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HomeMy WebLinkAboutNC0039586_NOV-2019-LV-0738 Response_20191113(� DUKE ENERGY. NOV 13 2013 Serial: RA-19-0435 Certified Mail Number: 7014 2120 0003 3196 6831 Return Receipt Requested Mr. S. Jay Zimmerman, Chief Water Quality Regional Operations Section NC DEQ Division of Water Resources Raleigh Regional Office 3800 Barrett Drive Raleigh, NC 27609 Tanya M. Hamilton Vice President Harris Nuclear Plant 5413 Shearon Harris Road New hill, NC 27562-9300 NC Dept of Environmental Quality NOV 14 20 Raleigh Regional Office Subject: Duke Energy Progress, LLC — Shearon Harris Nuclear Plant (HNP) NPDES Permit No. NCO039586 Notice of Violation & Intent to Assess Civil Penalty Case Number: NOV-2019-LV-0738 Wake County Dear Mr. Zimmerman: On November 4, 2019, Duke Energy Progress, LLC (Duke Energy) received the subject Notice of Violation & Intent to Assess Civil Penalty letter dated October 30, 2019. In accordance with the letter, Duke Energy submits this response regarding Outfall 005 effluent Oil & Grease results for August 2019. Within the August 2019 Discharge Monitoring Report (DMR), we explained results for the primary and backup samples collected August 10, 2019 for Outfall 005 (batch radwaste treatment system) Oil & Grease from Treated Laundry and Hot Shower Tank B (TL&HS Tank B) were 25.0 mgll and 26.6 mgll, respectively. Results from our contract lab were not received until August 26 and 29 which did not support for any additional compliance sampling. Notification of the effluent limit for Oil & Grease was communicated to the Raleigh Regional Office (Bolick) on August 30, 2019. Outfall 005. is an internal outfall tributary to the main combined discharge outfall (Outfall 006) serving HNP which discharges into Harris Reservoir. Multiple processing tanks are part of Outfall 005. These tanks are processed, isolated and sampled individually before each tank is batched released. Only one tank is released at a time. On August 10, 2019, batch discharge flow from Outfall 005 was reported as 0.02 mgd. Flow for the combined discharge (Outfall 006) for August 10, 2019 was reported as 12.841 mgd. Outfall 005 represented less than 0.2% of the total flows discharged to Harris Reservoir on this date. Due to this minor composition of batch radwaste treatment system Oil & Grease (26.6 MGIL; <0.2%) in the overall discharge to Harris Reservoir, we feel confident stating no potential threat to public health or the environment was created as a result of these Oil & Grease daily maximum and monthly average Water Quality Regional Operations Section Serial RA-19-0435 exceedances. Also, subsequent Oil & Grease monitoring for internal Outfall 005 has consistently complied with the daily maximum and monthly average Oil & Grease limitations. Additional actions taken by HNP included: 1. The TL&HS Tank B with Oil & Grease in the release has been taken out of service and will be cleaned prior to returning to service; 2. The carbon filters in the Outfall 005 batch radwaste treatment system have been changed; 3. The presence of resin in the radwaste treatment system may have made Oil & Grease removal less effective, the resin vessel has been taken out of service for repairs; 4. Operational Oil & Grease samples are being taken to ensure Outfall 005 batch radwaste treatment system is removing Oil & Grease to within regulatory