HomeMy WebLinkAboutWA-27532_38684_CA_SCH_20180319
EXECUTIVE SUMMARY
The Handy Mart 61 site is located at 4328 Highway 11 South in Winterville, Pitt County, North Carolina. The
property operates as a petroleum retail facility, convenience store and restaurant. The site is covered by concrete
and grass. An underground storage tank (UST) system consisting of one 20,000-gallon gasoline, one 12,000-
gallon gasoline, one 10,000-gallon diesel USTs and associated dispensers and product piping is currently in use at
the site.
On February 6, 2018, during annual compliance testing activities, a non-passing hydrostatic result was reported
for the 20,000-gallon gasoline UST spill bucket. Therefore a site check was required by NCDEQ.
On March 2, 2018, GRI conducted a site check in the area of the 20,000-gallon gasoline UST spill bucket. One
soil boring (SB-1) was advanced to approximately 2 feet below grade at the end of the tank, adjacent to the non-
passing spill bucket. A concentration of TPH-GRO that exceeded the Regulatory Action Level was reported in
the soil sample collected from SB-1 (2’). Based on this information, GRI recommends that a Limited Site
Assessment should be conducted for the site.
TABLE OF CONTENTS
A. SITE HISTORY AND CHARACTERIZATION .................................................................................. 1
B. SITE CHECK PROCEDURES ................................................................................................................ 1
C. SITE INVESTIGATION .......................................................................................................................... 2
D. SUMMARY AND CONCLUSIONS ........................................................................................................ 2
E. LIMITATIONS .......................................................................................................................................... 3
FIGURES
Figure 1: Site Location Map
Figure 2: Site Map
Figure 3: Soil Quality Map
TABLES
Table 1: UST Owner/Operator Information
Table 2: UST System Information
Table 3: Summary of Soil Sample Analytical Results
APPENDICES
Appendix A: Subsurface Logs
Appendix B: Laboratory Report – Soil Samples
1
A. SITE HISTORY AND CHARACTERIZATION
1. UST Owner and Operator Information:
In accordance with the Site Check Report guidelines, the underground storage tank (UST) owner and operator
information has been summarized in the attached Table 1.
2. UST System Information:
In accordance with the Site Check Report guidelines, the UST system information has been summarized in the
attached Table 2.
3. Non-UST Information:
There are currently no above ground petroleum storage tanks (ASTs) and no known ASTs formerly at the site.
4. Comprehensive Description of the Release:
Annual compliance testing was completed on February 6, 2018. Based on the testing, non-passing hydrostatic
results were reported for the 20,000-gallon gasoline UST spill bucket. The non-passing spill bucket was repaired
subsequently and received passing compliance test results on February 28, 2018. A site check was required
according to the North Carolina Department of Environmental Quality (NCDEQ). On March 2, 2018, one soil
boring (SB-1) was advanced approximately 2 feet below ground surface (bgs) at the end of the tank, adjacent to
the non-passing spill bucket. A release at the site was discovered upon receipt of the laboratory results for the
soil sample collected in March 2018.
5. Description of the Site Characteristics:
The Handy Mart 61 site is located at 4328 Highway 11 South in Winterville, Pitt County, North Carolina (Figure
1). The property operates as a petroleum retail facility, convenience store and restaurant. There are one 20,000-
gallon gasoline, one 12,000-gallon gasoline, and one 10,000-gallon diesel USTs currently in use at the site along
with associated dispensers and product piping. The surrounding properties are commercial and residential. A
Site Map has been included as Figure 2.
B. SITE CHECK PROCEDURES
1. Results of Tank and Line Tightness Testing:
On February 6, 2018, one non-passing UST spill bucket was reported at the site. The non-passing spill bucket
was repaired and received passing compliance test results on February 28, 2018.
2. Summary of Site Check Procedure:
GRI performed a site check on March 2, 2018, that included the collection of one soil sample at the spill bucket
associated with the 20,000-gallon gasoline UST. The soil boring was advanced adjacent to the spill bucket to a
depth of approximately 2 feet bgs. One soil sample (SB-1 (2’)) was collected from the terminus of the boring. A
2
soil boring log is provided as Appendix B.
