow meter operational? 0 ❑ ❑ ❑
(If units are separated)Does the chart recorder match the flow meter? ❑ ❑ ❑
Comment: The effluent flow meter is used for reporting and was last calibrated 8-30-2019 b
Clearwater. The meter display showed 1.88 MGD at approximately 11:40 AM.
Effluent Pipe Yes No NA NE
Is right of way to the outfall properly maintained? ❑ ❑ ❑
Are the receiving water free of foam other than trace amounts and other debris? ❑ ❑ ❑
If effluent (diffuser pipes are required) are they operating properly? ❑ ❑ 0 ❑
Comment: Outfall appears to have a "Y-s lit"and discharges from two separate outlets in the same
location. Staff is requested to veriy and describe location of split.
Effluent Sampling Yes No NA NE
Is composite sampling flow proportional? M ❑ ❑ ❑
Is sample collected below all treatment units? M ❑ ❑ ❑
Is proper volume collected? ❑ ❑ ❑
Page# .9
Permit: NCO020389 Owner-Facility: Benson W WTP
Inspection Date: 02/1712020 Inspection Type: Compliance Evaluation
Effluent Sampling Yes No NA NE
Is the tubing clean? 0 ❑ ❑ ❑
#Is proper temperature set for sample storage(kept at less than or equal to 6.0 degrees a ❑ ❑ ❑
Celsius)?
Is the facility sampling performed as required by the permit((requency,sampling type M ❑ ❑ ❑
representative)?
Comment: The sampler temperature was noted as 3.0 degrees Celsius. The revious inspection noted
that samples were being collected at a rate that did not meek permit requirements. The
sampler is now set to collect 120 mL samples and is flow_proportional.
Standby Power Yes No NA NE
Is automatically activated standby power available? ❑ ❑ ❑
Is the generator tested by interrupting primary power source? ❑ ❑ ❑
Is the generator tested under load? 0 ❑ ❑ ❑
Was generator tested&operational during the inspection? ❑ 0 ❑ ❑
Do the generator(s)have adequate capacity to operate the entire wastewater site? M ❑ ❑ ❑
Is there an emergency agreement with a fuel vendor for extended run on back-up power? ❑ 0 ❑ ❑
Is the generator fuel level monitored? M ❑ ❑ ❑
Comment: The generator on site is equipped to provide power for the entire plant. The unit is manually
tested. The ORC stated that it has been several months since a test was last performed._
DWR staff recommended testing tau to-testin q the generator on a regular basis and
periodically under load (with appropriate documentation)to ensure that it will function
properly when necessary.
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