limits; and 5. Other radwaste associated tankage was inspected and tested for Oil & Grease to ensure no oil or grease was present in the tanks. Duke Energy Progress, LLC respectfully requests that the Division of Water Resources take into consideration these aspects related to the subject Notice of Violation prior to a decision to proceed forward with a civil penalty assessment for the daily maximum and monthly average Oil & Grease exceedances. If you have any questions regarding this matter, please contact Mr. Bob Wilson, HNP Site Environmental Professional at (919) 362-2444. 1 certify, under penalty of law, that this document and all attachments were prepared under my direction or supervision in accordance with a system designed to assure that qualified personnel properly gather and evaluate the information submitted. Based on my inquiry of the person or persons who manage the system, or those persons directly responsible for gathering the information, the information submitted is, to the best of my knowledge and belief, true, accurate, and complete. 1 am aware that there are significant penalties for submitting false information, including the possibility of tines and imprisonment for knowing violations. Sincerely, Tanya M. Hamilton Vice President, Harris Nuclear Plant Duke Energy Progress, LLC Water Quality Regional Operations Section Serial RA-19-0435 Enclosures: INIRA-19-0063 — NGD incoming Correspondence Notice of Violation & Intent to Assess Civil Penalty NOV-2019-LV-0738 RA-19-0387 October 2, 2019 — August 2019 eDMR Submittal cc: Ms. Vanessa Manuel, NC DEQ DWR Raleigh Regional Office Certified Mail Number: 7014 2120 0003 3196 5848 Return Receipt Requested Water Quality Regional Operations Section RA-19-0435 Enclosures INIRA-19-0063 — NGD Incoming Correspondence Notice of Violation & Intent to Assess Civil Penalty NOV-2019-1-V-0738 (3 pages including cover) Water Quality Regional Operations Section Serial RA-19-0435 Harris Nuclear Plant RA-19-0387 October 2, 2019 — August 2019 eDMR Submittal (22 pages including cover) ROY COOPER On ernnr MICHAEL S. REGAN 5eartar� LINDA CULPEPPER Dower Certified Mail # 7017 0190 0000 9562 7268 Return Receipt Reguested Paul Draovitch, Senior VP Duke Energy Progress LLC 526 S Church St - Ec3xp Charlotte, NC 28202 'sr�rf IN/RA-19-0063 NGD Incoming Correspondence NORTH CAROLINA Environmenfaf Quality 2010 October 30, 2019 Cr,, e a .� k SUBJECT: NOTICE OF VIOLATION & INTENT TO ASSESS CIVIL PENALTY Tracking Number: NOV-2019-LV-0738 Permit No. NCO039586 Shearon Harris Nuclear Power Plant Wake County Dear Permittee: A review of the August 2019 Discharge Monitoring Report (DMR) for the subject facility revealed the violation(s) Indicated below: Limit Exceedance Violati n s : Sample Limit Reported Location Parameter Date Value Value Type of Violation 005 Effluent Oil & Grease (00556) 8/10/2019 20 25.8 Daily Maximum Exceeded 005 Effluent Oil & Grease (00556) 8/31/2019 15 25.8 Monthly Average Exceeded A Notice of Violation/Intent to Issue Civil Penalty is being issued for the noted violations of North Carolina General Statute (G.S.) 143-215.1 and the facility's NPDES WW Permit. Pursuant to G.S. 143-215.6A, a civil penalty of not more than twenty-five thousand dollars ($25,000.00) may be assessed against any person who violates or fails to act in accordance with the terms, conditions, or requirements of any permit issued pursuant to G.S. 143-215.1. t +` fits--f._3 _ _.