Loading...
HomeMy WebLinkAboutMO-3182_7570_CA_FPR_20200921_Free Product Recovery ReportSeptember 21, 2020 WBTV Television One Julian Price Place Charlotte, North Carolina Attention: Mr. Mike Gurthie Reference: Free Product Recovery Report Jefferson Pilot Communications Company NCDEQ Incident # 7570 Charlotte, North Carolina S&ME Project No. 4335-14-135A Dear Mr. Gurthie: S&ME, Inc. (S&ME) submits this Free Product Report in general accordance with our proposal No. 43-1900163 dated November 11, 2019, and as authorized by the North Carolina Department of Environmental Quality (NCDEQ) Task Authorization No. 7570-23 signed on November 11, 2019. The services were based on the NCDEQ issued Notice of Regulatory Requirements (NORR) on October 30, 2019, directing WBTV Television to continue free product recovery efforts. A site map indicating the locations of the monitoring wells is provided as Figure 1. A summary of historic free product and liquid levels are presented in the attached Table 1. Between November 13, 2019 and June 18, 2020, free product was observed in each of the wells gauged during one or more gauging events: MW-1 (June 18, 2020), and MW-2 (December 2019, January 2020, February, March, April, May and June 2, 2020). The free product recovery events conducted during this reporting period are summarized in the attached Table 2, with details regarding each recovery event provided in the attached Table 3. As can be seen in Tables 2 and 3, a total of approximately 0.36 gallon of free product was recovered via product adsorbent socks during this reporting period. Based on a review of historical data, the free product thicknesses are trending downward. Based on the presence of free product in monitoring wells MW-1 and MW-2, S&ME recommends that free product removal efforts be continued for a period of six months. Free product thicknesses will be measured in January 2020 to document the effectiveness of the absorbent socks. S&ME recommends that the next groundwater monitoring event be conducted approximately one month after the six months of free product removal efforts. S&ME, Inc. 19751 Southern Pine Boulevard I Charlotte, NC 28273 1 p 704.523.4726 1 www.smeinc.com a Free Product Recovery Report Jefferson Pilot ` ot Communications Company NCDEQ Incident # 7570 Charlotte, North Carolina S&ME Project No. 4335-14-135A If you have any questions concerning this report, please contact us at your convenience. Sincerely, SWE, Inc. _ C, •.� 6- SEAL r-: } Laura Beth Slagle David R. Loftis, P. 03 t^" Staff Professional Senior Engineer ���J1,, Itl1 cc: Ms. Trudy Beverly, NCDEQ DWM, UST Section, Mooresville Regional Office September 21, 2020 2 Attachments Attachment I — Figures -4 1 MW-1 EW-1 • MW-1 MW-10 MW-5 o � � it N O O = Y 4 O a - E 4 Nlf V 1 � w # 41 0 O 120 4 (FEET) a t REFERENCE: 2019 AERIAL PHOTOGRAPH a GIS BASE LAYERS WERE OBTAINED FROM MECKLENBURG COUNTY. THIS MAP IS FOR c INFORMATIONAL PURPOSES ONLY. ALL FEATURE LOCATIONS DISPLAYED ARE APPROXIMATED. THEY ARE NOT BASED ON CIVIL SURVEY INFORMATION, UNLESS STATED OTHERWISE. 