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HomeMy WebLinkAbout8003_RowanCountyGrounwaterWellInstall_GWMR_20170809 Golder Associates NC, Inc. 5B Oak Branch Drive Greensboro, North Carolina, 27407 Tel: (336) 852-4903 Fax: (336) 852-4904 www.golder.com Engineering Lic. No. C-2862/Geology Lic. No. C-399 Golder Associates: Operations in Africa, Asia, Australasia, Europe, North America and South America August 9, 2017 0636572017 Ms. Jackie Drummond Department of Environmental Quality Division of Waste Management - Solid Waste Section 2090 US Highway 70 Swannanoa, North Carolina 28778 jaclynne.drummond@ncdenr.gov RE: SUMMARY OF REPLACEMENT GROUNDWATER MONITORING WELL INSTALLATION ROWAN COUNTY LANDFILL, PERMIT NO. 80-03 ROWAN COUNTY, NORTH CAROLINA Dear Jackie: On behalf of Rowan County, Golder Associates NC, Inc. (Golder) is submitting the enclosed letter report summarizing the installation of groundwater monitoring well MW-28R at the active Rowan County Municipal Solid Waste (MSW) Landfill in Woodleaf, North Carolina (NC). The groundwater monitoring well was installed in accordance with the Title 15A of the North Carolina Administrative Code (NCAC), Subchapter 2C Section .0100 (the North Carolina Well Construction Standards) as a replacement well for MW-28 as approved in your correspondence dated December 13, 2016. On July 11, 2017, a Golder licensed geologist provided oversight for the installation of groundwater monitoring well MW-28R. The well was installed by South Atlantic Environmental Drilling and Construction Company, Inc. (SAEDACCO) of Fort Mill, South Carolina, a NC licensed driller. The equipment consisted of a Gus Pech Brute drilling rig utilizing 4.25-inch inner diameter (ID) hollow stem augers (HSAs). The boring was advanced with HSAs to a depth of approximately 32 feet below ground surface (bgs). The monitoring well was constructed with 2-inch schedule 40 polyvinyl-chloride (PVC) screen and riser pipe. The 0.010-inch slotted screen was installed from 17 to 32 feet bgs. The filter pack consisted of Driller Service Inc. (DSI) #2 sand from 15 to 32 feet bgs. A filter pack seal was installed from 13 to 15 feet bgs and consisted of 3/8-inch bentonite chips. The remaining annular space was filled with Type I Portland cement. The surface completion consisted of a lockable steel protective casing and a 3-foot by 3-foot by 0.5-foot concrete apron. The boring / well construction log and Form GW-1 Rev. 8/13 are provided as Attachment A. The monitoring well construction is also summarized on Table 1. The well was developed on July 13, 2017, utilizing an air lift pump system until field parameters stabilized and relatively sediment-free water was obtained. The well was developed for approximately 2.5 hours. During that period of time approximately 48 gallons of water were removed to achieve a turbidity of less than 10 nephelometric turbidity units (NTUs). The well development forms are provided as Attachment B. The well was surveyed by Ribelin Land Surveying, Inc. A sealed survey letter is provided as Attachment C. The location of MW-28R is shown on Drawing 1. The replacement well MW-28R was sampled during the routine semi-annual sampling event in July 2017 and results will be submitted under separate cover. Should you have any questions or require additional information, please do not