�f Rii' RYy':�s :"�z j cF3 '.� S 4 rri3 iJl s8 1 r14 [' PI'flf ..:f! 04 x ci6 If you wish to provide additional information regarding the noted violations, request technical assistance, or discuss overall compliance please respond in writing within ten (10) business days after receipt of this Notice. A review of your response will be considered along with any Information provided on the submitted Monitoring Report(s). You will then be notified of any civil penalties that may be assessed regarding the violations. If no response is received in this Office within the 10-day period, a civil penalty assessment may be prepared. Remedial actions should have already been taken to correct this problem and prevent further occurrences in the future. The Division of Water Resources may pursue enforcement action for this and any additional violations of State law. If the violations are of a continuing nature, not related to operation and/or maintenance problems, and you anticipate remedial construction activities, then you may wish to consider applying for a Special Order by Consent. Reminder: Pursuant to Permit Condition 6 in Section E, the Permittee is required to verbally notify the Regional Office as soon as possible, not to exceed 24 hours, from first knowledge of any non-compliance at the facility including limit violations, bypasses of, or failure of a treatment unit. A written report may be required within 5 days if directed by Division staff. Prior notice should be given for anticipated or potential problems due to planned maintenance activities, taking units off-line, etc. If you have any questions concerning this matter or to apply for an SOC, please contact Vanessa Manuel of the Raleigh Regional Office at 919-791-4255. Sincerely, S. Ja immerman, P.G., Chief Water Quality Regional Operations Section Division of Water Resources, NCDEQ Cc: WQS Raleigh Regional Office - Enforcement File Laserfiche ��✓ b. :• .3'. • f _vC: '" --.. - _...- :3 4.3 f J.4'7 , :f �: 3:s'r33=. :ii Water Quality Regional Operations Section Serial RA-19-0435 Harris Nuclear Plant RA-19-0387 October 2, 2019 — August 2019 eDMR Submittal (22 pages including cover) (� DUKE ENERGY. OCT 0 2 X11 Serial; RA-19-0387 Certified Mail Number: 7016 2140 0000 9417 7122 Return Receipt Requested NC Department of Environment and Natural Resources Division of Water Resources Water Quality Permitting Section ATTENTION: Central Files 1617 Mail Service Center Raleigh, North Carolina 27699-1617 Subject Duke Energy Progress, LLC Hams Nuclear Plant and Harris Energy and Environmental Center National Pollutant Discharge Elimination System (NPDES) Permit Number NC0039586 Electronic Discharge Monitoring Reports (eDMRs) Ladies and Gentlemen: John R. Dills Plant Manager Harris Nuclear Plant 5413 Shearon Harris Rd New Hill NC 27562- 9300 In accordance with NPDES Permit Number NC0039586, enclosed are the August 2019 eDMRs for the Hams Nuclear Plant and Hands Energy and Environmental Center. If you have any questions or require additional information. please contact Mr. Bob Wilson at (919) 362-2444 or Mr. Don Safrit at (919) 546-6146. 