0 SITE MAP III JEFFERSON PILOT COMMUNICATIONS 1 JULIAN PRICE PLACE CHARLOTTE, MECKLENBURG COUNTY, NC 14mr 2 T, ® MONITORING WELLS SCALE: FIGURE NO. 1"=60' DATE: 10-2-19 2 PROJECT NUMBER 4335-14-135A Attachment II — Tables Table 1 Summary of Historic Free Product and Liquid Levels Jefferson Pilot Communications Company (Incident No. 7570) One Julian Price Place, Charlotte, Mecklenburg County, NC S&ME Project No. 4335-14-135A Product Type: #2 Diesel Well # MW-1 Recovery None .. 08/12/05 47.80 48.70 0.90 10.80 Corrected 47.93 None 08/18/05 47.87 48.83 0.96 11.52 48.01 None 08/24/05 47.93 48.97 1.04 12.48 48.08 None 08/29/05 47.96 49.01 1.05 12.60 48.11 None 09/06/05 48.06 49.23 1.17 14.04 48.23 None 10/03/05 48.43 49.80 1.37 16.44 48.62 None 11/03/05 48.61 50.27 1.66 19.92 48.85 None 02/03/06 48.14 49.51 1.37 16.44 48.33 None 03/10/06 47.90 49.07 1.17 14.04 48.07 None 03/23/06 47.93 49.15 1.22 14.64 48.10 None 05/15/06 48.10 49.55 1.45 17.40 48.31 None 05/25/06 48.17 49.73 1.56 18.72 48.39 None 06/16/06 48.58 50.40 1.82 21.84 48.84 None 07/07/06 48.86 50.82 1.96 23.52 49.14 None 07/17/06 48.86 50.82 1.96 23.52 49.14 Bailing 08/18/06 49.29 51.53 2.24 26.88 49.61 Bailed approx 1 gallon of product/water None 06/19/07 47.21 48.43 1.22 14.64 47.38 Bailing 07/15/11 47.14 48.52 1.38 16.56 47.34 Bailed approx 0.2 gallon of product/water AFVR 11/29/11 47.37 48.61 1.24 14.88 47.55 Recovered 191 gallons of product total using MW- None 01/11/12 47.00 48.34 1.34 16.08 47.19 Product check following AFVR Event AFVR 04/05/12 49.37 51.00 1.63 19.56 49.60 Recovered 36 gallons of product total using MW- None 05/09/12 46.64 46.84 0.20 2.40 46.67 Product check following AFVR Event MMPE 08/20/12 47.94 48.28 0.34 4.08 47.99 Recovered 130.25 gallons of product total using None 09/11/12 48.03 48.07 0.04 0.48 48.04 Product check following MMPE Event MMPE 03/04/13 50.62 51.10 0.48 5.76 50.69 Product check before MMPE Event MMPE 03/08/13 49.81 0.00 0.00 49.81 Product check following MMPE Event None 03/14/13 50.65 50.91 0.26 3.12 50.69 MMPE 12/02/13 49.93 50.43 0.50 6.00 50.00 Product check before MMPE Event MMPE 12/06/13 49.75 0.00 0.00 49.75 Product check following MMPE Event None 01/06/14 46.85 46.89 0.04 0.48 46.86 MMPE 06/16/14 44.33 44.35 0.02 0.24 44.33 Product check before MMPE Event MMPE 06/20/14 48.49 0.00 0.00 48.49 Product check following MMPE Event None 07/08/14 44.37 44.38 0.01 0.12 44.37 MMPE 12/15/14 45.12 45.18 0.06 0.72 45.13 Product check before MMPE Event MMPE 12/19/14 46.72 0.00 0.00 46.72 Product check following MMPE Event None 01/05/15 47.92 0.00 0.00 47.92 MMPE 06/01/15 44.38 0.00 0.00 44.38 Product check before MMPE Event MMPE 06/05/15 49.00 0.00 0.00 49.00 Product check following MMPE Event None 07/01/15 44.83 44.85 0.02 0.24 44.83 Bailing 11/18/15 49.66 50.00 0.34 4.08 49.71 Boom 12/16/15 48.85 48.88 0.03 0.36 48.85 Boom 01/19/16 --- 46.98 0.00 0.00 46.98 Boom 02/17/16 --- 47.30 0.00 0.00 47.30 Boom 03/16/16 --- 46.74 0.00 0.00 46.74 Boom 04/18/16 46.69 46.70 0.01 0.12 46.69 Boom 07/19/16 --- 47.11 0.00 0.00 47.11 Boom 02/17/17 48.40 48.41 0.01 0.12 48.40 Boom 03/21/17 49.15 0.00 0.00 49.15 Boom 04/18/17 48.82 0.00 0.00 48.82 Boom 05/16/17 48.85 48.91 0.06 0.72 48.86 Boom 06/16/17 48.81 0.00 0.00 48.81 Boom 07/14/17 48.25 0.00 0.00 48.25 None 11/27/17 49.17 49.20 0.03 0.00 49.17 None 01/24/18 49.46 49.55 0.09 1.08 49.47 Boom 02/21/18 49.30 49.41 0.11 1.32 49.32 Boom 03/27/18 49.75 49.76 0.01 0.12 49.75 Boom 04/27/18 49.05 0.00 0.00 49.05 Boom 07/24/18 49.40 0.00 0.00 49.40 Boom 08/22/18 