HomeMy WebLinkAbout8505_Duke_Belews_RepairCQA_DIN25918_20160407Belews Creek Steam Station
3195 Pine Hall Road
Belews Creek, NC 27009
336-445-0610
336-669-2994
www.duke-energy.com
April 1, 2016
North Carolina Department of Environmental Quality
Division of Waste Management
Solid Waste Section
2090 U.S. Highway 70 Swannanoa, North Carolina 28778
Attn: Mr. Larry Frost
Re: Duke Energy Carolinas - Belews Creek Steam Station FGD Residuals Landfill (Permit No. INDUS-8505)
Stokes County
Dear Mr. Frost,
Attached you will find for your review the Construction Quality Assurance (CQA) Certification
Report for the liner repair at the Flue Gas Desulfurization (FGD) Residual Landfill (Permit No.
INDUS-8505). The CQA oversight and report was generated by Joyce Engineering.
This document is being submitted electronically. Please let me know if you would like to receive paper copies.
Respectfully submitted,
Melonie Martin
Environmental Services
Attachments: FGD Residual Landfill Liner Repair CQA Cetification Report, Duke Energy Carolinas, Belews Creek Steam Station, FGD Residual Landfill
cc (via e-mail): Will Harrison, Duke
Evan Andrews, Duke
Ed Sullivan, Duke Ed Mussler, NCDEQ
Prepared for:
DUKE ENERGY
Belews Creek Steam Station
3195 Pine Hall Rd.
Belews Creek, NC 27009
BELEWS CREEK STEAM STATION
FGD RESIDUAL LANDFILL LINER REPAIR
CONSTRUCTION QUALITY ASSURANCE
CERTIFICATION REPORT
March 31, 2016
Prepared by:
2211 West Meadowview Road, Suite 101
Greensboro, NC 27407 NC CORP LIC: C-0782
JEI Project: 845
Amy Davis, P.E. Senior Project Consultant
Joyce Engineering, Inc. North Carolina Corporate Lic: C-078
Duke Energy Belews Creek Steam Station Page i Joyce Engineering, Inc. FGD Landfill Geosynthetic Liner Repair March 2016 CQA Certification Report
TABLE OF CONTENTS
Page
Table of Contents ......................................................................................................................... i
1.0 Introduction ...................................................................................................................... 1
2.0 Construction Quality Assurance Activities ................................................................... 1
2.1 General ................................................................................................................... 1
2.2 Liner Damage Survey ............................................................................................ 1
2.3 Liner Repair ........................................................................................................... 1
3.0 Conclusion ........................................................................................................................ 2
Attachments
Photos Sequence of liner repair work
Certifications Geosynthetic materials
Drawing FGD Landfill Existing Conditions
Duke Energy Belews Creek Steam Station Page 1 Joyce Engineering, Inc. FGD Landfill Geosynthetic Liner Repair March 2016
CQA Certification Report
1.0 INTRODUCTION
Duke Energy operates the Flue Gas Desulfurization (FGD) landfill constructed in
accordance with Sub-Title D Regulations, North Carolina Solid Waste Management Rules 15A NCAC 13B and the General Permit Conditions of Permit # 85-05. This report, prepared by
Joyce Engineering, Inc. (JOYCE) for Duke Energy addresses the quality assurance activities
performed on March 18, 2016 during FGD residuals landfill geosynthetic liner repair at the
Belews Creek Steam Station.
Charah had retained Chesapeake Containment Systems (CCS) to perform the
geosynthetic liner damage repair. Joyce Engineering, Inc. retained by Duke Energy provided
oversight and quality assurance for the liner repair work. The damaged section of the landfill
liner system measured approximately 6 feet by 4 feet and damage to the liner system consisted of
a tear in the protective geocomposite layer, geomembrane liner and the Geosynthetic Clay Liner (GCL). The liner damage had occurred during mining of gypsum on the east end of Cell 4 slope.