3. Soil Excavation Activities:
No soil excavation activities were conducted.
C. SITE INVESTIGATION
1. Field Screening:
Soil samples collected during the March 2018 Site Check activities were not screened for volatile organic
compounds (VOCs).
2. Soil Sampling Information:
Soil sample SB-1 (2’) was collected on March 2, 2018, and submitted for laboratory analyses of gasoline-range
total petroleum hydrocarbons (TPH-GRO) by EPA Method 8015D. A concentration of TPH-GRO that exceeded
the Regulatory Action Level (RAL) was reported in the soil sample collected from SB-1 (2’). A soil sample
location map is presented as Figure 3. A summary of soil sample analytical results is presented in Table 3. A
complete laboratory report is provided as Appendix B.
3. Ground Water and Surface Water Sampling Information:
Ground water and surface water samples were not collected as part of the site check.
4. Quality-Control Measures:
Clean, disposable nitrile gloves were used for the collection of the soil sample. The samples were collected in
laboratory supplied containers and shipped to the laboratory in a cooler following proper chain-of-custody
procedures.
D. SUMMARY AND CONCLUSIONS
The site is commercial and surrounding properties are commercial and residential.
On February 6. 2018, non-passing hydrostatic result was reported for the 20,000-gallon gasoline UST
spill bucket. The non-passing spill bucket was repaired and received passing compliance test results on
February 28, 2018.
A Site Check was conducted on March 2, 2018, to determine if a petroleum release had occurred.
A concentration of TPH-GRO that exceeded the RAL was reported in the soil sample collected from
SB-1 (2’).
Based on this information, a release has occurred at the site. GRI recommends that a Limited Site
Assessment should be conducted for the site.
3
E. LIMITATIONS
This report has been prepared for the exclusive use of E. J. Pope & Son, Inc. for the specific application to the
referenced site in Pitt County, North Carolina. The assessment was conducted based on the scope of work and
level of effort specified by NCDEQ and with resources adequate only for that scope of work. Our findings have
been developed in accordance with generally accepted standards of geology and hydrogeology practices in the
State of North Carolina, available information, and our professional judgment. No other warranty is expressed or
implied.
The data that are presented in this report are indicative of conditions that existed at the precise locations sampled
and at the time the samples were collected. In addition, the data obtained from samples would be interpreted as
being meaningful with respect to parameters indicated in the laboratory report. No additional information can
logically be inferred from these data.
FIGURES
Copyright (C) 2009 MyTopo, 2006-2018 TomTom
SCALE 1:24000
0 1000 2000 3000 4000 5000
FEET
Declination
MN 9.90° W
MN
Location: 035.5431340° N 077.4054830° WDate: 03/16/18
Scale: 1 inch = 2,000 ft.
Copyright (C) 2009 MyTopo
Figure 1
Handy Mart 61
4328 Highway 11 South, Winterville, Pitt County, NC
Incident No. N/A
GRI Project No. 4735
TABLES
UST ID Number 1 - 3 Facility ID Number
Owner or Operator?
Owner/OperatorE. J. Pope & Son, Inc.06/01/2000 to Present
Address Telephone Number
Post Office Drawer 649, Mount Olive, North Carolina 28365 (919) 658-6566
TABLE 1
UST OWNER/OPERATOR INFORMATION
HANDY MART #61
0-036234
Name of Owner or Operator Dates of Ownership / Operation
Page 1 of 1
Was Release
Associated
with UST
System?
(Yes / No)
1 Diesel Diesel 10,000 06/01/00 Fiberglass 8' x 26' 6"Flex Current No
2 Gasoline Gasoline 12,000 06/01/00 Fiberglass 10' 6" x 18' 7"Flex Current No
3 Gasoline Gasoline 20,000 06/01/00 Unknown 10' 6" x 30' 11.5"Flex Current Yes
Notes:
• Data obtained from the NCDEQ registered tank database.
• FRP: Fiberglass Reinforced Plastic.
Construction
Details
Tank
Dimensions
Description of
Associated
Product Piping
and
Pumps
Status
of
UST
TABLE 2
UST SYSTEM INFORMATION
HANDY MART #61 (INCIDENT NO. PENDING)
Date: 03/16/18 Facility ID # : 0-036234
UST
ID
No.