49.69 49.72 0.03 0.36 49.69 None 04/01/19 45.85 0.00 0.00 45.85 None 05/06/19 45.11 0.00 0.00 45.11 None 06/03/19 45.13 0.00 0.00 45.13 None 07/02/19 44.94 0.00 0.00 44.94 None 08/01/19 45.49 0.00 0.00 45.49 None 09/09/19 45.80 0.00 0.00 45.80 None 11/13/19 44.82 0.00 0.00 44.82 None 12/10/19 44.97 0.00 0.00 44.97 None 01/10/20 45.07 0.00 0.00 45.07 None 02/12/20 44.88 0.00 0.00 44.88 None 03/30/20 44.75 0.00 0.00 44.75 None 04/30/20 44.48 0.00 0.00 44.48 None 06/02/20 44.45 0.00 0.00 44.45 None 06/18/20 43.92 43.93 0.01 0.12 43.92 Page 1 of 4 0 I' I Table 1 Summary of Historic Free Product and Liquid Levels Jefferson Pilot Communications Company (Incident No. 7570) One Julian Price Place, Charlotte, Mecklenburg County, NC S&ME Project No. 4335-14-135A Product Type: #2 Diesel Well # Recovery Date DTP DTW FPT FPT Corrected DTW Comment EW-1 Skimmer 08/24/05 1 45.19 0.00 0.00 45.19 Sk,-off-wen D,gel.pedmch,,kfo,thep,,,,,ceoff,,,p,odu,t Skimmer 08/29/05 45.12 47.72 2.60 31.20 45.49 Skimmer Off Skimmer 09/06/05 45.20 45.22 0.02 0.24 45.20 Skimmer Off Skimmer 10/03/05 45.65 0.00 0.00 45.65 Skimmer Off Skimmer 11/03/05 45.90 0.00 0.00 45.90 Skimmer Off Skimmer 05/25/06 47.32 0.00 0.00 47.32 Skimmer Off Skimmer 08/18/06 46.60 0.00 0.00 46.60 Skimmer Off Skimmer 06/19/07 44.39 0.00 0.00 44.39 Skimmer Off Bailing 07/15/11 50.08 52.16 2.08 24.96 50.38 Bailed approx 0.3 gallon of product/water AFVR 11/29/11 50.41 50.98 0.57 6.84 50.49 Recovered 191 gallons of product total using MW- None 01/11/12 50.03 51.43 1.40 16.80 50.23 Product check following AFVR Event AFVR 04/05/12 46.40 47.80 1.40 16.80 46.60 Recovered 36 gallons of product total using MW- None 05/09/12 49.48 50.77 1.29 15.48 49.66 Product check following AFVR Event MMPE 08/20/12 50.75 52.49 1.74 20.88 51.00 Recovered 130.25 gallons of product total using None 09/11/12 50.99 51.42 0.43 5.16 51.05 Product check following MMPE Event MMPE 03/04/13 48.68 48.83 0.15 1.80 48.70 Product check before MMPE Event MMPE 03/08/13 49.81 0.00 0.00 49.81 Product check following MMPE Event None 03/14/13 45.67 45.70 0.03 0.36 45.67 MMPE 12/02/13 46.94 47.10 0.16 1.92 46.96 Product check before MMPE Event MMPE 12/06/13 49.60 0.00 0.00 49.60 Product check following MMPE Event None 01/06/14 49.84 50.09 0.25 3.00 49.88 MMPE 06/16/14 47.34 47.40 0.06 0.72 47.35 Product check before MMPE Event MMPE 06/20/14 49.55 0.00 0.00 49.55 Product check following MMPE Event None 07/08/14 47.41 47.44 0.03 0.36 47.41 MMPE 12/15/14 48.12 48.29 0.17 2.04 48.14 Product check before MMPE Event MMPE 12/19/14 49.65 0.00 0.00 49.65 Product check following MMPE Event None 01/05/15 48.25 48.33 0.08 0.96 48.26 MMPE 06/01/15 47.36 47.39 0.03 0.36 47.36 Product check before MMPE Event MMPE 06/05/15 50.01 0.00 0.00 50.01 Product check following MMPE Event None 07/01/15 47.82 47.91 0.09 1.08 47.83 Bailing 11/18/15 47.75 47.79 0.04 0.48 47.76 Boom 12/16/15 --- 48.85 0.00 0.00 48.85 Boom 01/19/16 --- 44.06 0.00 0.00 44.06 Boom 02/17/16 --- 44.44 0.00 0.00 44.44 Boom 03/16/16 --- 43.80 0.00 0.00 43.80 Boom 07/19/16 42.22 42.24 0.02 0.24 42.22 Boom 02/17/17 45.70 0.00 0.00 45.70 Boom 03/21/17 45.63 0.00 0.00 45.63 Boom 04/18/17 45.62 0.00 0.00 45.62 Boom 05/16/17 45.39 45.40 0.01 0.12 45.39 Boom 06/16/17 45.09 0.00 0.00 45.09 Boom 07/14/17 45.02 0.00 