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HomeMy WebLinkAboutNC0038377_Report_20200129 ift,; DUKE James Wells ba Vice President ENERGY: Environmental,Health and Safety Programs&Environmental Sciences 526 South Church Street Charlotte,NC 28202 (980)373-9646 January 29, 2020 Via Overnight Mail RECEIVED FEB 0 4 2020 Linda Culpepper NCDEQ/DWR/NPDES Director of Water Resources North Carolina Department of Environmental Quality 1617 Mail Service Center Raleigh, NC 27699-1617 Bob Sledge Division of Water Resources North Carolina Department of Environmental Quality 1617 Mail Service Center Raleigh, NC 27699-1617 • Subject: Report Under Special Order by Consent — EMC SOC WQ S 18-005 Duke Energy Progress, LLC— Mayo Steam Electric Plant NPDES Permit NC0038377 Quarterly Progress Report for 4th Quarter 2019 Dear Ms. Culpepper and Mr. Sledge: On behalf of Duke Energy Progress, LLC (DEP), I am submitting to you the Mayo Steam Electric Plant Progress Report summarizing the work and activities undertaken with respect to closure of coal ash surface impoundment as required by the Mayo Steam Electric Plant NPDES Permit NC0038377 Special Order by Consent (SOC), SOC No. S 18-005 Section 2.c.2). As required by the SOC, I certify under penalty of law that this document and all attachments were prepared under my direction or supervision in accordance with a system designed to assure that qualified personnel properly gather and evaluate the information submitted. Based on my inquiry of the person or persons who manage the system, or those persons directly responsible for gathering the information, the information submitted is, to the best of my knowledge and belief, true, accurate, and complete. I am aware that there are significant penalties for submitting false information, including the possibility of fine and imprisonment for knowing violations. • Ms. Culpepper and Mr. Sledge January 29, 2020 Page 2 Please direct any questions concerning the Mayo Steam Electric Plant NPDES Permit NC0038377 SOC No. S 18-005 to Lori Tollie at (336) 854-4916. Sincerely, James ells Vice P esident, Environment, Health & Safety Programs and Environmental Sciences Duke Energy CC: Richard Baker, Duke Energy Lori Tollie, Duke Energy Leanne Wilson, Duke Energy George Hamrick, Duke Energy Paul Draovitch, Duke Energy Matt Hanchey, Duke Energy Randy Hart, Duke Energy r • NPDES PERMIT NC0038377 SPECIAL ORDER BY CONSENT EMC SOC S18-005 QUARTERLY PROGRESS REPORT MAYO STEAM STATION JANUARY 29, 2020 1 Background and Summary On August 15, 2018, Duke Energy Carolinas, LLC (DEC)and the North Carolina Environmental Management Commission entered into a Special Order by Consent - EMC SOC S18-005 (SOC) applicable to the Mayo Steam Station (Mayo). This report is submitted in accordance with Section 2.c.2) of the SOC. In compliance with Section 2 c 2), this report summarizes the work and activities undertaken with respect to decanting work and closure of coal ash surface impoundments at Mayo. The quarterly reports are due no later than the last day of January,April,July, and October for the duration of the SOC, once the decanting process has begun. The Mayo Steam Station is located in Roxboro, NC(Person County),on Mayo Lake.Mayo Lake is a man made reservoir constructed by the impoundment of the Mayo Creek. The Mayo Steam Station is a single unit, 727-megawatt,coal-fired generating facility, which began commercial operation in 1983. Mayo's ash basin has a single impoundment, which is regulated by the North Carolina Department of Environmental Quality. The ash basin covers approximately 153 acres with a current ash inventory of approximately 6.6 million tons of ash as of January 2020. Mayo historically wet sluiced coal combustion residual (CCR) products into a surface impoundment located on the property. This surface impoundment is known as the Ash Basin, which is impounded by the following dam: • Ash Basin(PERSO-035) The Ash Basin received CCR products from its initial operation in 1983 until 2019. Mayo ceased wet sluicing of bottom ash in May 2013 when the dry bottom ash system became operational. The Ash Basin was removed from service inJune 2019 upon the completion of the diversion of all other wastewater flow to a newly lined retention basin. Decanting Status In compliance with this SOC, Duke Energy initiated design and procurement efforts in Q3 2018 for a decanting water treatment system at Mayo. Purchase Orders were awarded in January 2019 for the WWTS pad and electrical infrastructure installations, as well as a Purchase Order for the wastewater treatment supplier. Duke Energy commenced construction of the infrastructure and system in March 2019 and completed it in May 2019. Duke Energy provided advanced notice for the projected start date of decanting to NCDEQ on June 27, 2019, as required by the NPDES Permit, and written notification for the initiation of decanting per the SOC on June 27, 2019. Through December 31, 2019, approximately 7 feet have been decanted from an initial depth of 46 feet. Mayo: 2 I . Decanting stopped at Mayo following a sloughing event on September 14, 2019, and likely will not resume until Q2 2020. The timing depends on action by NC Dam Safety on a request by Duke Energy to downgrade the FGD Basin Dam after solids from the FGD Basin are removed. This event, along with limits on the decanting rate, could potentially affect the Station's ability to meet its required completion date Mayo: 3