1 certify, under penalty of law, that this document and all attachments were prepared under my direction or supervision in accordance with a system designed to assure that qualified personnel properly gather and evaluate the information submitted. Based on my inquiry of the person or persons who manage the system, or those persons directly responsible for gathering the information, the information submitted is, to the best of my knowledge and belief, true, accurate, and complete. I am aware that there are significant penalties for submitting false information, including the possibility of fines and Imprisonment for knowing violations. Sincerely, John kills Enclosures: Electronic Discharge Monitoring Reports (signed original and one copy) Division of Water Resources Serial: RA-19-0387 /page 2 bc: Della Allen Jim Eayres Chase Fulk Don Safrit Bob Wilson Darlene Wallace Nuclear Records Division of Water Resources Serial: RA-19-0387 Enclosure 1 Harris Nuclear Plant and Harris Energy and Environmental Center NPDES Permit Number NCO039586 Electronic Discharge Monitoring Reports Submitted Electronically on August 20, 2019 (20 pages including cover) vrut•.� rl:Rw f NO.: NC0039386 PLIMI I % F H-S10\: 4 0 FM I LI I V NAME: Slicuton I lards Nuclur Puncr Plant CI.dSS: PC-2 Oil V M It NAME: nuke Energy Pro ss I I C OltC: Della R Allen G R W F: PC.. CD %Ilt PERIOD. 08-2019 (August 2019) COMPLI %NCE STATUS! Compliant ORC HAS CHANGED: No VERSION: 10 CO\TACT 1'lIONER:9193622966 PL10il•I•. r,%Tt S: Mlive COUNIN- Wake OIIC CElt It NUNlllER: 27903 STATUS: Prmcsscd 51111MISSION IMTE:0912712019 ORC/Certifier Signature: Dcllla Allen E-Nlait:dclla.allest @j duke:-cncrgy.com Phone H:919-362-2966 By this signature, I eertiry that this report is accuelle and complutu to ll_t= best of my knowledge 09/23/2019 Date The permitliw shall report to the Director or ilia appmpriaie Rugiunal Off ice any noncompliance that potentially threatt:n% public health or the envirnrtmunt_ Any infunaation shall be prut ided ornll) %%ithin 24 hours from the time the permiue:e became uaarc of the circumstances. A writtcei submission shall also be provided within 5 days of the lime the permilice becomes ut ere orthe circumslanct:s, Ifflu: facility is noncompliant, please attach a list of currcclit a actions being lnkcn and a time-lable for improvement; 1a be made as required by part 11_C.6 of the NI'DI S permit. _A\-� A PCrmiIIaaISubinIttc Signn c:'•• Jahn Dills C-NIuii:john.di Isaduke-energy.com Pcrnli4ec Addrccs: 5413 Sharon Barris Rd New [lilt NC 27562 Pcnnit C-(piralion Date: O8.,3le2021 0912712019 Phone 0:919-362-2000 Data l certify, under penult) of law, that this document and all attachments acre prepared under my direction or supervision in accordance with a system designed to assure that qualified personnel properly gather and evaluate the information submitted. Raced on my inquiry of the person or persons who managed the s) sicm, or those Persons dimcl I} respnn,ible for gathering the information, the information submitted is, to the best army kno+%ledge and bclier true, accurate, and eumplctc_ I um auarc that there are significant penalties for submitting false information, including ilia possibility noires and imprisonment far knowing violations CERTIFIED LABORATORIES L%B NAME: Oda Enertry Progrcss. En- veranmcMul Testing Solutions. Inc. ENCO 1.2bomtrnics - gazy. PACE Anal tical.Gel Lalwmtoncs, DEC - llunlersville. Duke LM—I • Carplrrias - IMEC Outfall 007 CERTIFIED LAIC M 398.037, 391, 67. 233. 