0.00 45.02 None 11/27/17 44.24 44.25 0.01 0.12 44.24 None 01/24/18 47.49 0.00 0.00 47.49 Boom 02/21/18 46.30 0.00 0.00 46.30 Boom 03/27/18 45.22 0.00 0.00 45.22 Boom 04/27/18 45.70 0.00 0.00 45.70 Boom 07/24/18 44.77 44.80 0.03 0.36 44.77 Boom 08/22/18 42.34 0.00 0.00 42.34 None 04/01/19 42.97 0.00 0.00 42.97 None 05/06/19 37.66 0.00 0.00 37.66 None 06/03/19 42.11 42.12 0.01 0.00 42.11 Installed sock Boom 07/02/19 37.85 0.00 0.00 37.85 None 08/01/19 NO DATA Sock was 5% saturated. Sock was removed None 09/09/19 42.98 0.00 0.00 42.98 None 11/13/19 37.42 0.00 0.00 37.42 None 12/10/19 37.67 0.00 0.00 37.67 None 01/10/20 37.84 0.00 0.00 37.84 None 02/12/20 37.45 0.00 0.00 37.45 None 03/30/20 37.38 0.00 0.00 37.38 None 04/30/22 37.00 0.00 0.00 37.00 None 06/02/20 37.10 0.00 0.00 37.10 None 06/18/20 41.44 0.00 0.00 41.44 Page 2 of 4 0 II Table 1 Summary of Historic Free Product and Liquid Levels Jefferson Pilot Communications Company (Incident No. 7570) One Julian Price Place, Charlotte, Mecklenburg County, NC S&ME Project No. 4335-14-135A Product Type: #2 Diesel Well # Recovery Date DTP DTW FPT FPT Corrected DTW Comment MW-2 None 08/12/05 43.13 44.98 1.85 22.20 43.39 None 08/18/05 43.22 45.09 1.87 22.44 43.49 None 08/24/05 43.29 45.19 1.90 22.80 43.56 None 08/29/05 43.32 45.52 2.20 26.40 43.63 None 09/06/05 43.41 45.35 1.94 23.28 43.69 None 10/03/05 43.83 44.35 0.52 6.24 43.90 None 11/03/05 44.10 45.98 1.88 22.56 44.37 None 02/03/06 43.60 45.25 1.65 19.80 43.83 None 03/10/06 43.31 44.93 1.62 19.44 43.54 None 03/23/06 43.35 45.00 1.65 19.80 43.58 Skimmer 03/29/06 43.33 44.96 1.63 19.56 43.56 Skimmer moved from MW-9 to MW-2, Needs new Skimmer 05/15/06 44.42 46.22 1.80 21.60 44.68 Skimmer 05/25/06 44.52 47.00 2.48 29.76 44.87 Skimmer 06/16/06 45.24 45.30 0.06 0.72 45.25 Skimmer 07/07/06 45.58 45.73 0.15 1.80 45.60 Skimmer 07/17/06 45.58 45.73 0.15 1.80 45.60 Skimmer 08/18/06 45.96 46.70 0.74 8.88 46.07 Base of Belt above liquid surface Skimmer 06/19/07 43.64 44.60 0.96 11.52 43.78 Skimmer Off Bailing 07/15/11 46.53 48.29 1.76 21.12 46.78 Bailed approx 0.2 gallon of product/water AFVR 11/29/11 46.92 48.11 1.19 14.28 47.09 Recovered 191 gallons of product total using MW- None 01/11/12 45.65 46.31 0.66 7.92 45.74 Product check following AFVR Event AFVR 04/05/12 45.05 45.82 0.77 9.24 45.16 Recovered 36 gallons of product total using MW- None 05/09/12 45.14 45.43 0.29 3.48 45.18 Product check following AFVR Event MMPE 08/20/12 46.42 47.17 0.75 9.00 46.53 Recovered 130.25 gallons of product total using None 09/11/12 46.51 46.89 0.38 4.56 46.56 Product check following MMPE Event MMPE 03/04/13 46.08 47.10 1.02 12.24 46.22 Product check before MMPE Event MMPE 03/08/13 46.41 0.00 0.00 46.41 Product check following MMPE Event None 03/14/13 46.18 46.45 0.27 3.24 46.22 MMPE 12/02/13 45.28 46.48 1.20 14.40 45.45 Product check before MMPE Event MMPE 12/06/13 47.05 0.00 0.00 47.05 Product check following MMPE Event None 01/06/14 45.35 45.53 0.18 2.16 45.38 MMPE 06/16/14 42.76 42.89 0.13 1.56 42.78 Product check before MMPE Event MMPE 06/20/14 47.79 0.00 0.00 47.79 Product check following MMPE Event None 07/08/14 42.83 42.89 0.06 0.72 42.84 MMPE 12/15/14 43.52 43.98 0.46 5.52 43.59 Product check before MMPE Event MMPE 12/19/14 46.17 0.00 0.00 46.17 Product check following MMPE