The location is in the southeast corner of Cell 4 shown on the attached Drawing, Sheet 1, FGD
Landfill Existing Conditions.
2.0 CONSTRUCTION QUALITY ASSURANCE ACTIVITIES
2.1 General
Joyce Engineering, Inc. provided Construction Quality Assurance (CQA) activities for the repair work. The following sections describe the specific areas of CQA:
2.2 Liner Damage Survey
Representatives of Duke Energy and Joyce Engineering, Inc. surveyed the extent of damage to the liner system prior to commencing the repair work. The damage to the liner system
was observed in one location through the three layers of the geosynthetic liner system. The
damage to the liner was reportedly caused by trackhoe bucket catching the synthetic liner system
during excavation of the gypsum. No other locations of liner damage were observed, but the
layer of gypsum was noted as being thin over the liner system in the east end of Cell 4 where the mining activity had been recently conducted.
Fleming Engineering, retained by Duke Energy, surveyed the existing conditions and cut-
fill of the gypsum grades. Drawing No. 1 of 2, attached with this report, shows the existing
conditions of the achieved mining grades and the location of the damaged liner.
2.3 Liner Repair
Chesapeake mobilized on March 18, 2016 to the FGD landfill for the liner repair work.
Charah cleaned the damage area by brushing soil, gypsum and dust from the area to be worked
on. The ripped geocomposite and geomembrane were cut and removed. CCS trimmed the
Duke Energy Belews Creek Steam Station Page 2 Joyce Engineering, Inc. FGD Landfill Geosynthetic Liner Repair March 2016
CQA Certification Report
damaged geomembrane edge to prepare for the new patch material placement. The existing
GCL was pulled back in its placed and loose powder bentonite was poured over the perimeter of
the repair area to provide a continuous seam between the existing and new GCL. A new piece of
GCL was placed over the damaged GCL to cover the entire area. The new GCL panel extended a minimum of 12 inches in all direction beyond the damaged edges of the existing GCL.
Prior to beginning the geomembrane patch installation, CCS turned the extrusion welder
DemTech MX-43 on to allow the welding unit to heat and reach its operating temperature. The
pre-heat temperature was observed and recorded 458 oF. The ambient temperature was recorded 72 oF. After the welder had reached its operating temperature a test weld was conducted on the
new geomembrane. Two pieces of the geomembrane were welded together to form a weld
approximately three feet long. Test sections of the welded seam were cut for shear and peel
testing. Each test piece was one inch wide across the weld. Three test samples were tested in
accordance with specification for shear and peel.
Project specifications for the geomembrane:
Parent material tensile stress at yield 130 lbs./in/min.
Seam strength: Shear strength 95% of parent material = 123.5
Peel strength 62% of parent material = 80.6 Test results: Sample 1 Sample 2 Sample 3
Shear 160 145 166
Peel 103 102 108
Tensiometer for the shear/peel testing:
Pro Tester T-100; Serial No. 207100; CCS Unit No. T 22
Calibration Date: August 14, 2015
Following the test weld, CCS proceeded to the production welding of the patch. The
geomembrane liner was patched with new material and extrusion welded to the liner. The
extrusion weld was tested for seam quality by use of a vacuum box. The entire welded seam
was tested in segments, which were observed satisfactory by holding a 3 psi vacuum for 15
seconds. A new panel of geocomposite was placed over the repair and left un-attached. The repair area was covered with plastic sheeting until the staff from DEQ can visit the site and
observe the membrane liner repair. Attached photos illustrate the sequence of the repair work.
3.0 CONCLUSION
The damaged geosynthetic liner in the Cell 4 was repaired on Friday, March 18, 2016.
The geocomposite cushion layer to protect the geomembrane was placed loosely over the
geomembrane to allow personnel from DEQ to inspect the repair area. The repair area was then temporarily covered with black plastic to keep rain and run-on off the liner. DEQ visited the site
Duke Energy Belews Creek Steam Station Page 3 Joyce Engineering, Inc. FGD Landfill Geosynthetic Liner Repair March 2016
CQA Certification Report
on Wednesday March 23, 2016. The geocomposite has been secured in place after DEQ
reviewed the repair.