Current
or Most
Recent
Contents
Previous
Contents
Capacity
(gallons)
Date
Installed
Page 1 of 1
Date: 03/14/18
5030/
8015D
3550/
8015C
50 100
NE NE
NE NE
SB-1 (2')03/02/18 2 191 NR
Notes:
• Results reported in mg/kg (milligrams per kilograms)
• ft-BGS: feet below ground surface.
• RAL: Regulatory Action Level.
• MCCs: Maximum Contaminant Concentrations.
• SCLs: Soil Cleanup Levels.
• < : Less than the method detection limit specified in the laboratory report
• Concentrations in bold face type exceeded the RALs.
• NE: Not Established
• NR: Not Requested.
TABLE 3
SUMMARY OF SOIL SAMPLE ANALYTICAL RESULTS
HANDY MART #61
INCIDENT NO. N/A
Facility ID #: 0-036234
RAL (mg/kg)
Soil to Water MCC (mg/kg)
Residential SCLs (mg/kg)
Analytical Method Sample IDDate Collected (mm/dd/yy)Sample Depth(ft-BGS)Gasoline-Range TPHDiesel-Range TPHPage 1 of 1
APPENDICES
APPENDIX A
Subsurface Logs
Geological Resources, Inc.Phone:(704) 845-4010
3502 Hayes Road Fax:(704) 845-4012
Monroe, NC 28110
SUBSURFACE LOG
Project Handy Mart 61 Project #4735
Address 4328 Highway 11 South, Winterville, Pitt County, NC 28590
Boring Number SB-1 Date Drilled
Sample Method Grab Drilling Method Hand Auger
Completion Details Completed to 2'; abandoned with soil cuttings & concrete subsequent to sampling
Driller Geological Resources, Inc.Log By Jimmy Hines
#
Lab Sample OVA
Depth Sample Interval(ft)ppm LITHOLOGY
0' - 0.67' Concrete
0
2 SB-1 2
4
6
8
10
12
14
16
18
20
22
24
26
28
30
32
34
36
38
40
03/02/18
0.67' - 2' Fine gray sand and gravel
Boring terminated at 2'.
APPENDIX B
Laboratory Report – Soil Samples
03/14/18
Technical Report for
GRI (Geological Resources Inc.)
Hardy Mart 61; 4328 Hwy 11 S, Winterville, NC
4735
SGS Job Number: FA52219
Sampling Date: 03/02/18
Report to:
GRI
3502 Hayes Rd
Monroe, NC 28110
wlr@geologicalresourcesinc.com; carriekennedy@geologicalresourcesinc.com;
jjr@geologicalresourcesinc.com; nml@geologicalresourcesinc.com
ATTN: William Regenthall
Total number of pages in report:
Certifications: FL(E83510), LA(03051), KS(E-10327), IL(200063), NC(573), NJ(FL002), NY(12022), SC(96038001)
DoD ELAP(ANAB L2229), AZ(AZ0806), CA(2937), TX(T104704404), PA(68-03573), VA(460177),
AK, AR, IA, KY, MA, MS, ND, NH, NV, OK, OR, UT, WA, WV
This report shall not be reproduced, except in its entirety, without the written approval of SGS.
Test results relate only to samples analyzed.
SGS North America Inc. • 4405 Vineland Road • Suite C-15 • Orlando, FL 32811 • tel: 407-425-6700 • fax: 407-425-0707
Test results contained within this data package meet the requirements
of the National Environmental Laboratory Accreditation Program
and/or state specific certification programs as applicable.
Client Service contact: Muna Mohammed 407-425-6700
Caitlin Brice, M.S.
General Manager
Orlando, FL 03/14/18
e-Hardcopy 2.0
Automated Report
13
SGS is the sole authority for authorizing edits or modifications to this document.
Unauthorized modification of this report is strictly prohibited.
Review standard terms at: http://www.sgs.com/en/terms-and-conditions
The results set forth herein are provided by SGS North America Inc.