Event None 01/05/15 43.71 43.92 0.21 2.52 43.74 MMPE 06/01/15 42.81 42.96 0.15 1.80 42.83 Product check before MMPE Event MMPE 06/05/15 46.41 0.00 0.00 46.41 Product check following MMPE Event None 07/01/15 43.26 43.55 0.29 3.48 43.30 Bailing 11/18/15 45.20 45.65 0.45 5.40 45.26 Boom 12/16/15 49.90 49.91 0.01 0.12 49.90 Boom 01/19/16 --- 44.08 0.00 0.00 44.08 Boom 02/17/16 --- 44.40 0.00 0.00 44.40 Boom 04/18/16 --- 42.09 0.00 0.00 42.09 Boom 07/19/16 42.62 42.65 0.03 0.36 42.62 Boom 02/17/17 NP 44.62 0.00 0.00 44.62 Boom 03/21/17 NP 44.31 0.00 0.00 44.31 Boom 04/18/17 NP 44.58 0.00 0.00 44.58 Boom 05/16/17 NP 44.18 0.00 0.00 44.18 Boom 06/16/17 NP 44.02 0.00 0.00 44.02 Boom 07/14/17 NP 43.73 0.00 0.00 43.73 None 11/27/17 44.25 44.30 0.05 0.00 44.26 None 01/24/18 45.01 45.17 0.16 1.92 45.03 Boom 02/21/18 45.25 0.00 0.00 45.25 Boom 03/27/18 48.95 0.00 0.00 48.95 Boom 04/27/18 44.50 0.00 0.00 44.50 Boom 07/24/18 48.95 0.00 0.00 48.95 Boom 08/22/18 45.28 45.34 0.06 0.72 45.29 None 04/01/19 40.60 0.00 0.00 40.60 None 05/06/19 40.80 0.00 0.00 40.80 None 06/03/19 41.11 0.00 0.00 41.11 None 07/02/19 40.62 0.00 0.00 40.62 None 08/01/19 41.08 0.00 0.00 41.08 None 09/09/19 41.20 41.24 0.04 0.48 41.21 Added new sock Boom 11/13/19 40.10 0.00 0.00 40.10 Boom 12/10/19 40.88 40.90 0.02 0.24 40.88 Sock 10%saturated, left existing sock in well. Boom 01/10/20 41.01 41.04 0.03 0.36 41.01 Sock replaced, 80%saturated. Boom 02/12/20 40.72 40.76 0.04 0.48 40.73 Sock replaced, 60%saturated. Boom 03/30/20 40.38 40.40 0.02 0.00 40.38 Sock replaced, 50%saturated. Boom 04/30/20 39.95 39.97 0.02 0.24 39.95 Removed sock, 80%saturated. None 06/02/20 40.10 40.12 0.02 0.24 40.10 None 06/18/20 39.75 0.00 0.00 39.75 Page 3 of 4 Table 1 I' Summary of Historic Free Product and Liquid Levels Jefferson Pilot Communications Company (Incident No. 7570) One Julian Price Place, Charlotte, Mecklenburg County, NC S&ME Project No. 4335-14-135A Product Type: #2 Diesel Well # Recovery Date CITP DTW FPT FPT Corrected DTW Comment MW-3 Skimmer 08/12/05 43.82 45.43 1.61 19.32 44.05 Skimmer started on 8/12/05 Skimmer 08/15/05 44.11 44.11 0.00 0.00 44.11 Skimmer 08/18/05 44.13 44.17 0.04 0.48 44.14 Skimmer 08/24/05 44.22 44.22 0.00 0.00 44.22 Skimmer 08/29/05 44.23 44.50 0.27 3.24 44.27 Skimmer 09/06/05 44.32 44.32 0.00 0.00 44.32 Skimmer 10/03/05 44.70 45.03 0.33 3.96 44.75 Skimmer 11/03/05 45.73 45.75 0.02 0.24 45.73 Skimmer 02/03/06 43.13 43.45 0.32 3.84 43.18 Skimmer 03/10/06 44.78 45.60 0.82 9.84 44.90 Skimmer 03/23/06 44.93 44.97 0.04 0.48 44.94 Skimmer 05/15/06 45.10 45.10 0.00 0.00 45.10 Skimmer 05/25/06 45.21 45.21 0.00 0.00 45.21 Skimmer 06/16/06 45.67 45.68 0.01 0.12 45.67 Skimmer 07/07/06 46.00 46.00 0.00 0.00 46.00 Skimmer 07/17/06 46.00 46.00 0.00 0.00 46.00 Skimmer 08/18/06 46.43 47.05 0.62 7.44 46.52 Base of Belt above liquid surface Skimmer 06/19/07 44.60 45.45 1.45 17.40 44.21 1-gallon from MW-1 placed in drum Bailing 07/15/11 46.86 48.98 2.12 25.44 47.16 Bailed approx 0.3gallon of product/water AFVR 11/29/11 47.21 49.12 1.91 22.92 47.48 Recovered 191 gallons of product total using MW- None 01/11/12 45.97 47.08 1.11 13.32 46.13 Product check following AFVR Event AFVR 04/05/12 45.35 46.65 1.30 15.60 45.53 Recovered 36 gallons of product total using MW- None 05/09/12 45.46 46.28 0.82 9.84 