No preview available
HomeMy WebLinkAboutAQ_F_1800073_20010520_CEM_GenCorr (2) North Carolina Department of Environment and Natural Resources i Division of Air quality Technical Services Section i Michael F.Easley, Governor NCDENR William G.Ross,Jr., Secretary Alan W. Klimek,P.E.,Director May 20, 2001 Mr. Gregg Worley - Chief Operating Source Section Air and Radiation Technology Branch U.S. Environmental Protection Agency The Atlantic Federal Center, 61 Forsyth Street Atlanta, Georgia 30303 SUBJECT: Part 75 Audit Summary Report Duke Power's Marshall Steam Plant, Unit 3 Dear Ms. Pierce: . Attached is the Part 75 Level II audit report for Duke Power's Marshall Steam Plant, Unit 3 that I conducted on February 19, 2001. The audit addressed all aspects of a Level II audit including: Inspections of the CEMS, Records review and RATA observation. In general, no compliance problems involving any regulatory requirements of Part 75 were observed. The Quality Assurance manual appears complete and fully implemented. The maintenance logs as well as emission data records including missing data periods also appear complete. These records reflect correctly the daily activities on the CEM systems. If you have any questions regarding this audit,please call me at (919) 715-0726. Sincerely, Richard R. Simpson Environmental Engineer Attachment cc: Ms. Kim Nguyen, EPA Clean Air Market Division Mr. Steven Isenhour, Duke Power Designated Representative,MRO Central Files,Catawba County Mike Aldridge,NCDENR-w/o attachment 1641 Mail Service Center, Raleigh, North Carolina 27699-1641 2728 Capital Blvd., Suite 166, Raleigh, NC 27604 Phone: 919-733-1728 \ FAX: 919-733-1812 \ Internet:http://da0,state.nc.us/ AN EQUAL OPPORTUNITY \ AFFIRMATIVE ACTION EMPLOYER— 50%RECYCLED /10%POST CONSUMER PAPER Part 75 Audit Report APPENDIX A Duke Power: Marshall Steam Station Unit #3 Appendix A-1 (Section 2.2) Pre-Audit Data: Audit Date: February 19,2001 Company Name: Duke Power Plant Name: Marshall Steam Station CRIS Code: 2727 Unit ID: 3 Company Contact: Steven Isenhour Plant Contact: Cam Ritchie Phone Number: 704-373-3230 Phone Number: 828-478-2121 Address: Energy Center P.O. Box 1006 Address: 8320 East N.C. 150 Charlotte, N.C.28201-1006 Terrell, N.C. 28682 Inspector Name: Richard Simpson Phone Number: 919-715-0726 Attendee: Randy Wooten Phone Number: 704-382-6730 Representing: Duke Power Environ. Main fuel type: Coal Gas Oil Back-up/emergency fuel type: Coal Gas Oil Normal load: High Mid Low SO, (ppm) NO. (ppm) CO, (ppm) Opacity(%) Typical emission 509.2 228 12.8 14.2 Emission limit if applicable Appendix A-3 (Section 2.7) Pre-Audit Meeting Check List X Purpose of inspection X Inspection agenda X Specific areas to be observed X Safety requirements X Records to be reviewed and copying needed X Facility's policies on photography and confidentiality X Inspection and audit techniques to be used _NA System's response time X "Hands-off" policy and the need for a CEMS technician X Plant point of contact for different parts of the audit Appendix A-4 (Section 3) CEMS Inspection Probe and umbilical line (Section 3.1) YES NO Comments The probe in the same location as X when the unit was certified/recertified Any unusual event(s)that required an X explanation from the source Conditioning and dilution air systems f Section 3.2) YES NO Comments Chemical used to remove potential X Desicates and H2O. contaminants changed according to a prescribed schedule Filter changed according to schedule X Changed on a quarterly basis. Analyzer(Section 3.3) YES NO Comments System configured as it was when it X received certification/recertification Any modification to the systems that X may affected its performance Preventative Maintenance performed X according to schedule Major component replaced since X certification/recertification Span setting in the proper position X Rotameter (sample flow rate) X Setting at 5 liter/min. If out of range of 3-8, settings agreed with QA plan then alarm sounds. Also referenced in the Quality Assurance Manual(QA). Analyzer Comments S02 I.D. #301 TECO Serial No. 43H-45221-273 NO I.D.