Please share your ideas about
how we can serve you better at:
EHS.US.CustomerCare@sgs.com
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FA52219
Table of Contents
-1-
Sections:
Section 1: Sample Summary ...................................................................................................3
Section 2: Summary of Hits ....................................................................................................4
Section 3: Sample Results ........................................................................................................5
3.1: FA52219-1: SB-1 (2') ....................................................................................................6
Section 4: Misc. Forms ............................................................................................................7
4.1: Chain of Custody ...........................................................................................................8
Section 5: GC Volatiles - QC Data Summaries .....................................................................10
5.1: Method Blank Summary ................................................................................................11
5.2: Blank Spike Summary ...................................................................................................12
5.3: Matrix Spike/Matrix Spike Duplicate Summary ...........................................................13 123452 of 13
FA52219
SGS North America Inc.
Sample Summary
GRI (Geological Resources Inc.)
Job No:FA52219
Hardy Mart 61; 4328 Hwy 11 S, Winterville, NC
Project No: 4735
Sample Collected Matrix Client
Number Date Time By Received Code Type Sample ID
FA52219-1 03/02/18 08:45 JH 03/06/18 SO Soil SB-1 (2')
Soil samples reported on a dry weight basis unless otherwise indicated on result page.
3 of 13
FA522191
Summary of Hits Page 1 of 1
Job Number:FA52219
Account:GRI (Geological Resources Inc.)
Project:Hardy Mart 61; 4328 Hwy 11 S, Winterville, NC
Collected:03/02/18
Lab Sample ID Client Sample ID Result/
Analyte Qual RL MDL Units Method
FA52219-1 SB-1 (2')
TPH-GRO (C6-C10)191 29 14 mg/kg SW846 8015C
4 of 13
FA522192
SGS North America Inc.
Sample Results
Report of Analysis
Orlando, FL
Section 3
5 of 13
FA522193
SGS North America Inc.
Report of Analysis Page 1 of 1
Client Sample ID:SB-1 (2')
Lab Sample ID:FA52219-1 Date Sampled:03/02/18
Matrix:SO - Soil Date Received:03/06/18
Method:SW846 8015C Percent Solids:88.7
Project:Hardy Mart 61; 4328 Hwy 11 S, Winterville, NC
File ID DF Analyzed By Prep Date Prep Batch Analytical Batch
Run #1 UV082219.D 1 03/09/18 17:12 EG n/a n/a GUV4335
Run #2
Initial Weight Final Volume Methanol Aliquot
Run #1 5.55 g 5.0 ml 20.0 ul
Run #2
CAS No.Compound Result RL MDL Units Q
TPH-GRO (C6-C10)191 29 14 mg/kg
CAS No.Surrogate Recoveries Run# 1 Run# 2 Limits
460-00-4 4-Bromofluorobenzene 91%56-149%
98-08-8 aaa-Trifluorotoluene 87%66-132%
ND = Not detected MDL = Method Detection Limit J = Indicates an estimated value
RL = Reporting Limit B = Indicates analyte found in associated method blank
E = Indicates value exceeds calibration range N = Indicates presumptive evidence of a compound
6 of 13
FA5221933.1
SGS North America Inc.
Misc. Forms
Custody Documents and Other Forms
Includes the following where applicable:
• Chain of Custody
Orlando, FL
Section 4
7 of 13
FA522194
FA52219: Chain of Custody
Page 1 of 2
8 of 13
FA5221944.1
Job Number:FA52219 Client:GRI
Date / Time Received:3/6/2018 9:30:00 AM Delivery Method:FED EX
Project:4735
Airbill #'s:811062255113
Cooler Information
1. Custody Seals Present
2. Custody Seals Intact
4. Cooler temp verification
3. Temp criteria achieved
5. Cooler media
IR Gun
Ice (Bag)
Trip Blank Information
1. Trip Blank present / cooler
2. Trip Blank listed on COC
2. Samples preserved properly
Sample Information
1. Sample labels present on bottles
5. Sample recvd within HT
4. Condition of sample
3. Sufficient volume/containers recvd for analysis:
Intact
Comments
SM001Rev. Date 05/24/17
SGS Sample Receipt Summary
Cooler Temps (Raw Measured) °C:
Cooler Temps (Corrected) °C:
Cooler 1: (3.8);
Cooler 1: (4.2);
3. Type Of TB Received
W or S N/A
6. Dates/Times/IDs on COC match Sample Label
7. VOCs have headspace
8. Bottles received for unspecified tests
9. Compositing instructions clear
10. Voa Soil Kits/Jars received past 48hrs?
11. % Solids Jar received?