45.58 Product check following AFVR Event MMPE 08/20/12 46.73 47.94 1.21 14.52 46.90 Recovered 130.25 gallons of product total using None 09/11/12 46.88 47.32 0.44 5.28 46.94 Product check following MMPE Event MMPE 03/04/13 46.53 47.00 0.47 5.64 46.60 Product check before MMPE Event MMPE 03/08/13 48.55 0.00 0.00 48.55 Product check following MMPE Event None 03/14/13 46.55 46.85 0.30 3.60 46.59 MMPE 12/02/13 45.86 46.20 0.34 4.08 45.91 Product check before MMPE Event MMPE 12/06/13 48.47 0.00 0.00 48.47 Product check following MMPE Event None 01/06/14 45.79 45.82 0.03 0.36 45.79 MMPE 06/16/14 43.27 43.28 0.01 0.12 43.27 Product check before MMPE Event MMPE 06/20/14 46.31 0.00 0.00 46.31 Product check following MMPE Event None 07/08/14 43.34 43.45 0.11 1.32 43.36 MMPE 12/15/14 44.02 44.51 0.49 5.88 44.09 Product check before MMPE Event MMPE 12/19/14 48.28 0.00 0.00 48.28 Product check following MMPE Event None 01/05/15 44.15 44.59 0.44 5.28 44.21 MMPE 06/01/15 43.30 43.51 0.21 2.52 43.33 Product check before MMPE Event MMPE 06/05/15 47.49 0.00 0.00 47.49 Product check following MMPE Event None 07/01/15 43.76 44.05 0.29 3.48 43.80 Boom 02/17/17 NP 44.84 0.00 0.00 44.84 Boom 03/21/17 NP 44.58 0.00 0.00 44.58 Boom 04/18/17 NP 44.29 0.00 0.00 44.29 Boom 05/16/17 NP 44.32 0.00 0.00 44.32 Boom 06/16/17 NP 44.05 0.00 0.00 44.05 Boom 07/14/17 NP 44.10 0.00 0.00 44.10 None 11/27/17 45.26 45.32 0.06 0.00 45.27 None 01/24/18 45.53 45.60 0.07 0.84 45.54 Boom 02/21/18 44.83 44.90 0.07 0.84 44.84 Boom 03/27/18 45.07 45.10 0.03 0.36 45.07 Boom 04/27/18 44.64 0.00 0.00 44.64 Boom 07/24/18 49.27 0.00 0.00 49.27 Boom 08/22/18 45.66 45.74 0.08 0.96 45.67 None 04/01/19 42.29 42.31 0.02 0.24 42.29 Installed new sock Boom 05/06/19 41.53 41.68 0.15 1.80 41.55 Sock was 80%saturated. Installed new sock. Boom 06/03/19 40.52 40.56 0.04 0.48 40.53 Sock was 100%saturated. Installed new sock. Boom 07/02/19 41.32 41.44 0.12 1.44 41.34 Sock was 90%saturated. Installed new sock. Boom 08/01/19 41.40 0.00 0.00 41.40 Sock was 50%saturated. Sock was removed None 09/09/19 41.73 0.00 0.00 41.73 None 11/13/19 40.51 0.00 0.00 40.51 None 12/10/20 40.48 0.00 0.00 40.48 None 01/10/20 40.62 0.00 0.00 40.62 None 02/12/20 40.20 0.00 0.00 40.20 None 03/30/20 40.02 0.00 0.00 40.02 None 04/30/20 39.82 0.00 0.00 39.82 None 06/02/20 39.77 0.00 1 0.00 39.77 None 06/18/20 39.89 0.00 1 0.00 39.89 Notes: DTP: Depth to Product from Top of Casing (ft): Feet DTW : Depth to Water from Top of Casing (in): Inches FPT : Free Product Thickness (gal) : Gallons ....: No Free Product Indicated Corrected Depth to Water is calculated by: [Depth to Water] - [Free Product Thickness x 0.85811 Page 4 of 4 Table 2 IIIE Free Product Recovery - Overall Summary Jefferson Pilot Communications (UST Incident # 7570) One Julian Price Place, Charlotte, NC S&ME Project No. 4335-14-135A Date 11/13/19 DTP NM DTW 44.82 FP 0.00 FP Recovered 0.00 DTP NM DTW 40.10 FP 0.00 FP Recovered 0.00 DTP NM DTW 40.51 FP 0.00 FP Recovered 0.00 DTP NM DTW 37.42 FP 0.00 FP Recovered 0.00 FP Recovered 0.00 12/10/19 NM 44.97 0.00 0.00 40.88 40.90 0.00 0.00 NM 40.48 0.00 0.00 NM 37.67 0.00 0.00 0.00 01/10/20 NM 45.07 0.00 0.00 41.01 41.04 0.03 0.11 NM 40.62 0.00 0.00 NM 37.84 0.00 0.00 0.11 02/12/20 NM 44.88 0.00 0.00 40.72 40.76 0.04 0.08 NM 40.20 0.00 