#302 TECO Serial No. 42D-46848-276 Diluent C0)02 I.D. #303 TECO Serial No. 41 H-46117-275 Flow I.D. #304 Panametrics CEM68 Serial No. 170 Opacity I.D. #305 United Sciences 500C Serial No. 0993672 Appendix A- 4 (Section 3) Page 2 CEMS Inspection (Cont.) Accessories (Section 3.4) Gas Cylinder Cert. Type of gas Cylinder Expiration Certificate on No. Conc. (SRM/CRM/GMIS/Protocol) Pressure Date file NOx CC52136 819.33 Triblend High gas 800 3/9/01 Yes S02 " " 1460 " " " " " " " " CO2 It It 1 6.6% i{ „ f{ „ f{ „ i{ It NOx CC117317 556.42 Triblend Bias Gas 600 11/9/01 Yes S02 It " 963 " ,1 iL 11 ff „ " It CO2 It It 11.2% « O2 CC59907 12.6% Mid Gas 600 10/22/01 Yes Regulators: Are correct type of regulators used? YES NO Are the regulators damaged? YES NO Data Acquisition and Handling System (Section 3.5) How is the daily calibration recorded? Automatically through DAHS. How are the linearity, RATA tests results recorded? Automatically on DAHS. When and how frequent does the source back up the data? Twice per week with backup tape and electronically. YES NO Comments or explanation Are all pertinent data recorded? X Is any data input by hand? If so, does X DAHS data agree with hard copy data? Can the source display last missing X dataperiod? I Appendix A-5 (Section 4.1) Quality Assurance Records Review Does the source have a written CEMS QA Plan? YES NO Did the sources have difficulty locating it? YES NO Date of the most recent update: 4/1/00- Revision 4 Comments: None Do the following items appear in the CEMS QA Plan?: YES NO Comments or explanation Calibration error test X In section 6.3 pg. 21 of QA Manual. procedures Linearity check procedures X In section 7.1 pg. 26 of QA Manual and Appendix B. Calibration adjustment X In section 6.3 pg.24 of QA Manual. procedures Linearity adjustment X In section 7.1 pg.26 and Appendix B of QA Manual. procedures RATA procedures X In section 7.2 pg.29 of QA Manual. Corrective maintenance RATA X In section 7.2 pg.29 and section 7.2.8 of QA Manual. procedures Preventive Maintenance X In section 8 pg.30 of QA Manual. procedures Spare parts list NA Troubleshooting matrix X In Figure 8-10 pg.51 of QA Manual. Record keeping and reporting X In section 9 pg. 52 of QA Manual. Add-on emission control(s) X Existing ESP. information (if applicable) Appendix A-6 (Section 4.2) Maintenance Log review Comments: None Do the following items appear in the Maintenance Log?: being followed Comments or explanation daily preventive X In section 8.3 pg. 32 &figure 8-2 pg. 34 of QA Manual. maintenance Last performed on 2/19/01. weekly preventive X In section 8.3 pg. 32 of QA Manual and Figure 8 pg. 35. Last maintenance performed on 2/19/01. monthly preventive X NA maintenance quarterly preventive X In section 8.3 pg. 32 of QA Manual and Figure 8-5 pg. 37. maintenance Last performed on 2/8/01. semi-annual preventive X In section 8.3 pg. 32 & 37 of OA Manual and Figure 8-5 maintenance pg.38. Last performed on 7/19/01. annual preventive X In section 8.3 pg. 32 of QA Manual and Figure 8-5 pg. 39. maintenance Last performed on 2/23/00. I I ( I 5 Amount of maintenance log reviewed: 90 (# of days) Indicate if the following items appeared in the Maintenance Log: YES NO N/A Comments Recurring failures or malfunctions X Repeated adjustments to the zero X and/or span Parts replacement and/or adjustment X Annually rebuild pumps as preventive maintenance. Analyzer, DAHS replacement X Performance evaluations, stack tests X Corrective actions for malfunctions, X calibrations, etc. Pre-RATA (adjustments before X RATA) Reported monitor availability X Availability 99%. 1 I Appendix A-7 (Section 4.3) Emissions Data Records Review Amount of data reviewed: 90 (#of days) from:_1/01/01_to: 2/19/01 YES NO Comment Reported emission values were X NOx on 2/6/01 at 14:00. correctly adjusted Code 13 Analyzer failure. Daily calibrations conducted X Linearity test conducted as required X RATA/Bias test conducted as X required Is the source in compliance with the Not Applicable. NOx emission limit if applicable? Missing data period(s) identified in X Value was verified. the quarterly report Missing period(s) agreed with the X quarterly report data Correct values used during missing X data period(s) Data missing period agrees with the X Value was verified. maintenance log data Method of deterrnination code is X correctly applied Event(s) in the maintenance log X book reflected in the quarterly report Any unusual event(s) required X explanation from the source If a back up monitor was used, is NA- No backup. there an explanation as to why the primary monitor wasn't used? Appendix A-8 (Section 5) Daily Calibration Summary Plant: Duke Power-Marshall Steam Station State: NC ORIS Code: 2727 Common Stack or NADB Boiler ID(s):_Unit 3 If offline calibrations are done,was the offline-online test passed? NA System/Component ID: 301 _ Parameter Monitored: S02 Span Value,S: 1700 CE Results Date/time