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HomeMy WebLinkAbout1812_DukeMarshall_Piez_ReplacementCompletion Report_FID1891048_20240725DUKE ENERGY July 25, 2024 North Carolina Department of Environmental Quality Division of Waste Management Solid Waste Section 2090 U.S. Highway 70 Swannanoa, NC 28778 Attn: Ms. Sarah Moutos (submitted electronically) Re: Piezometer Replacement (Abandon/Install) Completion Report Industrial Landfill No.1 Phase 3 Permit No.: 1812-INDUS-2008 Marshall Steam Station Terrell, North Carolina 28682 Dear Ms. Moutos: 525 S. Tryon St. Charlotte NC, 28202 The Solid Waste Section approved Duke Energy's request for abandoning and replacing Industrial Landfill No.1 (1812-INDUS; ILF) Phase 3 piezometers CLF-22-306 and CLF-22-307 in a letter dated June 14, 2024. Duke Energy is providing the Completion Report for the piezometer replacements, including the well abandonment records, well installation records, boring logs, well construction information, survey data, and water level information both pre -abandonment and post -installation. The piezometer replacement activities were conducted by S&ME on June 25-27, 2024. Well abandonment and construction records (GW-30 and GW-1 forms) were submitted separately to the NCDEQ Information Processing Unit. If you need additional information regarding this submittal do not hesitate to email or call me at Ashley.HealvCcDduke-energy.com or (717) 982-0986. Respectfully submitted, J4$1�Ai Ashley Healy, P.G. Environmental Services Attachments: Completion Report for Monitoring Well Replacements (S&ME, July 2024) cc (via e-mail): Deana Yitbarek, NCDEQ Sherri Stanley, NCDEQ Dan Zakary, Duke Energy Scott Saunders, Duke Energy Jake Muessen, Duke Energy John Metcalf, Duke Energy Tyler Hardin, Duke Energy Anne Davin, Duke Energy Jasmine Tayouga, S&ME www.duke-energy.com Page 1 of 1 July 24, 2024 Duke Energy Marshall Steam Station 8320 NC Hwy 150 E Terrell, North Carolina 28673 Attention: Ms. Ashley Healy, P.G. EHS Waste and Groundwater Programs, Duke Energy Reference: Completion Report for Monitoring Well Replacements Duke Energy Marshall Steam Station Catawba County, North Carolina S&ME Project No. 21410007, Ph. 02 Dear Ms. Healy: S&ME, Inc. (S&ME) is pleased to present this Completion Report (hereafter, Report) for the replacement of two (2) groundwater monitoring wells at Duke Energy's Marshall Steam Station (hereafter, Site), located at 8320 NC Hwy 150 E, in Catawba County, North Carolina. These wells were replaced to support the construction of Cell 7 within Phase 3 of the Industrial Landfill (ILF) — Permit No. 1812. This Report summarizes the activities performed by S&ME at the Site between June 2511 and 27t", 2024, as well as a certification statement signed by a North Carolina licensed geologist, Julie Robertson, P.G, certifying that each monitoring well was abandoned and replaced in compliance with the applicable standards and guidance as discussed in this Report. Background and Summary S&ME understands that as part of the ILF Phase 3 geotechnical investigation, monitoring wells CLF22-306 and CLF22-307 were installed by others in March of 2022 to collect monthly groundwater elevation data and demonstrate the vertical separation between groundwater and the compacted soil liner base grade design for Cell 7. Duke Energy requested that these wells be relocated due to their current location being in the vicinity of haul roads and ongoing construction and earthwork activities. Additionally, the water levels in CLF22-306 and CLF22- 307 have declined several feet since they were installed. To continue monitoring groundwater levels and confirm the groundwater and soil base grade vertical separation is met, replacement wells (CLF22-306R and CLF22-307R) were installed as close as practical to the original wells, given the current and future Site conditions and on -going construction activities (see Figure 1 in Attachment 1). These replacement wells were also installed deeper than the original wells to allow for an increased water column in each well for continued groundwater elevation data collection. Monitoring Well Abandonment The original monitoring wells CLF22-306 and CLF22-307 were abandoned by a North Carolina registered well driller on June 261", 2024. Each monitoring well was abandoned in accordance with the 75A NCAC 02C Section S&ME, Inc. 12016 Ayrsley Town Blvd., Suite 2-A I Charlotte, NC 282731 p 704.523.4726 1 www.smeinc.com Completion Report for Monitoring Well Abandonments Duke Energy Marshall Steam Station S&ME Project Number 21410007, Ph. 02 July 24, 2024 Page 2 .0113 Standards for the Abandonment of Wells (hereafter, Well Abandonment Standards). S&ME personnel provided support and oversight during the abandonment process for each monitoring well to confirm compliance with the Well Abandonment Standards as mentioned above. Per the Well Abandonment Standards, a well must be permanently abandoned if it acts as a source or channel of contamination. Each of these wells were abandoned prior to earthwork and grading operations to