HomeMy WebLinkAbout20130802 Ver 1_General Correspondence_20140205D w �.� 13 -ogaa
FRAC -OUT REPORT
Feature K -3 (UT to New Hope Creek)
Frac -Out Report
PSNC Durham Pipeline Project
Orange County, North Carolina
February 05, 2014
Name and company of person reporting frac -out: Ben Smith (Piedmont Utility
Group, LLC Foreman) — Contractor for'PSNC. Cell phone,number is (704) 473 - 4125.
Responsible party: Piedmont Utility Group, LLC from Shelby, NC.
Owner — Ryan Ware
Telephone (704) 473 -4840.
Contractor performing HDD: Piedmont Utility Group, LLC
Date and time of frac -out: Tuesday, February 412014 at 12:33 pm.
How'was frac -out detected: Ben Smith (Piedinont-Utility, Group, LLC - Foreman)
noticed drilling mud,at the'toe of slope and the�cul'vert extending,.undeineath Mt: Sinai
Road was completely inundated.
Location of the frac -out: Feature K =3, UT to New Hope Creek at Station 293+00.
See attached map.
Type of material: Bentonite clay and water slurry — standard HDD drilling mud.
Description of frac -out and efforts to protect sensitive areas: The drilling
operation was stopped immediately upon noticing the4rilling mud at the toe of slope.
The source ofthe drilling mud release turned out to be'through a seam in the concrete
reinforced culvert that extends,underneath Mt. ,Sinai. Tom Perez (S &ME Environmental
Inspector) was contacted immediately, and secondary containment,measures as shown,in
the attached pictures were installed to limit the migration of drilling,mud downstream and
to prevent any more from entering the stream. A back -hoe was used to dig a containment
pit as shown in Picture 1, and a pump was then installed in the containment pit in order to
recapture and recirculate'the drilling'mud- back`into the operation. Walter Cole (S &ME
Project Manager) reported incident to Chem Smith of the North Carolina Department of
Water Resources at 2:00 pm on Tuesday, February 4, 2014. Walter Cole and Tom Perez
performed an inspection together on February 5, 2014, assessing the containment
measures and documenting conditions.
Estimated size of frac =out (quantity and area): A fine layer of drilling,mud
impacted the stream for approximately 150 feet. The containment pit measured
approximately 4 feet X 4 feet X 4 feet. Due to the quick action of the contractor and
S &ME, INC. /3201 Spring Forest Road / Raleigh, NC 27616 by 919.872.2660 IF 919.876.3958 / www.smeinc.com
Wing mud "entered the, stream and due , to,the
environmentali very nspedtpr, velittle Ari
secondary containment measures,-there was ,no visible flow entering New Hope: Creek,
froffiXeattireK.J afth6 lime of M�- spectibif.
Proposed additional HDD activities: Thvdosigpedleligth of the HDD is
approximately I'000 feetand,thdiniflaID110t hole,,'•wasfcojppldte. -TlfeTracrout,occurrqd
duringIthd 115'mch,reaming,opprafion. There•wilf be Imorexeams,after,the B ihch,ream
is completed ompleted before pipe, pull back-,, and WArilLbb3, to 4 weeksbef6re,,the entire HDD. is
complete,
Proposed final, cleanup method: Omconlpletion,df 'HD.P activities, Pie&fibnt
'Utility"Group,, LLO will remove,any,drilling, mud, aq& turbid water withi , n, pri
mary, and
secondary containment areas,. ,The mfid°intCyfeqi&e,remoVAl'by hand or vacuum truck.
Upon,completioA,bf cl0an-up, activities,,sazid'bagsjh-ay bakes, gift, fende, sections, and' other
'Contadmnent,materials,will,,al'so'be=rernoved.
Party-'respons! b lie for'clean up: PiedmofttjUtilityGroupj1tLt,
General comments: IvAppearg that the drilling,mdhas beewconthindd within the
containment. it and 'the entire volume of mud coming from culvertis, being recycled back
into theArillffig operation. The,,contractor stopped dtilling-operation, acted, in good faith
- -
.to� contain the drilling hatid, and immediately notified enviid nmentaIftfonifeits,. "The,
'contractor and' inspectors, should remain alert for rain ,events and should take actions
•necessary, to contain ,drill,.miid/tiiibidwater 4n ;impadted,area. Efforts focldaii up -the
:impacted should start as,soon asprapticalfolloi0hg bore completion.'
-Attachment: Fra:d.707ut,Rep6rt�SitdPh6tbgi,-aphg I-S.
Frac-oat.Locdti6n Map.,
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