hesitate to contact the undersigned at (336) 852-4903. We appreciate your assistance with this project. ATTACHMENT A BORING AND WELL CONSTRUCTION LOGS AND WELL CONSTRUCTION RECORDS 2.00 2.00 2.00 2.00 1.40 2.00 1.50 2.00 1.80 2.00 1.90 2.00 1.80 2.00 2.00 2.00 0.00 - 2.00SILTY CLAY, w < PL, some coarse sand,orange-brown mottled red, soft 2.00 - 4.00CLAYEY SAND, coarse sand, poorlygraded, red mottled grey and orange brown,dry, loose 4.00 - 6.00SILTY CLAY, w < PL, red, firm 6.00 - 11.00SAND, poorly graded, medium to coarse,angular, compact, orange-brown mottledgrey, dry 11.00 - 16.00SAND, poorly graded, medium to coarse,angular, loose, grey-brown, mottled white,moist 16.00 - 21.00SAND, poorly graded, angular quartz gravel,10% coarse, light brown mottled white,moist 21.00 - 26.00SAND, poorly graded, coarse quartz andmicaceous sand, 10-20% coarse, angularquartz gravel, compact, light brown, someblack staining, moist 26.00 - 32.00SAND, poorly graded, coarse quartz andmicaceous sand, 20% coarse, angularquartz gravel, compact, light brown andwhite, moist Boring completed at 32.00 ft Portlant Type1 Cement 3/8"BentoniteChips #1 TypeSand 0.010' SlottedScreen 3-2-9-10 8-10-11-15 4-4-5-6 4-6-7-5 4-5-7-8 7-9-9-13 11 21 9 13 12 18SSSSSSSSSSSS681.04 679.04 677.04 672.04 667.04 662.04 657.04 651.04 2.00 4.00 6.00 11.00 16.00 21.00 26.00 1 2 3 4 5 6 7 8 CL SC CL SP SP SP SP SP SOIL PROFILE SHEET 1 of 1 ELEVATION(ft)WELLCONSTRUCTIONDETAILS SAMPLES DESCRIPTION RECORD OF BOREHOLE MW-28R RECLOCATION: Rowan County, NC DRILL RIG: Gus Pech BruteDATE STARTED: 7/11/17DATE COMPLETED: 7/11/17 DEPTH(ft)0 5 10 15 20 25 30 35 40 45 LOG SCALE: 1 in = 5.5 ft DRILLING COMPANY: SAEDACCO DRILLER: Rich Lemire GA INSPECTOR: William Ballow CHECKED BY: Ben Draper, P.G. DATE: 9/12/17 NORTHING: 731,882.07EASTING: 1,538,013.18GS ELEVATION: 683.04TOC ELEVATION: 685.26 PROJECT: Rowan County - Active LandfillPROJECT NUMBER: 0636572017DRILLED DEPTH: 32 ft DEPTH W.L.:24.29 ftDATE W.L.:7/11/17TIME W.L.:1129GW ELEVATION:660.97 ft MONITORING WELL/PIEZOMETERDIAGRAM and NOTES WELL CASING Interval: 0.0'-17.0' Material: Schedule 40 PVC Diameter: 2" Joint Type: Threaded WELL SCREEN Interval: 17.0'-32.0' Material: Schedule 40 PVC Diameter: 2" Slot Size: 0.010" End Cap: Schedule 40 PVC FILTER PACK Interval: 15.0'-32.0' Type: #1 Type Sand FILTER PACK SEAL Interval: 13.0'-15.0' Type: 3/8" Bentonite Chips ANNULUS SEAL Interval: 0.0'-13.0' Type: Portlant Type 1Cement WELL COMPLETION Pad: 3'x3'x6" Protective Casing: AnodizedAluminum DRILLING METHODSSoil Drill: 4.25 inch HSARock Drill: N/A BOREHOLE RECORD MW-28R_LOG.GPJ PIEDMONT.GDT 8/8/17N-VALUE140 lb hammer30 inch drop BLOWSper 6 in USCSTYPESAMPLE NO.DEPTH(ft) ELEV.GRAPHICLOG680 675 670 665 660 655 650 645 640 Rich Lemire 2593A SAEDACCO Inc X 7-11-2017 MW-28R ROWAN COUNTY MSW LANDFILL 789 Campbell Rd. Woodleaf, NC 27054 Rowan County, WOODLEAF, NC, 27054 ROWAN X X 1 32' 14' 8" AUGERS 0 17' 2"SCH40 PVC 17' 32' 2" .010 SCH40 PVC 0 13' PORTLAND POURED 15' 32' SAND 2# 0 10' RED CLAY 10' 32' SAPERLITE BENTONITE FROM 13' TO 15'. 