In general the area of excavation in Cell 4, where the landfill liner system was damaged, appears to have from few inches to one foot of gypsum cover over the geosynthetic liner system.
Observed tire marks on the gypsum surface (photo 9) show no signs of pumping or
rutting. Based on these observations, it does not appear the liner materials have been
compromised.
Based on the following, the weight of the dump trucks and the excavation equipment do
not appear to exceed the bearing capacity of the subsoils, and therefore should not compromise
the liner materials.
• The FGD landfill design calculations indicate a minimum bearing capacity for the
subsoils of 10.6 ksf or 10,600 psf.
• The ground pressure for the Komatsu 330 excavator is approximately 1490 psf, less than the minimum bearing capacity of the subsoils.
• The load per tire for a fully loaded tandem axle truck (80,000 lbs), assuming 4 tires per
axle is 8,500 lbs per tire (34,000 lbs per axle/4 tires). Assuming a tire contact area of 1 sf, the ground pressure would be equal to 8,500 psf, less than the minimum bearing
capacity of the subsoils.
In accordance with the Construction Plan Application, a minimum of three feet of
operational cover and waste must be placed over the liner before truck traffic is allowed. The mining operations in the future should be conducted in accordance with the permit documents.
This report is to state that the repair to the FGD landfill geosynthetic liner was conducted
in general accordance with plans and specifications.
Sincerely,
JOYCE ENGINEERING, INC.
Amy Davis, P.E. Hannu Kemppinen, P.G.
Senior Project Consultant Senior Project Consultant
Reference: Geosynthetic Design Guidance for Hazardous Waste, Landfill Cells and Surface
Impoundments by G.M Richardson and R.M. Koerner.
Duke Energy Belews Creek Steam Station Page 4 Joyce Engineering, Inc. FGD Landfill Geosynthetic Liner Repair March 2016
CQA Certification Report
1. Damaged geosynthetic liner at Belews Creek FGD landfill
2. Damage area prepared for repair.
Duke Energy Belews Creek Steam Station Page 5 Joyce Engineering, Inc. FGD Landfill Geosynthetic Liner Repair March 2016
CQA Certification Report
3. Powder bentonite was placed over existing GCL to seal with new GCL.
4. New panel of GCL placed to cover existing damaged GCL.
Duke Energy Belews Creek Steam Station Page 6 Joyce Engineering, Inc. FGD Landfill Geosynthetic Liner Repair March 2016
CQA Certification Report
5. Installer tacking membrane patch before extrusion welding.
6. Patch edge was ground clean in preparation for extrusion welding.
Duke Energy Belews Creek Steam Station Page 7 Joyce Engineering, Inc. FGD Landfill Geosynthetic Liner Repair March 2016
CQA Certification Report
7. Installer extrusion welding a patch to the damaged liner.
8. Installers conducting vacuum box test on completed extrusion weld around the patch.
Duke Energy Belews Creek Steam Station Page 8 Joyce Engineering, Inc. FGD Landfill Geosynthetic Liner Repair March 2016