248, 3145 PERM -Nis) COLLECTING SAMPLES. Daniel Johnson. Della Allca. Jerry Bolcy. Pend Mellon, Kathy Petersen. Daffy Butler. Rolm Vickers. Ulm Perry. Henry Duncan. Jordan Karp and Dale Tysrngcr PARANIETCR CODES Pwumeter Cads assistance may be obtained by calling the NPDES Unit (919) B07-6300 or by visiting http:ltportal.ncdenr.argl�%tbr%vgfs%sp/psrnpdcVfor ms. Use only units of measurement designated in the reporting facility's NPDES permit for reporting data. • No Flow/Discharge rmm Site: Check this box if no discharge occurs and as a exult, there arc no dote to be entered for all of the parameters on the DM for entire monitoring period. " ORC on Site?: ORC must visit facility and document visitation of facility as required per 15A NCAC BG .0204. "' Signature of PcrmitwL: [f signed by other than the permiucc, then delegation of the signatory authority must be on Me with the state per 15A NCAC 20 _0506(b)(2)(0). NPOCS PFIt,111'r,NO.: NCO039536 PERMIT % ERSION: J a FACILITY NAME: Slw:uun Harris Nucicar Pot= Plant CLASS: PC-2 OWNER NAME: Oukc GRaSy Progress LLC ORG Della It Al:cn GRAM: PC-2 ORC IIAS CII ►\GEI): No ewIlt rF.IIIOI):OS•2019(August 2019) VERSION: 10 PER,►Il r STATUS: Actirc COU. rl': ►►'akc OIlC CCRT NUMBER: 27903 SrATUS: Prucesscd NPOESl'l:RAllI'1\O.-NC0039586 PERdlll VERSION:4.0 CACll.l IT NAME: Shearon (farms Nuclear llimcr Plant CL,USS: rC-Z OWNER NAME: Duke Enrrgy Progress I LC ORC: Della R Allcn GRADE: PC-3 ORC HAS CIIANGEIi: No eD.11lt PERIOD: 08.2019 (August 7019) VEILSION: 10 ` rERMIT Sl .%Tt1S: Aclivc COilM% IVake ORC CERT R UMBER. 27903 ST.\TVS: Processed SAMPLING LOCATION: EFFLUENT DISCHARGE NO.: 001 NO DISCHARGE*: NO No RepoMttg Rwan: ENFRVSE - No Flow•Re0se fteeych: ENVIVTIIR - No Vuilaion Advcnc Warier: NOFLOW - No Flow. HOLIDAY - No Viliudio0 1101d y NPOES ITI(MIT NO.: NCO039586 PFRtiIYi' VERSION: d 0 PERMI I'SFA ITS: Amw FACILI I V NAME: Shearon Harris Nuclear Pastier Plant CI, %SS-. PC-2 cat Nl V: Wake OWNER NANIF,: fluke Energy Progress LLC ORC: Bella It Allen OtiC MIT NU]I1i1.11: 27903 GRADE. I'C•2 O8C ILAS CIIANGEO: No e11111t IT-11101):08.2019(August 2019) VERSION. 1.0 STATUS: Processed WWI - EI1luent Curnmenls: Chramium is not beinU added to the sysicin maximum Free Chlorine numbers are instantaneous rcadipzs. Na free available or total cldarmc dischar e - 0 minutes Week I Parameter (OO4DOI p1l sam ii d on 07-30-19, Parameter. (50060) Chlorine Total Residual. Parameter (78739) Chlorination duration, and Parameter (50064) Chlorine. Free Available sampled on O7.31.19 and mponedanitily2019cMilt NPOES PERMIT NO.: NCO039586 PERMIT VERSION: 4 0 FACILITY NAME: Slscaron llarris Nuclear Putter Plant CLASS: PC-2 OWNER NAME: Duke Energy Progress LLC OItC: Della It Allen GRADE: PC-2 OItC MS CHANGED: No tWilt 11FRIOD: 08.2019 (August 2019) VERSION: 1.0 PER 111T STATUS: Actit t: COUNTY: Wakc ORC CEItT NVNJREIt. 27903 STATUS: Ptoccsscd SAMPLING LOCATION: EFFLUENT DISCHARGE NO.: 002 NO DISCHARGE*: NO MEEMMMENE -•-• No Rrponing Reason: ENFRUSE - No Flow-ReuwAccycir; ENVWTIIR - No Visitation ALh-cne Wealber, NOFLOW - No Flaw. HOLIDAY - No Visiwion - Holiday NPUES PER,IUT NO.: NCDD39586 PERmI r x ERSION: 4 0 FACILITY NAME: Shearnn Harris Nuclear Power Plant CLASS: PC-2 OWNER NAME: Duke Energy Progress LLC ORC: Della R Allen GRADE: PC-2 ORC HAS CIIANCED: No eD.