reduce the likelihood that the wells would act as a channel for contaminants to reach groundwater once the well was removed during excavation and earthwork activities. A summary of pertinent monitoring well information for each of the wells abandoned is located in Table 1 in Attachment II. As required by the Well Abandonment Standards, a Well Abandonment Record (GW-30 Form) was completed and signed for the two (2) wells abandoned. S&ME submitted these GW-30 Forms to the North Carolina Department of Environmental Quality (NCDEQ) — Division of Water Resources (DWR) Information Processing Unit, and they are included in Attachment III as reference. Each of the monitoring wells were abandoned following the general steps listed below: If present, any dedicated tubing, pumps, or transducers were removed from the well and left on site with Duke Energy personnel. Depth to water from ground surface was measured using an electronic water level meter. The bottom of each well was also tagged to ensure no discrepancies between recorded and actual well depth data exist. The volume of water in the well was calculated based on the measured water level. Each well was abandoned using coated bentonite pellets in accordance with the general requirements of 02C Standards, as equipment access to these wells was very limited at the time of abandonment. S&ME understands that the protective well covers and concrete pads will be removed from each of the abandoned well locations by the general earthwork contractor on Site. Installation of Replacement Monitoring Wells The replacement monitoring wells were installed by a North Carolina Registered well driller; CLF22-306R was installed on June 251", 2024, and CLF22-306R was installed on June 261", 2024. Each of these wells was constructed as typical Type II Monitoring Wells in accordance with the 75A NCAC 02C Section .0108 Standards of Construction: Wells Other than Water Supply (hereafter, Well Construction Standards). S&ME personnel provided support and oversight during the well installation process. Each of the replacement monitoring wells were installed following the general steps listed below: A borehole was drilled using 3.25-inch Hollow Stem Augers (HSAs) to the target elevations provided by Duke Energy. It should be noted that CLF22-307R was drilled 3.2-feet deeper than proposed to confirm adequate water would be present once the well was installed. No sampling was performed; however, S&ME personnel classified soil from the auger cuttings in general accordance with the United Soil Classification System (USCS), in addition to recording other pertinent drilling information including hard drilling zones and the depth water was encountered during drilling. The HSAs were removed from the borehole and a 2-inch diameter Type II monitoring well was installed at each location (CLF22-306R and CLF22-307R) as specified below: 2-inch diameter sch. 40 Polyvinyl Chloride (PVC) casing 10-foot PVC 0.010-inch slotted screen (pre -packed) S&ME, Inc. Completion Report for Monitoring Well Abandonments Duke Energy Marshall Steam Station S&ME Project Number 21410007, Ph. 02 No. 2 filter sand pack to 2-feet above the top of the well screen A 2-foot annular seal (bentonite pellets) above the sand pack Neat cement grout from ground surface to top of annular seal Protective steel cover 4-inch-thick concrete well pad (2-foot by 2-foot) Four (4) bollards were installed around each well location July 24, 2024 Page 3 Once well installation was completed, each well was developed by S&ME personnel on June 261" and 27t", 2024, following the general steps below: Depth to water was measured (from ground surface), and the volume of water present in each well was calculated Each well was then pumped until a minimum of three (3) well volumes were removed, and a turbidity less than 50 NTUs was achieved If a well was pumped dry, it was monitored, and recharge rates were recorded Periodically, the pump was moved up and down to increase agitation and removal of any soil particles during development Boring logs including the soil lithology, drilling observations, and well construction details are included as Attachment IV. A summary of pertinent monitoring well construction information for each of replacement wells is located in Table 2 in Attachment II. As required by the Well Construction Standards, a Well Construction Record (GW-1 Form) was completed and signed for the two (2) wells installed. S&ME submitted these GW-1 Forms to the NCDEQ-DWR Information Processing Unit, and they are included in Attachment III as reference. Well development forms are included in Attachment V. Monitoring Well Replacement Certification Monitoring wells CLF22-306 and CLF22-307 discussed in this Report were abandoned in accordance with the requirements of the Well Abandonment Standards by a certified Well Driller licensed in the State of North Carolina. Replacement monitoring wells CLF22-306R and CLF22-307R were installed as typical Type II monitoring wells by a certified Well Driller licensed in the State of North Carolina. Under