CQA Certification Report
9. FGD landfill east end of Cell 4 gypsum mining area.
ROLL #LOT #LINER TYPE
Thickness
Measurement
ASTM D5994
(Modified)
METRIC ENGLISH
MIN
MAX
AVE
mm mil
mm
mm
mil
mil
Thickness
Length
Width
m
m
feet
feet
Specific Gravity
ASTM D792
MFI ASTM D1238 COND. E Melt Flow Index 190C/2160 g ‐ g/10 min
Carbon Black Content ASTM D4218 Range
Carbon Black Dispersion ASTM D5596 Category
Tensile Strength
ASTM D6693
(2 inches / minute)
MD
TD
Tensile Elongation
ASTM D6693
(2 inches / minute) Lo
= 1.3" Yield
Lo = 2.0" Break
Average Elongation @ Yield
Average Elongation @Break
Dimensional Stability
ASTM D1204 (Modified)Average Dimensional Change
Tear Resistance
ASTM D1004 (Modified)Average Tear Resistance
Puncture Resistance
FTMS 101 Method 2065 Modified
Puncture Resistance
ASTM D4833 (Modified)
ESCR ASTM D1693
Average Peak Load
Minumum Hrs w/o Failures
Notched Constant Tensile Load
ASTM D5397 Pass/Fail @ 30%
Customer
PO
Destination
Date
Signature
Quality Control Department
g/cc
%
%
%
%
N
N
1500 Hrs
300 Hrs
ppi
ppi
psi
psi
OIT(Standard) ASTM D 3895 minutes
lbs
lbs
N/mm
N/mm
mm mil
G15C081001 HFA610150 60 HD MICROSPIKE B/W
1.42
1.81
1.54
56
71
61
60
153.926
7.01
1.52
505
23
182
.947
.20
2.4
10 in Category 1
‐0.75
134
PASS
CERTIFIED
156
19033
27
Asperity
ASTM D7466
Top
Bottom
33
32
mil
mil
Grade K307
2791
2599
3377
3169
16
14
409
549
63
57253.5
596.0
2/16/2015
psi
psi
TD ppiN/mm 167
ppi
29
MD N/mm 20335
Average Strength @ Yield
Average Strength @ Break
MD
TD
%
%
MD
TD
MD
TD
lbsN280.2
Chesapeake Containment Systems
15117
Lumberton, NC
Average
METRIC ENGLISH
Average Density
CERTIFIED
mm
mm
.84
.81
OA#29693
Product:
MARLEX POLYETHYLENE K307 BULK
Lot Number: HFA610150 ____________________________________________________________________________
Property Test Method Value Unit____________________________________________________________________________
Melt Index ASTM D1238 0.20 g/10mi
HLMI Flow Rate ASTM D1238 19 g/10mi
Density D1505 or D4883 0.938 g/cm3
Pellet Count P02.08.03 29 pel/g
Production Date 01/03/2015____________________________________________________________________________
The data set forth herein have been carefully compiled by Chevron Phillips Chemical Company LP (CPChem).
However, there is no warranty of any kind, either expressed or implied, applicable to its use, and the user assumes
all risk and liability in connection therewith.
Troy Griffin
Quality Systems Coordinator
For CoA questions contact Customer Service Representative at +1-832-813-4806
AGRU AMERICA INC:GEORGETOWN
500 GARRISON RD
GEORGETOWN SC 29440
USA
Recipient: PALMER
Fax:
CoA Date: 01/16/2015
Delivery #: 88988285
Page 1 of 1
PO #: 008968
Weight: 190700 LB
Ship Date: 01/16/2015
Package: BULK
Mode: Hopper Car
Car #: CHVX890305
Seal No: 16294
Shipped To:
Certificate of Analysis
PRODUCT DATA SHEET
AT THE CORE:
This composite clay liner
is composed of a uniform
layer of granular sodium
bentonite between a
nonwoven and scrim-
nonwoven textile for
dimensional stability.
GSE BentoLiner NWL Geosynthetic Clay Liner METRIC
GSE BentoLiner “NWL” is a needlepunched reinforced composite geosynthetic clay liner
(GCL) comprised of a uniform layer of granular sodium bentonite encapsulated between
a nonwoven and a scrim-nonwoven geotextile for dimensional stability. The product is
intended for moderate to steep slopes and moderate to high load applications where in-
creased internal shear strength is required.