%IR PERIOD: 09-2019 (August 2019) VERSION: 10 Ou1ra11002 - EMurnt Comments: STP 2 down for maintenance UV disinrmlion being used. no chlorin is added to the system Anal le QuAficr ror 0&%tl9 for MonihiX Ammonia art: as f01iow3 (0) Ammonia (NH3) concentration in sample is gmwcr than the Total K'elJohl Nit n RN) concentration Analk Qualifier for 08113/19 for DOD an as rollmv (113) The dissolved oxygen depletion of the dilutian ►tialcr blank exceeded 0 2 mg1L Annly1c Quahfer for 08127119 for DOD are as follom: 106) The precision between 111c sam Ic and sample duplicate exceeded laboratory control limits PERMITSTATUS: Act -I've COU\TV: Woke ORC CERT NUMBLIt: 27903 STATUS: Promwd Week I Parameter ICO310) DOD, 5•D (20 Deg, C1- Concentration. Parameter COS30) Solids, Total Sus ndcd - Concentration, and Parameter (31616) Coltform. Fecal 61F. hIFC nwih. 44 5 C sam led on 07-30-19 and reported on July 2019 eDb1R NI'UCS I'ERdl11' NO.: NCO039586 MIl111T VER510.\: 4 0 FACILITY NAME: Shearun I lams Nuclear Pmwr Plain C! ASS: PC.2 OWNER NAME; puke Energy Progress LLC ORC: [klla It Allen GRADE. I'C-2 ORC HAS CIIANGED: No ellitlll i'E11101). 08.20191August 2019) VERSION: 10 i' IMIIT STATUS: Active COULNTV: Wake OKC CERT NUt1RIM. 27903 STATI S: I'ruccssetl SAMPLING LOCATION: EFFLUENT DISCHARGE NO.: 003 NO DISCHARGE*: YES "No Itepwinu R=son ENFRUSE • No Flo+wAeuzeMccyclr; ENVWTIIII - No Viuirarian Adverse Wesdm; NOFLOW No Flow, HOLIDAY - No Viuurion Ifolidsy NPpF:S i'F.101IT SO.: NC0039586 PEIt;;\11T VERSION: a 0 HACI1.I1 V vA,\IE: Slowron Ilarris Nuclumr Pu11rr Plaw CLASS: PC-2 OWNER NA Ili: Duke Energy Pmgress I.LC ORC: Milo R Allen GRADE,: PC-3 OKC IIAS CIIANGF:I): No enact PERIOD: 03.2019 (August 2019) V£RSIOS: 1.0 PCI!\1IT STATUS: Active COUNTY: Wake ORC CERT NUd111CII. 27903 STATUS: Processed SAMPLING LOCATION: EFFLUENT DISCHARGE NO.: 004 NO DISCHARGE*: NO 4 f a iw>r [ttvr n3u W=Llr 2 X m ah \l'rdr Eteima�e cne Grab rLffw 7Ss•c.w W1.rint ld" .w It. Im's..k u.. 11jam m9d1 MjPl f 120 10 Y NOFLOIY = 600 ]0 a NOFLOW 600 65 I3 NORM 610 23 V 0166 97 e3 120 1' S V 0 173 Us Y NOFLOW 120 12 Y 0 167 e 120 9 V NOFL01V 710 ray N 0171 1e 600 A 3 0 130 11 6m 63 NOR MY If 1:0 12.y 0141 107 c3 If S00 12 11 300 11 ENIM.OW .0167 a 410 Its 0131 u 600 Ia o.t16 Ir 600 6 11 we ! 1:0 12 9136 r S 1e 14.10 12 Y Nollow 1� 1.10 12 Y 0161 11 120 Icy Y 0179 u 310 7 N NORM 11 600 12 a 019 11 630 2 Y 0167 ,. 1e 120 12 Y NOFLOW 1r 1;0 123 V 0172 „ s o 12 Y 017 13 320 T Y NOFLOW 1e 600 la N 0172 11 600 6y N NOFLOW MrW3 A..ner t,i�N, 1� 1/ If 1673:9 l9 • a Dig 107 0 o.el x>rr�, 0 139 197 in —1 Na Reponing Reason: ENFRUSE - No Flow•RemeRecyc1c; ENVI UR - No Vril.Ylian Adcene Wcarlxr; N:OFLOW .- No Flow, ROLIDAY - No Vnitalion Floliday NPDES PERMIT NO.: NCO039586 PERMIT VERSION. a 0 FACILITY NAME: Shearon Ilarris Nuclear Poutr Plum CUSS: PC•2 OWNER NAME: Duke Energy Propms LLC ORC: Della R Allen GRADE: PC-2 ORC HAS CHANGED: No ebhIRPERIOD: 08-2019(Augum2019) VIERSIOY:10 Oulla(1004 - EMuent Comments: Dorch releases - Row only reported on days release!. Week I Paramerer (005551 oil & Grcase sampled 07-38.19 and rcporrcd on flee July 2019 cDSIR PERMITSPATUS: Active COUN'M Wake ORC CERT NUNIIIER: 27903 STATUS: Processed .NPWS PER III I' NO.: NCO039386 PERMIT VERSION: 4 0 r 1C1 LITY NAME: Slic2nul l iarris Nuclear Po"a Plus CL155: PC-2 OWNER NAW. Duk-c rncrey Progress LLC ORC: Dells R Allcn CRAVE: PC-2 OIIC HAS CIIANGED. No Olin PERIDU:08-3019(Augus12019) YEILSION:IO PERIII r STATUS: Active COi YFY: 1Vakc DI{C CEIVI' NUAIBEW 27903 STAI US: Processed SAMPLING LOCATION: EFFLUENT DISCHARGE NO.: 005 NO DISCHARGE*: NO > aa+ $ sum CRita MS4 [u mw Grab Grab nmv ri1-c— 01"Me 2400.64 It. rI11011..1. 