the supervision of an S&ME licensed geologist, an S&ME professional was on site to observe each well abandonment and installation. Closure S&ME appreciates each and every opportunity to be of service to Duke Energy. Please contact us if you have any questions regarding this report. S&ME, Inc. Completion Report for Monitoring Well Abandonments July 24, 2024 Duke Energy Marshall Steam Station Page 4 S&ME Project Number 21410007, Ph. 02 Sincerely, 5&ME, Inc. t, f„4,nC)JF' Vil Jasmine Tayouga, E.I. Julie P. Robertson, P.G. Project Manager/Team Lead Vice President/Services Manager jtayouga@smeinc.com iobertson@smeinc.com Attachments: I — Figures II — Tables III — Well Abandonment and Construction Records (GW-30/GW-1 Forms) IV — Boring Logs V — Well Development Forms S&ME, Inc. Attachments Attachment I — Figures Path: T:\Asheville-141 3rojects\2021\21410007 Duke Marshall CCP Closure On -Call Services Terrell NC\02_Well Abandonments\June2024\GIS\MSS_June2C FUTUREELF!FUTURE ILF ILF PHASESPHASE 4 CELL 7 0 400 800 (FEET) ; REFERENCE: THIS MAP IS FOR INFORMATIONAL PURPOSES ONLY. PREVIOUSLY ABANDONED AND/OR REMOVED MONITORING WELLS ARE NOT SHOWN ON THIS MAP. AERIAL IMAGERY DATE: JULY 8, 2024. ALL FEATURE LOCATIONS DISPLAYED ARE APPROXIMATED. THEY ARE NOT BASED ON CIVIL SURVEY INFORMATION, UNLESS x STATED OTHERWISE. _ MONITORING WELL REPLACEMENTS - JUNE 2024 III E DUKE ENERGY - MARSHALL STEAM STATION CATAWBA COUNTY, NORTH CAROLINA 07-22-2024 C;7 LEGEND MONITORING WELLS ABANDONED ON 6/26/2024 MONITORING WELLS INSTALLED ON 6/25 AND 6/26/2024 ■■ ■� INDUSTRIAL LANDFILL (ILF) BOUNDARIES (PERMIT NO. 1812) 1804 PH. II LANDFILL (PERMIT NO. 1804) ASBESTOS LANDFILL (PERMIT NO. 1804) DEMOLITION LANDFILL (PERMIT NO. 1804) SCALE: FIGURE NO. 1 " = 400 ' DATE: 7-22-2024 PROJECT NUMBER 21410007 Attachment II — Tables Table 1: Summary of Monitoring Well Abandonments CLF22-306 and CLF22-307 Monitoring Well Replacements Duke Energy - Marshall Steam Station S&ME Project No. 27470007, Ph. 02 Depth to Water Total Well Casing Stick -Up Total Well Depth s Screened Interval a Northing a Easting Date Prior to Well ID' z Depth Height (ft-bgs) (ft-bgs) (ft-NAD83) (ft-NAD83) Abandoned Abandonment (ft-toc) (ft-ags) (ft-toc) CLF22-306 28.3 3.3 25.0 15.0 to 25.0 685033.0 1413752.3 6/26/2024 26.7 CLF22-307 43.0 3.0 40.0 30.0 to 40.0 684539.9 1413247.5 6/26/2024 37.5 Notes: I Each monitoring well consisted of 2-inch inner diameter inner polyvinyl chloride (PVC) casing z Total Well Depth - prior to abandonment, the depth to the bottom of the screened interval was measured on each well 3 Screened intervals were recorded from information on the well tag at each location ° Northing and Easting coordinates provided by Duke Energy ft: feet ags: above ground surface bgs: below ground surface NAD83: North American Datum 1983 toc: top of casing Table 2: Summary of Well Construction Information CLF22-306 and CLF22-307 Monitoring Well Replacements Duke Energy - Marshall Steam Station S&ME Project No. 27470007, Ph. 02 Ground Casing Stick- Total Well Depth to 4 Geology in Well Date Northing Easting Surface Screened Interval Well ID 2 Up Height Depth 3 Water Screened Diameter Casing Type Installed (ft-NAD83) (ft-NAD83) Elevation (ft-bgs) (ft-ags) (ft-bgs) (ft-bgs) Intervals (in) (ft-MSL) CLF22-306R 1 6/26/2024 1 685002.97 1 1413817.98 1 814.4 1 4.0 1 34.0 1 22.9 1 24.0 to 34.0 SAP/PWR 2.0 Sch. 40 PVC CLF22-307R 1 6/25/2024 1 684435.19 1 1413298.66 1 804.3 1 3.2 1 28.9 1 21.8 1 18.9 to 28.9 SAP/PWR 2.0 Sch. 40 PVC Notes: 1 Northing and Easting coordinates measured by S&ME personnel with a GPS unit in the field 2 Ground Surface Elevation measured by S&ME personnel with a GPS unit in the field 3 Depth to Water measured in each well on 6/27/2024 4 Monitoring well screens consist of sch. 40 PVC 0.010-inch machine -slotted pipe (pre -packed) 5 SAP - Saprolite, PWR - Partially Weathered Rock ft: feet NAD83: North American Datum 1983 MSL: Mean Sea Level ags: above ground surface toc: top of casing bgs: below ground surface in: inches Sch. 40 PVC: Schedule 40 Polyvinyl Chloride Attachment III - Well Abandonment and Construction Records (GW-30 and GW-1 Forms) WELL ABANDONMENT RECORD 1. Well Contractor Information: Justin Marlowe Well Contractor Name (or well owner personally abandoning well on his/her property) 4452-A NC Well Contractor Certification Number Phenom Geotech Company Name 2. Well Construction Permit #: Not Applicable List all applicable well construction permits (i.e. UIC, County, State, Variance, etc) ifknown 3. Well use (check well use): Water Supply Well: ❑Agricultural ❑Municipal/Public ❑Geothermal (Heating/Cooling Supply) ❑Residential Water Supply (single) ❑Industrial/Commercial ❑Residential Water Supply (shared) ❑Irriation Non -Water Supply Well: RMonitoring ❑Recovery Injection Well: El Aquifer Recharge ❑Groundwater Remediation El Aquifer Storage and Recovery El Salinity Barrier El Aquifer Test ❑Stormwater Drainage ❑Experimental Technology ❑Subsidence Control ❑Geothermal (Closed Loop) ❑Tracer ❑Geothermal (Heating/Cooling Return) ❑Other (explain under 7g) 4. Date well(s) abandoned: 6/26/2024 5a. Well location: Duke Energy Carolinas Not Applicable Facility/Owner Name Facility ID# (if applicable) 8320 NC Hwy 150, Terrell, NC 28673 Physical Address, City, and Zip Catawba 461803426350 County Parcel Identification No. (PIN) 5b. Latitude and longitude in degrees/minutes/seconds or decimal degrees: (if well field, one lat/long is sufficient) 35.61623290 N-080.97265500 W CONSTRUCTION DETAILS OF WELL(S) BEING ABANDONED Attach well construction record(s) ifavailable. For multiple injection or non -water supply wells ONLY with the same construction/abandonment, you can submit one form. 6a. Well ID#: CLF22-306 6b. Total well depth: 25.0 (ft.) 6c. Borehole diameter: 6.0 (in.) 6d. Water level below ground surface: 23.4 (ft.) 6e. Outer casing length (if known): Not Applicable (ft.) 6f. Inner casing/tubing length (if known): 1 5. 0 (ft.) 6g. Screen length (if known): 1 0.0 (ft.) For Internal Use ONLY: WELL ABANDONMENT DETAILS 7a. For Geoprobe/DPT or Closed -Loop Geothermal Wells having the same well construction/depth, only I GW-30 is needed. Indicate TOTAL NUMBER of wells abandoned: Not Applicable 7b. Approximate volume of water remaining in well(s): 0. 3 (gal.) FOR WATER SUPPLY WELLS ONLY: 7c. Type of disinfectant used: 7d. Amount of disinfectant used: 7e. Sealing materials used (check all that apply): ❑ Neat Cement Grout N Bentonite Chips or Pellets ❑ Sand Cement Grout ❑ Concrete Grout ❑ Specialty Grout ❑ Bentonite Slurry ❑ Dry Clay ❑ Drill Cuttings ❑ Gravel ❑ Other (explain under 7g) 7f. For each material selected above, provide amount of materials used: 45 pounds coated bentonite pellets 7g. Provide a brief description of the abandonment procedure: Coated bentonite pellets were slowly poured into the well, and water was added to hydrate the pellets, until it reached the top of PVC casing. 8. Certification: - 7/19/2024 StgnaturcofCr:niScdWcllCantractororWcl]awna Date By signing this form, I hereby certify that the well(s) was (were) abandoned in accordance with 15A NCAC 02C .0100 or 2C .0200 Well Construction Standards and that a copy of this record has been provided to the well owner. 9. Site diagram or additional well details: You may use the back of this page to provide additional well site details or well abandonment details. You may also attach additional pages if necessary. SUBMITTAL INSTRUCTIONS 10a. For All Wells: Submit this form within 30 days of completion of well abandonment to the following: Division of Water Resources, Information Processing Unit, 1617 Mail Service Center, Raleigh, NC 27699-1617 10b. For Iniection Wells: In addition to sending the form to the address in 10a above, also submit one copy of this form within 30 days of completion of well abandonment to the following: Division of Water Resources, Underground Injection Control Program, 1636 Mail Service Center, Raleigh, NC 27699-1636 loc. For Water Supply & Iniection Wells: In addition to sending the form to the address(es) above, also submit one copy of this form within 30 days of completion of well abandonment to the county health department of the county where abandoned. Form GW-30 North Carolina Department of Environmental Quality - Division of Water Resources Revised 2-22-2016 WELL ABANDONMENT RECORD 1. Well Contractor Information: Justin Marlowe Well Contractor Name (or well owner personally abandoning well on his/her property) 4452-A NC Well Contractor Certification Number Phenom Geotech Company Name 2. Well Construction Permit #: Not Applicable List all applicable well construction permits (i.e. UIC, County, State, Variance, etc) ifknown 3. Well use (check well use): Water Supply Well: ❑Agricultural ❑Municipal/Public ❑Geothermal (Heating/Cooling Supply) ❑Residential Water Supply (single) ❑Industrial/Commercial ❑Residential Water Supply (shared) ❑Irriation Non -Water Supply Well: RMonitoring ❑Recovery Injection Well: El Aquifer Recharge ❑Groundwater Remediation El Aquifer Storage and Recovery El Salinity Barrier El Aquifer Test ❑Stormwater Drainage ❑Experimental Technology ❑Subsidence Control ❑Geothermal (Closed Loop) ❑Tracer ❑Geothermal (Heating/Cooling Return) ❑Other (explain under 7g) 4. Date well(s) abandoned: 6/26/2024 5a. Well location: Duke Energy Carolinas Not Applicable Facility/Owner Name Facility ID# (if applicable) 8320 NC Hwy 150, Terrell, NC 28673 Physical Address, City, and Zip Catawba 461803426350 County Parcel Identification No. (PIN) 5b. Latitude and longitude in degrees/minutes/seconds or decimal degrees: (if well field, one lat/long is sufficient) 35.61485080 N-080.9743201 ° W CONSTRUCTION DETAILS OF WELL(S) BEING ABANDONED Attach well construction record(s) ifavailable. For multiple injection or non -water supply wells ONLY with the same construction/abandonment, you can submit one form. 6a. Well ID#: CLF22-307 6b. Total well depth: 40.0 (ft.) 6c. Borehole diameter: 6.0 (in.) 6d. Water level below ground surface: 34.5 (ft.) 6e. Outer casing length (if known): Not Applicable (ft.) 6f. Inner casing/tubing length (if known): 30.0 (ft.) 6g. Screen length (if known): 1 0.0 (ft.) For Internal Use ONLY: WELL ABANDONMENT DETAILS 7a. For Geoprobe/DPT or Closed -Loop Geothermal Wells having the same well construction/depth, only I GW-30 is needed. Indicate TOTAL NUMBER of wells abandoned: Not Applicable 7b. Approximate volume of water remaining in well(s): 0. 