Calibration Value,R CEM Response,A (ppm,%, SCFH or fpm) (ppm,%,SCFH or fpm) (%of span) R-A (ppm,%,SCFH or fpm) Zero level check 2/19/01 253 252.2 0.0 Upscale check 7:05 AM 1440 1453.0 0.8 System/Component ID: 302 _ Parameter Monitored:_ NOx Span Value,S: 600 CE Results Date/time Calibration Value, R CEM Response,A (ppm,%, SCFH or fpm) (ppm,%,SCFH or fpm) (%of span) R-A (ppm,%,SCFH or fpm) Zero level check 2/19/01 91.7 91.3 0.1 Upscale check 7:05 AM 523.0 527.0 0.7 System/Component ID: 303 Parameter Monitored: CO2 Span Value,S: 20 CE Results Date/time Calibration Value, R CEM Response,A (ppm,%, SCFH or fpm) (ppm,%, SCFH or fpm) (%of span) R-A (ppm,%,SCFH or fpm) Zero level check 2/19/01 3.0 3.2 0.2 System/Component ID: Parameter Monitored: Span Value,S: CE Results Date/time Calibration Value, R CEM Response,A (ppm,%, SCFH or fpm) (ppm,%, SCFH or fpm) (%of span) R-A (ppm,%,SCFH or fpm) Zero level check Upscale check For NOx and SO.: CE = IN - Al x 100 S For CO2 and 02: CE = IR - AI where: CE = Calibration Error(%of span) A = Actual CEMS Response R = Reference Gas Value S =CEMS Span Value Appendix A-10 (Section 6.2) Page of Gas CEMS RATA Performance Plant:Duke Power:Marshall Steam Station State: NC ORIS Code:2727 Common Stack or NADB Boiler ID#(s): Unit 3 System ID: 301--304 Parameter Monitored:S02/NOx/CO2/Flow GENERAL TEST INFORMATION REQUIRED OPTIONAL INFORMATION INFORMATION Test Date 2/19/01 Was a calibration error check conducted on the source CEMS prior YES to initiating the RATA? Were the check results acceptable? YES Document the zero and upscale calibration error results for the day: ZERO: UPSCALE: Were any pre RATA adjustments made? NO Is the reference measurement system set-up consistentwith the YES system described within the test protocol? Verify calibration gas concentrations and certifications: YES Optional RM sampling system leak check conducted? YES Acceptable pre-test linearity check? YES Three-point RM sample traverse conducted during test runs? NO Traverse point locations(measured in reference to stack wall(ft.,in.) or as a%of diameter): (1)80.75" (2)112.25" (3)143.75" RM calibration checks conducted between test runs? YES Drift checks acceptable for observed test runs? YES Sampling system bias checks acceptable for observed test runs? YES No prohibited maintenance or adjustments made during the test? No (Part 75,App.A,Sec. 6.5) Was the primary fuel combusted during test? (Part 75,App.A,Sec. YES,Coal 6.5) Total number of RATA test runs observed: 5 Data reduction activities performed on-site by the test contractor? YES Reference measurement data (corrected for drift and bias)collected YES by the observer? (see RATA Field Data Forms) Relative accuracy results calculated on-site? YES Plant operated during RATA outlined in test protocol? YES Source CEMS concentration data reported by the DAHS on a wet or Wet dry basis? Relative Accuracy Result Reviewer Name: Richard Simpson Agency:NCDENR-DAQ Signature: Date Review Completed:2/19/01 Appendix A-11 (Section 6.2) Page of Flow Rate Monitor RATA Performance Plant::Duke Power: Marshall Steam Station State: NC ORIS Code:2727 Common Stack or NADB Boiler ID(s): Unit 3 System ID: 304 Peaking/Bypass Unit NA GENERAL TEST INFORMATION REQUIRED OPTIONAL INFORMATION INFORMATION Were any pre RATA adjustments made? NO Were any adjustments made to the monitor during the test? NO RM pitot type(i.e.,Type S,standard,etc.): I S-TYPE Differential pressure readout device(i.e.,manometer): Manometer Is the reference measurement system set-up consistent with YES the system described within the test protocol? How is moisture determined? METHOD 4 How often is moisture determined? EVERY RUN Was an optional pre-test pitot system leak check conducted? ) YES Cross-sectional area: I - -- Numberof RM traverse points: 12 RM traverse points in accordance with EPA Method 1? ) YES RM results calculated on-site by the test contractor? YES RM and flow rate monitor data corrected to wet standard I YES conditions? Relative accuracy result calculated on-site? YES LOAD-LEVEL SPECIFIC INFORMATION Low Load Normal Load High Load Test Date 2/19/01 Boiler unit load level(MW): 690 Cyclonic flow checked? NA Post-test pitot system leak check conducted?(mandatory) YES Post-test Method 4 leak check conducted? YES Number of RM test runs observed: 5 Relative Accuracy Result See comments. COMMENTS: Initial final results:S02-1.0%,NOx-1.9%,CO2-0.6%, Flow(high)-1.8% Reviewer Name: Rich rd Simpson Agency: NCDENR-DAQ Signature: � Date Review Completed: 2/19/01