Product Specifications
Tested Property Test Method Frequency Value
Geotextile Property
Cap Nonwoven, Mass/Unit Area ASTM D 5261 1/20,000 m2 200 g/m2 MARV(1)
Carrier Scrim Nonwoven, Mass/Unit Area ASTM D 5261 1/20,000 m2 200 g/m2 MARV
Bentonite Property
Swell Index ASTM D 5890 1/50,000 kg 24 ml/2 g min
Moisture Content ASTM D 4643 1/50,000 kg 12% max
Fluid Loss ASTM D 5891 1/50,000 kg 18 ml max
Finished GCL Property
Bentonite, Mass/Unit Area(2)ASTM D 5993 1/4,000 m2 3.66 kg/m2 MARV
Tensile Strength(3)ASTM D 6768 1/4,000 m2 7.8 kN/m MARV
Peel Strength ASTM D 6496 ASTM D 4632(4)
1/4,000 m2 610 N/m MARV93 N MARV
Hydraulic Conductivity(5)ASTM D 5887 1/Week 5 x 10-9 cm/sec max
Index Flux(5)ASTM D 5887 1/Week 1 x 10-8 m3/m2/sec max
Internal Shear Strength(6)ASTM D 6243 Periodically 24 kPa Typical
TYPICAL ROLL DIMENSIONS
Width x Length(7)Typical Every Roll 4.7 m x 45.7 m
Area per Roll Typical Every Roll 216 m2
Packaged Weight Typical Every Roll 1,179 kg
NOTES:
• (1)Minimum Average Roll Value.
• (2)At 0% moisture content.
• (3)Tested in machine direction.
• (4)Modified ASTM D 4632 to use a 100 mm wide grip. The maximum peak of five specimens averaged in machine direction.
• (5)Deaired, deionized water @ 34.5 kPa maximum effective confining stress and 13.8 kPa head pressure.
• (6)Typical peak value for specimen hydrated for 24 hours and sheared under a 9.6 kPa normal stress.
• (7)Roll widths and lengths have a tolerance of ±1%.
GSE is a leading manufacturer and marketer of geosynthetic lining products and services. We’ve
built a reputation of reliability through our dedication to providing consistency of product, price
and protection to our global customers.
Our commitment to innovation, our focus on quality and our industry expertise allow
us the flexibility to collaborate with our clients to develop a custom, purpose-fit solution.
For more information on this product and others, please visit us at
GSEworld.com, call 800.435.2008 or contact your local sales office.
This Information is provided for reference purposes only and is not intended as a warranty or guarantee. GSE assumes no liability in connection with the use of this Information. Specifications subject to change without notice. GSE and other trademarks in this document are registered trademarks of GSE Lining Technology, LLC in the United States and certain foreign countries. REV 15JUN2012
Tremco Incorporated
3735 Green Road Beachwood, Ohio 44122 216-292-5000
Sealant/Weatherproofing Division
Tremco Mameco/VULKEM Paramount™
Technical Services
We certify that PARAGRANULAR fine granular sodium bentonite system as manufactured by Tremco Inc.
Beachwood, OH, meets the following physical properties.
Fine Granular Sodium Bentonite:
DESCRIPTION: Fine granular sodium bentonite with an average particle size ranging between 20 and 100
mesh
PURITY: Hydrous Aluminum silicate comprised principally of the clay mineral montmorilonite
90% minimum. Contains small amounts of feldspar, biotite, selenite, ect.
COMPOSITION: Typical Chemical Analysis (moisture free)
SiO3 63.02% Al2O3 21.08%
Fe2O3 3.25%
FeO 0.35%
MgO 2.67% Na2O 2.57%
CaO 0.65%
H2O 5.64%
Trace elements 0.72%
FORMULA: A tri-layer expanding mineral structure of approximately:
(Al, Fe1.67,, Mg0.33) Si4O10(OH2)Na+Ca++0.33
MOISTURE CONTENT: Maximum 12% as shipped
WATER ABSORPTION: 600% of weight minimum
Sincerely,
Wes Hensley
Wes Hensley
Technical Services Representative
cc: File/Circ.