9 (gal.) FOR WATER SUPPLY WELLS ONLY: 7c. Type of disinfectant used: 7d. Amount of disinfectant used: 7e. Sealing materials used (check all that apply): ❑ Neat Cement Grout N Bentonite Chips or Pellets ❑ Sand Cement Grout ❑ Concrete Grout ❑ Specialty Grout ❑ Bentonite Slurry ❑ Dry Clay ❑ Drill Cuttings ❑ Gravel ❑ Other (explain under 7g) 7f. For each material selected above, provide amount of materials used: 68 pounds coated bentonite pellets 7g. Provide a brief description of the abandonment procedure: Coated bentonite pellets were slowly poured into the well, and water was added to hydrate the pellets, until it reached the top of PVC casing. 8. Certification: - 7/19/2024 StgnaturcofCr:niScdWcllCantractororWcl]awna Date By signing this form, I hereby certify that the well(s) was (were) abandoned in accordance with 15A NCAC 02C .0100 or 2C .0200 Well Construction Standards and that a copy of this record has been provided to the well owner. 9. Site diagram or additional well details: You may use the back of this page to provide additional well site details or well abandonment details. You may also attach additional pages if necessary. SUBMITTAL INSTRUCTIONS 10a. For All Wells: Submit this form within 30 days of completion of well abandonment to the following: Division of Water Resources, Information Processing Unit, 1617 Mail Service Center, Raleigh, NC 27699-1617 10b. For Iniection Wells: In addition to sending the form to the address in 10a above, also submit one copy of this form within 30 days of completion of well abandonment to the following: Division of Water Resources, Underground Injection Control Program, 1636 Mail Service Center, Raleigh, NC 27699-1636 loc. For Water Supply & Iniection Wells: In addition to sending the form to the address(es) above, also submit one copy of this form within 30 days of completion of well abandonment to the county health department of the county where abandoned. Form GW-30 North Carolina Department of Environmental Quality - Division of Water Resources Revised 2-22-2016 WELL CONSTRUCTION RECORD (GW-1) For Internal Use Only: 1. Well Contractor Information: Justin Marlowe Well Contractor Name 4452-A NC Well Contractor Certification Number Pheom Geotech Company Name 2. Well Construction Permit #:Not Applicable List all applicable well construction permits (i. e. UIC, County, State, Variance, etc.) 3. Well Use (check well use): Water Supply Well: ❑Agricultural ❑Municipal/Public ❑Geothermal (Heating/Cooling Supply) El Residential Water Supply (single) ❑Industrial/Commercial ❑Residential Water Supply (shared) ❑Ini ation ❑Wells>100,000GPD Non -Water Supply Well: OMonitoring ❑Recovery Injection Well: ❑Aquifer Recharge ❑Groundwater RemediatiolRemarks) El Aquifer Storage and Recovery El Salinity Barrier El Aquifer Test ❑Stormwater Drainage ❑Experimental Technology El Subsidence Control ❑Geothermal (Closed Loop) ❑Tracer ❑Geothermal (Heating/Cooling Return)❑Other (explain under #21 4. Date Well(s) Completed: 6/26/2024 Well ID# CLF22-306R 5a. Well Location: Duke Energy Carolinas Not Applicable Facility/Owner Name Facility ID# (if applicable) 8320 NC Hwy 150, Terrell, NC 28673 Physical Address, City, and Zip Catawba 461803426350 County Parcel Identification No. (PIN) 5b. Latitude and longitude in degrees/minutes/seconds or decimal degrees: (if well field, one lat/long is sufficient) 35.616154 N-80.972432 W 6. Is(are) the well(s): InPermanent or []Temporary 7. Is this a repair to an existing well: ❑Yes or [INo If this is a repair, fill out known well construction information and explain the nature of the repair under #21 remarks section or on the back of this form. 8. For Geoprobe/DPT or Closed -Loop Geothermal Wells having the same construction, only 1 GW-1 is needed. Indicate TOTAL NUMBER of wells drilled: Not Applicable 9. Total well depth below land surface: 34.0 (ft.) For multiple wells list all depths if different (example- 3@200' and 2@100) 10. Static water level below top of casing: 26.9 (ft.) If water level is above casing, use `•+" 11. Borehole diameter: 7.0 (in.) 12. Well construction method: Hollow Stem Auger (i.e. auger, rotary, cable, direct push, etc.) 14. WATER ZONES FROM TO DESCRIPTION N/A ft• N/A ft N/A fr. rt. 15. OUTER CASING (for multi -cased wells) OR LINER (if applicable) FROM I TO DIAMETER F THICKNESS I MATERIAL N/A ft. I N/A ft. I N/A in- I N/A I N/A 16. INNER CASING OR TUBING (geothermal closed -loop) FROM TO DIAMETER THICKNESS I MATERIAL N/A fr. N/A ft. N/A in' N/A N/A ft. ft. in. 17. SCREEN FROM TO DIAMETER SLOT SIZE THICKNESS MATERIAL 24.0 ff 34.0 ft• 2.0 in' 0.010 sch. 40 PVC ft. ft. in. 18. GROUT FROM TO MATERIAL EMPLACEMENT METHOD & AMOUNT 0.0 ft• 20.0 ft• neat cement grout pour -25 gallons 20.0 ft• 22.0 ft• bentonite