0.00 NM 37.45 0.00 0.00 0.08 03/30/20 NM 44.75 0.00 0.00 40.38 40.40 0.02 0.07 NM 40.02 0.00 0.00 NM 37.38 0.00 0.00 0.07 04/30/20 NM 44.48 0.00 0.00 39.95 39.97 0.02 0.11 NM 39.82 0.00 0.00 NM 37.00 0.00 0.00 0.11 06/02/20 NM 44.45 0.00 0.00 40.10 40.12 0.00 0.00 NM 39.77 0.00 0.00 NM 37.10 0.00 0.00 0.00 06/18/20 43.92 43.93 0.01 0.00 NM 39.75 0.00 0.00 NM 39.89 0.00 0.00 NM 41.44 0.00 0.00 0.00 Totals 0.00 0.36 0.00 0.00 0.36 Notes: Liquid levels measured from well top of casing, after removing socks ft :feet gal : gallons NM : None measured III Table 3 Free Product Recovery - Event Summaries Jefferson Pilot Communications (UST Incident # 7570) One Julian Price Place, Charlotte, NC S&ME Project No. 4335-14-135A ..12/10/2019 Casing Diameter in 2 2 2 4 Boring Diameter in 8 8 8 10 Annulus Porosity % 30% 30% 30% 30% Depth to Product ft 44.97 40.88 40.48 37.67 Depth to Water ft 44.97 40.90 40.48 37.67 Product Thickness ft 0.00 0.02 0.00 0.00 in 0.00 0.24 0.00 0.00 Total Boring Volume ft^3 0.00 0.01 0.00 0.00 Well Volume ft^3 0.00 0.00 0.00 0.00 Annulus Volume ft^3 0.00 0.00 0.00 0.00 Product Volume ft^3 0.00 0.00 0.00 0.00 gal 0.00 0.02 0.00 0.00 oz 0.0 2.3 0.0 0.0 % Sock Capacity % 0% 14% 0% 0% Sock Capacity oz 17 17 17 17 gal 0.13 0.13 0.13 0.13 # of Socks 0 1 0 0 Sock % Full 0% 10% 0% 0% Old Sock Reinstalled (#) 0 1 0 0 New Sock Installed (#) 0 0 0 0 Sock Volume gal 0.00 0.00 0.00 0.00 0.00 Bailed Volume gal 0.00 0.00 0.00 0.00 0.00 Total Volume gal 0.00 0.00 0.00 0.00 0.00 Notes: Liquid levels measured after removing socks Page 1 of 5 ILI I' I Table 3 Free Product Recovery - Event Summaries Jefferson Pilot Communications (UST Incident # 7570) One Julian Price Place, Charlotte, NC S&ME Project No. 4335-14-135A ..1/10/2020 Casing Diameter in 2 2 2 4 Boring Diameter in 8 8 8 10 Annulus Porosity % 30% 30% 30% 30% Depth to Product ft 45.07 41.01 40.62 37.84 Depth to Water ft 45.07 41.04 40.62 37.84 Product Thickness ft 0.00 0.03 0.00 0.00 in 0.00 0.36 0.00 0.00 Total Boring Volume ft^3 0.00 0.01 0.00 0.00 Well Volume ft^3 0.00 0.00 0.00 0.00 Annulus Volume ft^3 0.00 0.00 0.00 0.00 Product Volume ft^3 0.00 0.00 0.00 0.00 gal 0.00 0.03 0.00 0.00 oz 0.0 3.4 0.0 0.0 % Sock Capacity % 0% 20% 0% 0% Sock Capacity oz 17 17 17 17 gal 0.13 0.13 0.13 0.13 # of Socks 0 1 0 0 Sock % Full 0% 80% 0% 0% Old Sock Reinstalled (#) 0 0 0 0 New Sock Installed (#) 0 1 0 0 Sock Volume gal 0.00 0.11 0.00 0.00 0.11 Bailed Volume gal 0.00 0.00 0.00 0.00 0.00 Total Volume gal 0.00 0.11 0.00 0.00 0.11 Notes: Liquid levels measured after removing socks Page 1 of 5 Table 3 Free Product Recovery - Event Summaries Jefferson Pilot Communications (UST Incident # 7570) One Julian Price Place, Charlotte, NC S&ME Project No. 4335-14-135A Date Casing Diameter in 2 2 2/12/2020 2 4 Boring Diameter in 8 8 8 10 Annulus Porosity % 30% 30% 30% 30% Depth to Product ft 44.88 40.72 40.20 37.45 Depth to Water ft 44.88 40.76 40.20 37.45 Product Thickness ft 0.00 0.04 0.00 0.00 in 0.00 0.48 0.00 0.00 Total Boring Volume ft^3 0.00 0.01 0.00 0.00 Well Volume ft^3 0.00 0.00 0.00 0.00 Annulus Volume ft^3 0.00 0.00 0.00 0.00 Product Volume ft^3 0.00 0.00 0.00 0.00 gal 0.00 0.04 0.00 0.00 oz 0.0 4.6 0.0 0.0 % Sock Capacity % 0% 27% 0% 0% Sock Capacity oz 17 17 17 17 gal 0.13 0.13 0.13 0.13 # of Socks 0 1 0 0 