Misc. Information
25-Gram 5-GramNumber of Encores:1Number of 5035 Field Kits:Number of Lab Filtered Metals:
Test Strip Lot #s:pH 0-3 230315 pH 10-12 219813A Other: (Specify)
Y or N N/A
Y or N
Therm ID:IR 1; Therm CF:0.4; # of Coolers:1
Y or N N/A
12. Residual Chlorine Present?
Residual Chlorine Test Strip Lot #:
Technician:Reviewer:SHAYLAP Date:Date:3/6/2018 9:30:00 AM
FA52219: Chain of Custody
Page 2 of 2
9 of 13
FA5221944.1
SGS North America Inc.
GC Volatiles
QC Data Summaries
Includes the following where applicable:
• Method Blank Summaries
• Blank Spike Summaries
• Matrix Spike and Duplicate Summaries
Orlando, FL
Section 5
10 of 13
FA522195
Method Blank Summary Page 1 of 1
Job Number:FA52219
Account:GRINCC GRI (Geological Resources Inc.)
Project:Hardy Mart 61; 4328 Hwy 11 S, Winterville, NC
Sample File ID DF Analyzed By Prep Date Prep Batch Analytical Batch
GUV4335-MB UV082218.D 1 03/09/18 EG n/a n/a GUV4335
The QC reported here applies to the following samples:Method: SW846 8015C
FA52219-1
CAS No.Compound Result RL MDL Units Q
TPH-GRO (C6-C10)ND 5.0 2.5 mg/kg
CAS No.Surrogate Recoveries Limits
460-00-4 4-Bromofluorobenzene 94%56-149%
98-08-8 aaa-Trifluorotoluene 84%66-132%
11 of 13
FA5221955.1.1
Blank Spike Summary Page 1 of 1
Job Number:FA52219
Account:GRINCC GRI (Geological Resources Inc.)
Project:Hardy Mart 61; 4328 Hwy 11 S, Winterville, NC
Sample File ID DF Analyzed By Prep Date Prep Batch Analytical Batch
GUV4335-BS UV082217.D 1 03/09/18 EG n/a n/a GUV4335
The QC reported here applies to the following samples:Method: SW846 8015C
FA52219-1
Spike BSP BSP
CAS No.Compound mg/kg mg/kg %Limits
TPH-GRO (C6-C10)20 18.9 95 74-128
CAS No.Surrogate Recoveries BSP Limits
460-00-4 4-Bromofluorobenzene 96%56-149%
98-08-8 aaa-Trifluorotoluene 90%66-132%
* = Outside of Control Limits.
12 of 13
FA5221955.2.1
Matrix Spike/Matrix Spike Duplicate Summary Page 1 of 1
Job Number:FA52219
Account:GRINCC GRI (Geological Resources Inc.)
Project:Hardy Mart 61; 4328 Hwy 11 S, Winterville, NC
Sample File ID DF Analyzed By Prep Date Prep Batch Analytical Batch
FA52249-3MS UV082225.D 1 03/09/18 EG n/a n/a GUV4335
FA52249-3MSD UV082226.D 1 03/09/18 EG n/a n/a GUV4335
FA52249-3 UV082221.D 1 03/09/18 EG n/a n/a GUV4335
The QC reported here applies to the following samples:Method: SW846 8015C
FA52219-1
FA52249-3 Spike MS MS Spike MSD MSD Limits
CAS No.Compound mg/kg Q mg/kg mg/kg %mg/kg mg/kg %RPD Rec/RPD
TPH-GRO (C6-C10)5.7 U 22.7 24.7 109 22.7 23.7 104 4 74-128/17
CAS No.Surrogate Recoveries MS MSD FA52249-3 Limits
460-00-4 4-Bromofluorobenzene 99%94%89%56-149%
98-08-8 aaa-Trifluorotoluene 89%85%77%66-132%
* = Outside of Control Limits.
13 of 13
FA5221955.3.1