pellets pour -20 pounds ft. ft. 19. SAND/GRAN, Ft, PACK (if applicable) FROM TO MATERIAL EMPLACEMENT METHOD 22.0 ft• 34.3 ft• no. 2 filter sand pour ft. ft. 20. DRILLING LOG (attach additional sheets if necessary) FROM TO DESCRIPTION (color, hardness, soil/rock type, grain size, etc.) 0.0 ft- 15.0 ft- Sandy Silt (ML) - brownish red, non -plastic, fine ft. ft. to medium sand, micaceous [Residual] 15.0 rt• 29 0 ft. Silt (ML) - brown to yellowish brown, non- rt. rt. plastic, few fine sand, micaceous [Saprolite] 29.0 rt• 34.3 rt• Silty Sand (SM) - yellowish brown, pale red, ft. rt. white, fine to coarse, non -plastic fines, ft. ft. micaceous [Partially Weathered Rock] 21. REMARKS 22. Certification- " Signelurc of Certified Well Contractor or WCIJOwmcr 7/19/2024 Date By signing this form, I hereby certify that the well(s) was (were) constructed in accordance with 15A NCAC 02C .0100 or 15A NCAC 02C .0200 Well Construction Standards and that a copy of this record has been provided to the well owner. 23. Site diagram or additional well details: You may use the back of this page to provide additional well construction info (add'See Over' in Remarks Box). You may also attach additional pages if necessary. 24. SUBMITTAL INSTRUCTIONS Submit this GW-1 within 30 days of well completion per the following: 24a. For All Wells: Original form to Division of Water Resources (DWR), Information Processing Unit, 1617 MSC, Raleigh, NC 27699-1617 24b. For Injection Wells: Copy to DWR, Underground Injection Control (NC) Program, 1636 MSC, Raleigh, NC 27699-1636 24c. For Water Supply and Open -Loop Geothermal Return Wells: Copy to the county environmental health department of the county where installed FOR WATER SUPPLY WELLS ONLY: 24d. For Water Wells producing over 100,000 GPD: Copy to DWR, CCPCUA 13a. Yield (gpm) Method of test: Permit Program, 1611 MSC, Raleigh, NC 27699-1611 13b. Disinfection type: Amount: Form GW-1 North Carolina Department of Environmental Quality - Division of Water Resources Revised 6-6-2018 Monitoring Well Construction Form III a S&ME Project: Marshall Well Replacements Project Number: 21410007, Ph. 02 Driller/Company: Justin Marlowe/Phenom Geotech Well Installation Method: Hollow Stem Augers WELL NO. CLF22-306R Drill Rig: Mobile B-57 (tracked) Borehole Diameter (in.): 7.0 Start Date: 6/26/24 Northing (ft): 685002.97 Easting (ft): 1413817.98 Reference Point for Measurements: Below Ground Surface (BGS) Completion Date: 6/26/24 Depth to Water (ft. BGS): 22.9 Date: 6/27/24 Height of casing stick-up above ground surface (ft): 4.0 DEPTH Height of concrete pad above ground surface (in): 2.0 (in feet) Concrete pad thickness (in): 4.0 Ground Surface (Elevation 814.4') 0 Protective Surface Casing Size (in): 4 x 4 Type: Steel Bottom of Protective Surface Casing 1.0 Backfill Material Riser Casing Type: neat cement grout Type: sch. 40 PVC Dia (in): 2 Top of Annular Seal 20.0 Annular Seal Type: bentonite pellets Top of Filter Pack 22.0 Top of Screen 24.0 Screen Type Dia (in): 2 Filter Pack Type: sch. 40 PVC (pre -packed) Type: no. 2 filter sand Slot (in): 0.010 Bottom of Screen 34.0 Bottom of Sump I 34.3 Bottom of Hole I 34.3 WELL CONSTRUCTION RECORD (GW-1) For Internal Use Only: 1. Well Contractor Information: Justin Marlowe Well Contractor Name 4452-A NC Well Contractor Certification Number Pheom Geotech Company Name 2. Well Construction Permit #:Not Applicable List all applicable well construction permits (i. e. UIC, County, State, Variance, etc.) 3. Well Use (check well use): Water Supply Well: ❑Agricultural ❑Municipal/Public ❑Geothermal (Heating/Cooling Supply) El Residential Water Supply (single) ❑Industrial/Commercial ❑Residential Water Supply (shared) ❑Ini ation ❑Wells>100,000GPD Non -Water Supply Well: OMonitoring ❑Recovery Injection Well: ❑Aquifer Recharge ❑Groundwater RemediatiolRemarks) El Aquifer Storage and Recovery El Salinity Barrier El Aquifer Test ❑Stormwater Drainage ❑Experimental Technology El Subsidence Control ❑Geothermal (Closed Loop) ❑Tracer ❑Geothermal (Heating/Cooling Return)❑Other (explain under #21 4. Date Well(s) Completed: 6/25/2024 Well ID# CLF22-307R 5a. Well Location: Duke Energy Carolinas Not Applicable Facility/Owner Name Facility ID# (if applicable) 8320 NC Hwy 150, Terrell, NC 28673 Physical Address, City, and Zip Catawba 461803426350 County Parcel Identification No. (PIN) 5b. Latitude and longitude in degrees/minutes/seconds or decimal degrees: (if well field, one lat/long is sufficient) 35.614566 N-80.974141 W 6. Is(are) the well(s): InPermanent or ❑Temporary 7. Is this a repair to an existing well: ❑Yes or IlNo If this is a repair, fill out known well construction information and explain the nature of the repair under #21 remarks section or on the back of this form. 8. For Geoprobe/DPT or Closed -Loop Geothermal Wells having the same construction, only 1 GW-1 is needed. Indicate TOTAL NUMBER of wells drilled: Not Applicable 9. Total well depth below land surface: 28.9 (ft.) For multiple wells list all depths if different (example- 3@200' and 2@100) 10. Static water