Sock % Full 0% 60% 0% 0% Old Sock Reinstalled (#) 0 0 0 0 New Sock Installed (#) 0 1 0 0 Sock Volume gal 0.00 0.08 0.00 0.00 0.08 Bailed Volume gal 0.00 0.00 0.00 0.00 0.00 Total Volume gal 0.00 0.08 0.00 0.00 0.08 Notes: Liquid levels measured after removing socks Page 2 of 5 -s. i Table 3 Free Product Recovery - Event Summaries Jefferson Pilot Communications (UST Incident # 7570) One Julian Price Place, Charlotte, NC S&ME Project No. 4335-14-135A ..3/30/2020 Casing Diameter in 2 2 2 4 Boring Diameter in 8 8 8 10 Annulus Porosity % 30% 30% 30% 30% Depth to Product ft 44.75 40.38 40.02 37.38 Depth to Water ft 44.75 40.40 40.02 37.38 Product Thickness ft 0.00 0.02 0.00 0.00 in 0.00 0.24 0.00 0.00 Total Boring Volume ft^3 0.00 0.01 0.00 0.00 Well Volume ft^3 0.00 0.00 0.00 0.00 Annulus Volume ft^3 0.00 0.00 0.00 0.00 Product Volume ft^3 0.00 0.00 0.00 0.00 gal 0.00 0.02 0.00 0.00 oz 0.0 2.3 0.0 0.0 % Sock Capacity % 0% 14% 0% 0% Sock Capacity oz 17 17 17 17 gal 0.13 0.13 0.13 0.13 # of Socks 0 1 0 0 Sock % Full 0% 50% 0% 0% Old Sock Reinstalled (#) 0 0 0 0 New Sock Installed (#) 0 1 0 0 Sock Volume gal 0.00 0.07 0.00 0.00 0.07 Bailed Volume gal 0.00 0.00 0.00 0.00 0.00 Total Volume gal 0.00 0.07 0.00 0.00 0.07 Notes: Liquid levels measured after removing socks Page 3 of 5 A -s. Table 3 Free Product Recovery - Event Summaries Jefferson Pilot Communications (UST Incident # 7570) One Julian Price Place, Charlotte, NC S&ME Project No. 4335-14-135A ..4/30/2020 Casing Diameter in 2 2 2 4 Boring Diameter in 8 8 8 10 Annulus Porosity % 30% 30% 30% 30% Depth to Product ft 44.48 40.10 39.82 37.00 Depth to Water ft 44.48 40.12 39.82 37.00 Product Thickness ft 0.00 0.02 0.00 0.00 in 0.00 0.24 0.00 0.00 Total Boring Volume ft^3 0.00 0.01 0.00 0.00 Well Volume ft^3 0.00 0.00 0.00 0.00 Annulus Volume ft^3 0.00 0.00 0.00 0.00 Product Volume ft^3 0.00 0.00 0.00 0.00 gal 0.00 0.02 0.00 0.00 oz 0.0 2.3 0.0 0.0 % Sock Capacity % 0% 14% 0% 0% Sock Capacity oz 17 17 17 17 gal 0.13 0.13 0.13 0.13 # of Socks 0 1 0 0 Sock % Full 0% 80% 0% 0% Old Sock Reinstalled (#) 0 0 0 0 New Sock Installed (#) 0 0 0 0 Sock Volume gal 0.00 0.11 0.00 0.00 0.11 Bailed Volume gal 0.00 0.00 0.00 0.00 0.00 Total Volume gal 0.00 0.11 0.00 0.00 0.11 Notes: Liquid levels measured after removing socks Page 4 of 5 Table 3 Free Product Recovery - Event Summaries Jefferson Pilot Communications (UST Incident # 7570) One Julian Price Place, Charlotte, NC S&ME Project No. 4335-14-135A Date Casing Diameter in 2 2 6/18/2020 2 4 Boring Diameter in 8 8 8 10 Annulus Porosity % 30% 30% 30% 30% Depth to Product ft 43.92 39.75 39.89 41.44 Depth to Water ft 43.93 39.75 39.89 41.44 Product Thickness ft 0.01 0.00 0.00 0.00 in 0.12 0.00 0.00 0.00 Total Boring Volume ft^3 0.00 0.00 0.00 0.00 Well Volume ft^3 0.00 0.00 0.00 0.00 Annulus Volume ft^3 0.00 0.00 0.00 0.00 Product Volume ft^3 0.00 0.00 0.00 0.00 gal 0.01 0.00 0.00 0.00 oz 1.1 0.0 0.0 0.0 % Sock Capacity % 7% 0% 0% 0% Sock Capacity oz 17 17 17 17 gal 0.13 0.13 0.13 0.13 # of Socks 0 0 0 0 Sock % Full 0% 0% 0% 0% Old Sock Reinstalled (#) 0 0 0 0 New Sock Installed (#) 0 0 0 0 Sock Volume gal 0.00 0.00 0.00 0.00 0.00 Bailed Volume gal 0.00 0.00 0.00 0.00 0.00 Total Volume gal 0.00 0.00 0.00 0.00 0.00 Notes: Liquid levels measured after removing socks Page 5 of 5