11" YW% 111 1 9 t J20 $0 Y NOFLOR' = 600 10 Norco ' f 600 61 O NOFLOW' t 610 Si Y NOi9AN' a20 12 f Y NOFL011 1_0 121 Y NOFLOW T 420 12 Y NOFLOW -620 9 Y NORM • lzo 101 N Nanow q 600 65 0 cc2 , 259 1t 600 63 N NOrLOW 11 410 121 Y NOFLOW to 500 12 B NOFLOW 11 I $1101 11 a 0019 Is 410 Its 15 NOFLOW la 6w t0 0 NOFLOW 11 600 6 N NOFLOW u ISM f N NOFLOW u 4:0 U V NOFLOW >a 4:0 12 Y NOFLOW 11 420 12 Y NOFLOW v a.o 12.5 Y 001 L 310 7 N 0019 r+ 600 12 0 NOFLOW Sy 650 2 Y NOFLOW L 420 12 Y NOFLOW ?1 420 123 Y NOFLOW ¢ 420 112 IV NOFLOW Am 121 1 V NoFLOW 600 10 N NOFLOW 11 600 65 N !SOPLOW L1..61r A—W Ll.w is tl..dlr A...ape 09195 0 212 0•h w.Vr: 001 0 Sf 1 ".W A—t 6019 0 1231 • * No Reportirlp Remon ENFRUSE - No flow-ReuivItecyek: ENV%VTHR -No Visitaaan A4%c x Wcalbcr, NOFLOW. No flow. NOLIpAY - No Visitation Holiday NPI)ES PERMIT NO.: NCO039586 PEICMIF VERSION: 4.0 PERMITST.VTUS: Active IFACILITV NAME: Shearon Harris Nuclear Pourr Plant CI.,%SS: I'C-2 COUNTY: Wake OWNER NAME: Duke Energy Progress LLC ORC: Della R Allen ORC CERT NUN [BE R.- 27903 GRADE: PC-2 ORC IIAS CHANGED: No eD\IR PERIOD: 08--2019 (August 2019) VERSION: 1-0 STATUS: Promssed OutfaO 005 - EMucal Commcals: Batch rcicmcs - (low only reported an da) s released Qualifier for Oil and Grease an hlcthoJ Blank (U) Anal tc was analyzed for, but not detected above the MDL. MDA. MDC or LOD Oil and Grc= for Outfall 005 Sampled on 08.08-19 and Released on 08-10.19 tcsulrs received on 08-26-19 was 25 0 m . bxkupsmplcrcccivcdonOB-29-19%ims266mgfI Samples were awro ed for final result and mpoacd 25 8 mgA on eDh1R Raleigh Regional Office was nolifted on 09.30-19 ofhigh results source ofOtl wW Grease currently under ms•esligntion. Outfall WS Oil & Grease Exceeded On August 26, 2019, Harris Plant received preliminary notification from GEL Labs that the Oil & Grease for Outfall 005 was 25.0 mg/L for August 08, 2019 sample. The duplicate sample collected on August 08, 2019 was then shipped to GEL Labs. This result was determined to be 26.6 mg/I Oil & Grease on August 29, 2019. The Daily Max of 20 mg/I and the monthly max of 15 mg/1 for Oil & Grease were both exceeded because this was the only Oil & Grease sample for the month. The July 04, 2019 and the September 11, 2019 oil and Grease samples were < 4.17 mg/L for Outfall 005. HNP Chemistry then obtained multiple operational Oil & Grease samples. These Oil & Grease samples indicated no abnormal conditions (< 1.23 mg/1). Follow-up operational checks on the system noted no system challenges to corroborate an elevated result and all other NPOES values were in expected trends, There were no apparent equipment malfunctions. This event was reported to the NC DEQ DWR — Raleigh Regional Office on August 30, 2019. The event was determined not to require a 5-day follow-up report. Possible Causes: Residue oil and grease released on the wall of the tank, after the tank was processed and before the time of the tank's release. Corrective Actions: 1— Plant Operations has changed the Carbon filters In the Outfall 005 treatment system that Is used to remove Oil & Grease. IBNctl 2 —Chemistry will take operational Oil & Grease Sample to ensure that the Outfall 005 system is removing the oil and grease to within regulatory limits. 