level below top of casing: 25.0 (ft.) If water level is above casing, use `•+" 11. Borehole diameter: 7.0 (in.) 12. Well construction method: Hollow Stem Auger (i.e. auger, rotary, cable, direct push, etc.) 14. WATER ZONES FROM TO DESCRIPTION N/A ft N/A rt N/A fr. rt. 15. OUTER CASING (for multi -cased wells) OR LINER (if applicable) FROM I TO DIAMETER F THICKNESS I MATERIAL N/A ft. I N/A ft. I N/A in- I N/A I N/A 16. INNER CASING OR TUBING (geothermal closed -loop) FROM TO DIAMETER THICKNESS I MATERIAL N/A ft. N/A ft. N/A in' N/A N/A ft. ft. in. 17. SCREEN FROM TO DIAMETER SLOT SIZE THICKNESS MATERIAL 18 9 ft. 28.9 rt. 2.0 in' 0.010 sch. 40 PVC fr. ft. in. 18. GROUT FROM TO MATERIAL EMPLACEMENT METHOD & AMOUNT 0.0 fr• 15.0 fr• neat cement grout pour -19 gallons 15.0 fr• 17.0 fr• bentonite pellets pour -20 pounds ft. ft. 19. SAND/GRAVFt, PACK (if a livable) FROM TO MATERIAL EMPLACEMENT METHOD 17.0 ft• 29 2 ft' no. 2 filter sand pour ft. ft. 20. DRILLING LOG (attach additional sheets if necessary) FROM TO DESCRIPTION (color, hardness, soil/rock type, grain size, etc.) 0.0 ft' 7.5 ft- Silty Sand (SM) - reddish brown, medium, non -plastic fines, micaceous [RES] 7.5 ft' 16.0 ft' Sandy Silt (ML) - brownish red, white, non -plastic, ft. ft- fine to coarse sand, micaceous [Saprolite] 16.0 ft' 20.0 ft' Silty Sand (SM) - yellowish brown, white, red, medium to coarse, ft. ft. non -plastic fines, micaceous [Partially Weathered Rock] 20.0 1` 28.5 IL Well Graded Sand with Silt (SW-SM) - light brown, ft. ft. medium, non -plastic fines, micaceous [Saprolite] 21. REMARKS 28.5 to 29.2 - Same description as 20.0 to 28.5 interval, observed as Partially Weathered Rock 22. Certificatian, Signature Of Certified Well Contractor or Weil Owner 7/19/2024 Date By signing this form, I hereby certify that the well(s) was (were) constructed in accordance with 15A NCAC 02C .0100 or 15A NCAC 02C .0200 Well Construction Standards and that a copy of this record has been provided to the well owner. 23. Site diagram or additional well details: You may use the back of this page to provide additional well construction info (add'See Over' in Remarks Box). You may also attach additional pages if necessary. 24. SUBMITTAL INSTRUCTIONS Submit this GW-1 within 30 days of well completion per the following: 24a. For All Wells: Original form to Division of Water Resources (DWR), Information Processing Unit, 1617 MSC, Raleigh, NC 27699-1617 24b. For Injection Wells: Copy to DWR, Underground Injection Control (NC) Program, 1636 MSC, Raleigh, NC 27699-1636 24c. For Water Supply and Open -Loop Geothermal Return Wells: Copy to the county environmental health department of the county where installed FOR WATER SUPPLY WELLS ONLY: 24d. For Water Wells producing over 100,000 GPD: Copy to DWR, CCPCUA 13a. Yield (gpm) Method of test: Permit Program, 1611 MSC, Raleigh, NC 27699-1611 13b. Disinfection type: Amount: Form GW-1 North Carolina Department of Environmental Quality - Division of Water Resources Revised 6-6-2018 Monitoring Well Construction Form III a S&ME Project: Marshall Well Replacements Project Number: 21410007, Ph. 02 Driller/Company: Justin Marlowe/Phenom Geotech Well Installation Method: Hollow Stem Augers WELL NO. CLF22-307R Drill Rig: Mobile B-57 (tracked) Borehole Diameter (in.): 7.0 Start Date: 6/25/24 Northing (ft): 684435.19 Easting (ft): 1413298.66 Reference Point for Measurements: Below Ground Surface (BGS) Completion Date: 6/25/24 Depth to Water (ft. BGS): 21.8 Date: 6/27/24 Height of casing stick-up above ground surface (ft): 3.2 DEPTH Height of concrete pad above ground surface (in): 2.0 (in feet) Concrete pad thickness (in): 4.0 Ground Surface (Elevation 8043) 0 Protective Surface Casing Size (in): 4 x 4 Type: Steel Bottom of Protective Surface Casing 1.8 Backfill Material Riser Casing Type: neat cement grout Type: sch. 40 PVC Dia (in): 2 Top of Annular Seal 15.0 Annular Seal Type: bentonite pellets Top of Filter Pack 17.0 Top of Screen 18.9 Screen Type Dia (in): 2 Filter Pack Type: sch. 40 PVC (pre -packed) Type: no. 2 filter sand Slot (in): 0.010 Bottom of Screen 28.9 Bottom of Sump I 29.2 Bottom of Hole I 29.2 Attachment IV - Boring Logs PROJECT: Marshall Well Replacements BORING LOG: CLF22-306R Terrell, North Carolina S&ME Project No. 21410007, Ph. 02 Sheet 1 of 1 DATE: 06/26/2024 ELEVATION: 814 ft NOTES: Soils visually classified from auger cuttings. No soil samples collected. EQUIPMENT: Mobile B57 DATUM: NAVD88 OPERATOR: Justin Marlowe DEPTH: 34.3 ft HAMMER TYPE: Not Applicable CLOSURE: Installed Observation Well NORTHING: 684435.2 EASTING: 1413298.7 DRILLING METHOD: 4-1/4" HSA LOGGED BY: J. Tayouga SAMPLING METHOD: N/A PROJECT COORDINATE SYSTEM - NAD 1983 StatePlane North Carolina FiPS 320o Feet r — a v NOTES O 2 � z = a SAMPLE NO. BLOW COUNT O a v 0 (RECOVERY) MATERIAL DESCRIPTION DATA Well Details a ; (SPT N-value) W Z � W W 0 SANDY SILT (ML), brownish red, non - plastic fines, fine to medium grained sand, micaceous [RES] 810 5 E a)805 10 Neat Cement Grout (0.0' - 20.0' ) 15.0 800 15 SILT (ML), brown to yellowish