7/11/2017 ATTACHMENT B WELL DEVELOPMENT FORM ATTACHMENT C SURVEY LETTER DRAWING 1 i2 i3 i1 660650670 680 690 700 700 690 680 670 660 650 640640 OLD LANDFILL ENTRANCE SCALE HOUSE PROPERTY LINE 100-YEAR FLOODPLAIN EXISTING SEDIMENT BASIN EXISTING SEDIMENT BASIN FUTURE MSW LANDFILL (PHASES IV &V) FRENCH DRAIN SAMPLE POINT TO SW-1 (SEE NOTE 6) 710 710 EXISTING SEDIMENT BASIN EXISTING SEDIMENT BASIN EXISTING SEDIMENT BASIN MMW-6A MMW-2A MMW-3MMW-4 MMW-CD MMW-5A MMW-1 MMW-7 MMW-6 702.25MW-9 704.77MW-16 681.68 MW-13 678.41 MW-12 SW-4 663.05MW-23 663.06MW-23A 681.92MW-20 692.72MW-1 680.54MW-24R 658.46MW-6 SW-3 646.06 MW-7 641.64MW-18R 641.94MW-19 706.02MW-17 SW-5 SW-2 MW-25 MW-26 MW-27A MW-28 654.75655.02 657.51 660.30 MW-27 669.94 MMW-5 MMW-2 MMW-8 674.89MW-11 MW-28R CONSULTANT DESIGN PREPARED REVIEW APPROVED YYYY-MM-DD TITLE PROJECT No.Rev. PROJECTCLIENT Path: \\greensboro\CAD\_2006\0636572 - Rowan Co\PRODUCTION\_G - GW 2017\ | File Name: 0636572017H001.dwgIF THIS MEASUREMENT DOES NOT MATCH WHAT IS SHOWN, THE SHEET SIZE HAS BEEN MODIFIED FROM: ANSI D01 in0636572016 PHASE 100 DRAWING 10 2017-03-03 BSD MCG BSD RPK ROWAN COUNTY ACTIVE LANDFILLS PERMIT NO.80-03 ROWAN COUNTY, NORTH CAROLINA ROWAN COUNTY GROUNDWATER CONTOUR MAP JANUARY 17, 2017 0 FEET 250 500 SCALE EXISTING TOPOGRAPHIC CONTOUR FACILITY BOUNDARY APPROXIMATE LIMITS OF WASTE GROUNDWATER SURFACE CONTOURS APPROXIMATE GROUNDWATER FLOW SEGMENT USED TO CALCULATE GRADIENT EXISTING GROUNDWATER MONITORING WELL WITH GROUNDWATER ELEVATION NEWLY INSTALLED GROUNDWATER MONITORING WELL SURFACE WATER MONITORING POINT COMPLIANCE METHANE MONITORING POINT ASSESSMENT METHANE MONITORING POINT NOT AVAILABLE FRENCH DRAIN MONITORING POINT LEGEND NOTES REFERENCES i1i1 1. TOPOGRAPHIC CONTOUR INTERVAL = 2 FEET. 2. GROUNDWATER SURFACE CONTOUR INTERVAL = 10 FEET. 3. GROUNDWATER ELEVATIONS MEASURED ON JANUARY 17, 2017. 4. GROUNDWATER CONTOURS ARE BASED ON LINEAR INTERPOLATION BETWEEN AND EXTRAPOLATION FROM KNOWN DATA, TOPOGRAPHIC CONTOURS, AND KNOWN FIELD CONDITIONS. THEREFORE, GROUNDWATER CONTOURS MAY NOT REFLECT ACTUAL GROUNDWATER CONDITIONS. 5. GROUNDWATER CONTOUR LINES SHOW THE WATER TABLE SHAPE AND ELEVATION. THESE CONTOURS ARE INFERRED LINES FOLLOWING THE GROUNDWATER SURFACE AT A CONSTANT ELEVATION ABOVE SEA LEVEL. THE GROUNDWATER FLOW DIRECTION IS GENERALLY PERPENDICULAR TO THE GROUNDWATER SURFACE CONTOURS, SIMILAR TO THE RELATIONSHIP BETWEEN SURFACE WATER FLOW AND TOPOGRAPHIC CONTOURS. 6. SURFACE WATER MONITORING POINT SW-1 IS APPROXIMATELY 550 FEET OFF THE MAPPING LIMITS SHOWN AND IS COLLECTED FROM SECOND CREEK. 7. MONITORING WELL MW-27A IS UTILIZED FOR WATER LEVEL MONITORING ONLY. 8. THE LOCATION OF THE FRENCH DRAIN MONITORING POINT IS APPROXIMATE. 650 1. OVERALL SITE BASE TOPOGRAPHY PROVIDED BY S&ME ENGINEERING, INC. MW-25 NA SW-4 MW-7646.06 SITE LOCATION MAP 1" = 10,000' SITE LOCATION PE C-2862 PG C-399 GOLDER ASSOCIATES NC, INC. TABLE 1 August 2017 1 of 1 0636572017 from to from to MW-28R 07/11/17 2 731,882.070 1,538,013.180 683.04 685.26 32.00 651.04 24.29 658.75 17.00 32.00 666.04 651.04 Sand Compliance Well Notes: 1. ft AMSL = feet above mean sea level 2. bgs = below ground surface 3. TOC = top of casing Rowan County Landfill, Permit No. 80-03 Landfill Gas Monitoring Well Identification Date Installed Casing Diameter (inches) Elevations Total Depth Drilled Screened Interval ft AMSL Lithology of Screened IntervalNorthingEasting TABLE 1 Summary of Monitoring Well Construction Information STATUSGround Surface TOC Depth (ft bgs) Elevation (ft AMSL) Depth (ft bgs)Elevation (ft AMSL) Groundwater Surface Depth (ft bgs) Elevation (ft AMSL) Table 1.xlsx