3 —This Tank has been removed from service (CAU-1-19-6245-B TLHS-0079). A work request has been Issued to inspect the tank Internals to verify no oil or grease remains in the tank (WR 20153983). NPIAS P'111111 NO.: N00039596 PERMIT VEERSION: d 0 FACILITY NAME: Sharon I larris Nuclear Pouu 111mu CLASS: 11C-2 OWNER NAME: Duke Energy Piugress LLC OIIC-: MIN R Allen GRADE: PC-2 OIIC HAS CHANGED: No 03111 PERIOM09-2019(Augusl20191 VERSION: 10 PE011TSTATUS.- Active COUNTY: %Vake ORC CF.RT NUMBER: 27903 STATUS: Procuscd SAMPLING LOCATION: EFFLUENT DISCHARGE NO.: 006 NO DISCHARGE*: NO " No Rcponi%Reason ENFRUSE No Flow-Rcoxiliecyalc; ENV%MIR No Viriwion Adwnc ►Ycatl&er; NOFLOW - No Flow. HOLIDAY - No Visiution Holiday ,INPIAS PERMIT No... NCO039586 PERMIT VERSIM: d 0 FACILITY NAMIr: Shearon I Isms Nuclear Pimer Plant CLASS: PC-2 OWNER NA31F.: Duke Encrgy PmbRcss LLC CHIC: 001a R Allen GRADE: PC-2 ORC HAS CHANGED: No CWHI PERIOD: 09.3019(August 3019) VERSION: 10 PERM T STATUS: Active COI'NM: W4k,: ORC CFR 1''iU►IDER: 27903 STATUS: I'ruccs,ed SAMPLING LOCATION: EFFLUENT DISCHARGE NO.: 006 NO DISCHARGE*: NO (Continue) MEW momm MIMMMMM MIMIKE "" No kporsing Reason. ENFRUSE - No Flow.ReuulRegcle: ENVLVTIIR - No Vhk'flion Adverse Weadrcr NOFLOW - No Flow, HOLIDAY - No Visimion Hofiday NPOLS PERMIT NO.: NCOD39586 PER %IIT VERSIO.N: a 0 FACILITY NANIE: Shearon I lams Nuclear Po%%vr Plant CLASS: PC-2 O%V,NER y,L11E: Duke Engly Prois LLC ORC: Della R Allen GRADE: PC-2 ORC IIAS CHANGED: No e13*4I11 PERIOD:08-2019 (August 3019) VERSION: 1.0 PER STATUS: Aclive COUIN71': Wale ORC CERT NUMBER: 27903 STATUS: Processed on Wall 006 - E1Huent Cumnuols: Week I Paramelev (00010) Tem eralum. Water Deg. Centigrade. Pommctcr. (004DD) pil and Pammelcr (81313► fi drazine sampled 07-30.19 and reported on the July 2019 eDM NPUES PERIM' NO.: NCO039586 PERMIT VERSIDS: 4 0 FACILITY NAME: Shown l lams Nuclear Power Plant CLASS: PC•2 ` OWNER tiAME: Auks Energy Progress LLC ORC: Della R Allen GRADE: PC-2 ORC IIAS CIIA. iGED: No tDMR PERIOD: 08.2019 (August 2019) t'ERSION: 1.0 PERMITSTATUS: Active COUXTY: Wake ORC CERT NU3111 M. 37903 SrdTUS: Pruccsscd SAMPLING LOCATION: EFFLUENT DISCHARGE NO.: 007 NO DISCHARGE*: NO MIMS mm�� mm mm mm mm mm eParfiRB Itramon ENFRUSE - No Flow•Ilewe!(lecycle: ENVWTIM • No Viuption ,Adverse WeAcr. NOFLOW - No flow, 110LIDAY • No Vititation Iloliday rNPDEs PERMIT NO: NCO039396 PEItan I• %IF 11slON: 4 0 FACILITY NAME: Sharon I lams Nuclear 1'uarr Plam CLASS: PC-2 OWNERNAME. Duke Energy Progress LLC OKC: DOW R Atlen GRADE.- PC-2 ORC HAS CHANGED: No dMilt PERIOD. 08.2019 (August 2019) VERSION: 10 nuaursi•.%i,t S: Acl tc COUP I Y: %Vukc ORC CENT NUM11F R: 2m] STATUS: Prtxes,d SAMPLING LOCATION: EFFLUENT DISCHARGE NO.: 007 NO DISCHARCL*: NO (Continue) "" No Reporting Rc mn EWFRUSE . Na Flow-RcumMecyek: ENVWTI{R . No Visiutian Adsarse Weadmr: NOFLOW - No Flow. IIOLIDAY • No Visuadon Ilaliby NPDES PERM ITNO.: NCO039586 PER�111T VEItSION:4O FACILITY NAME: Shearon Ifords Nucfear Po%vcr Planl CLASS: PC-2 OWNER NAME: Duke Energy Progress LLC ORC: Ddlo R Allen GRADE: PC-2 MNIR PERIOD:O8-2019 (Au r t 2019) Oulfall 007 - EIIIueo1 Comments: Balch releases - flow only reponcd on days released No Dischw a on Week 1.3 or 4 ORC IUS CHANCED: No VERSION: 10 PERMIT STATUS: Active COUN"ry: Wake ORC CERT NU,IIIIER: 27903 STATUS: Processed