brown, non - plastic fines, few fine grained sand, micaceous [SAP] 795 20 Bentonite Seal (20.0' - 22.0') 2 o. Vo 790 25 29 0 No. 2 Filter Sand (22.0' - Rig 34.3') 785 SILTY SAND (SM), yellowish brown, pale 30 chatter red and white, fine to coarse grained sand, Screened Interval 3 d non -plastic fines, micaceous [PWR] (189' - 289') 34.3 35 Auger 780 Bore Hole terminated at 34.3 feet. refusal at 34.3 feet 775 40 GROUNDWATER DATE DEPTH(FT) REMARKS ATD 4 06/26/2024 25.0 END OF DRILLING SIF AFTER DRILLING = 06/27/2024 22.9 AFTER DRILLING = E I I GROUNDWATER DEPTHS ARE NOT EXACT AND MAY VARY SUBSTANTIALLY FROM THOSE INDICATED. ATD = AT TIME OF DRILLING LL=Liquid Limit, PL = Plastic Limit, NMC = Natural Moisture Content, PPV = Pocket Penetrometer (tsf), PTV = Pocket Torvane (tsf) PROJECT: Marshall Well Replacements BORING LOG: CLF22-307R Terrell, North Carolina S&ME Project No. 21410007, Ph. 02 Sheet 1 of 1 DATE: 06/26/2024 ELEVATION: 804 ft NOTES: Soils visually classified from auger cuttings. No soil samples collected. EQUIPMENT: Mobile B57 DATUM: NAVD88 OPERATOR: Justin Marlowe DEPTH: 29.2 ft HAMMER TYPE: Not Applicable CLOSURE: Installed Observation Well NORTHING: 685003.0 EASTING: 1413818.0 DRILLING METHOD: 4-1/4" HSA LOGGED BY: J. Tayouga SAMPLING METHOD: N/A PROJECT COORDINATE SYSTEM - NAD 1983 statePlane North Carolina FiPS 320o Feet r — a v v NOTES O 2 � z = a SAMPLE NO. MATERIAL DESCRIPTION BLOW COUNT DATA Well Details O a 0 a ; (RECOVERY) (SPT N-value) W Z � W W 0 SILTY SAND (SM), reddish brown to red, medium grained sand, non -plastic fines, E micaceous [RES] � 800 5 7.5 Neat Cement Grout (0.0' - SANDY SILT (ML), brownish red, white, 15.0') non -plastic fines, fine to coarse grained 795 10 v sand, micaceous [SAP] 0 Q vn 790 15 16.0 Rig Bentonite Seal (15.0' - 17.0') SILTY SAND (SM), yellowish brown, white, chatter/ red, medium to coarse grained sand, non - hard plastic fines, micaceous [PWR] drilling 20.0 785 20 (16.0' WELL -GRADED SAND WITH SILT (SW-SM), 20.0') brown, fine to coarse grained sand, non - plastic fines, micaceous [SAP] EZ No. 2 Filter Sand (17.0' - 0 292) 780 25 Q ; V) o Screened Interval (24.0' - 34.0') 28.5 29.2 775 a WELL -GRADED SAND WITH SILT (SW-SM), 30 Auger brown, fine to coarse grained sand, non - refusal plastic fines, micaceous [PWR] at 29.2 Bore Hole terminated at 29.2 feet. feet 770 35 765 40 GROUNDWATER DATE DEPTH(FT) REMARKS ATD 4 06/26/2024 23.2 END OF DRILLING SIF AFTER DRILLING = 06/26/2024 21.8 AFTER DRILLING = E I I GROUNDWATER DEPTHS ARE NOT EXACT AND MAY VARY SUBSTANTIALLY FROM THOSE INDICATED. ATD = AT TIME OF DRILLING LL=Liquid Limit, PL = Plastic Limit, NMC = Natural Moisture Content, PPV = Pocket Penetrometer (tsf), PTV = Pocket Torvane (tsf) Attachment V — Well Development Forms WELL DEVELOPMENT FORM Project Name: Marshall Well Replacements (June 2024) 5&ME Project No. 21410007, Ph. 02 Well ID: CLF-306R Well Depth: 38.0 ft-btoc Well Volume: 1.8 gal. Development Date: 6/27/2024 Well Diameter: 2.0 inches Screen Length: 10.0 ft. Equipment used for Development: Whale pump 3/8" poly tubing Electronic water level meter Turbidity Meter Static Water Level: 26.9 ft-btoc Total Purge Volume: 4.0 gal. Weather Conditions: Intermittent rain, 85' General Development Method(s): Placed pump approximately 1-foot off bottom of well. Moved pump up and down during pumping to increase agitation and removal of silt/soil particles. Date Time Method of Well Evacuation Purge Volume (gal) Pumping Rate (gal/min) Comments (e.g. clarity of water and success of development) 6/27/2024 10:00 Pump 2 -1 Slightly turbid at start of pumping, cleared up before going dry. Dry after approximately 2 gallons pumped at 10:02. 6/27/2024 10:20 Pump 2 1 Recharged to 26.0 ft-btoc after 20 minutes, pumped 2 minutes before going dry. Water was clear. Turbidity measured at 78.4 NTU during second round of pumping Notes: ft-btoc Feet below top of casing gal. Gallons ft. Feet WELL DEVELOPMENT FORM �. Project Name: Marshall Well Replacements (June 2024) 5&ME Project No. 21410007, Ph. 02 Well ID: CLF-307R Well Depth: 32.1 ft-btoc Well Volume: 1.2 gal. Development Date: 6/26/2024 Well Diameter: 2.0 inches Screen Length: 10.0 ft. Equipment used for Development: Whale pump 3/8" poly tubing Electronic water level meter Turbidity Meter Static Water Level: 25.0 ft-btoc Total Purge Volume: 3.5 gal. Weather Conditions: Sunny, 99' General Development Method(s): Placed pump approximately 1-foot off bottom of well. Moved pump up and down during pumping to increase agitation and removal of silt/soil particles. Date Time Method of Well Evacuation Purge Volume (gal) Pumping Rate (gal/min) Comments (e.g. clarity of water and success of development) 6/26/2024 15:15 Pump 1.5 -1 Slightly turbid at start of pumping, cleared up before going dry. Dry after approximately 1.5 gallons pumped at 15:17 6/26/2024 15:45 Pump 1 —1 Recharged to 28.0 ft-btoc after 30 minutes, pumped dry again. Water was clear. Turbidity measured at 26.8 NTU during second round of pumping Notes: ft-btoc Feet below top of casing gal. Gallons ft. Feet